Crash of a Lockheed L-188C Electra near Tell City: 63 killed

Date & Time: Mar 17, 1960 at 1525 LT
Type of aircraft:
Operator:
Registration:
N121US
Flight Phase:
Survivors:
No
Schedule:
Minneapolis – Chicago – Miami
MSN:
1057
YOM:
1959
Flight number:
NW710
Crew on board:
6
Crew fatalities:
Pax on board:
57
Pax fatalities:
Other fatalities:
Total fatalities:
63
Captain / Total flying hours:
27523
Captain / Total hours on type:
254.00
Copilot / Total flying hours:
2974
Copilot / Total hours on type:
200
Aircraft flight hours:
1786
Circumstances:
The four engine aircraft departed Chicago-Midway at 1438LT bound for Miami, carrying 57 passengers and a crew of six. While cruising at an altitude of 18,000 feet over the south of Indiana State, the aircraft entered a dive and crashed in a huge explosion in a snow covered field located east of Tell City. Some debris were also found in a wooded area. The aircraft disintegrated on impact and all 63 occupants were killed. The crew was unable to send any distress call prior to the accident.
Probable cause:
The Board determines that the probable cause of this accident was the separation of the right wing in flight due to flutter induced by oscillations of the outboard nacelles. Contributing factors were a reduced stiffness of the structure and the entry of the aircraft into an area of severe clear air turbulence.
Final Report:

Crash of a Lockheed L-188A Electra near Buffalo: 34 killed

Date & Time: Sep 29, 1959 at 2309 LT
Type of aircraft:
Operator:
Registration:
N9705C
Flight Phase:
Survivors:
No
Schedule:
Houston – Dallas – Washington DC – New York
MSN:
1090
YOM:
1959
Flight number:
BN542
Location:
Crew on board:
6
Crew fatalities:
Pax on board:
28
Pax fatalities:
Other fatalities:
Total fatalities:
34
Captain / Total flying hours:
20726
Captain / Total hours on type:
68.00
Copilot / Total flying hours:
11316
Copilot / Total hours on type:
95
Aircraft flight hours:
132
Circumstances:
Flight 542 departed the ramp at Houston at 2237LT, 22 minutes behind schedule with a total of 34 persons including a crew of six consisting of Captain Wilson Elza Stone, First Officer Dan Hollowell, Second Officer Roland Longhill, and Stewardesses Alvilyn Harrison, Betty Rusch and Leona Winkler, none of whom survived. The delayed departure was due to a mechanical discrepancy involving No. 3 generator. This generator was inoperative on arrival of N9705C at Houston. Prior to departure from Houston the Nos. 3 and 4 voltage regulators were interchanged. Actual gross weight upon departure was calculated at 83,252 pounds, including 17,000 pounds of fuel, and was 16,548 pounds less than the authorized gross weight of 99,800 pounds. The estimated time en route to Dallas was 41 minutes. The flight was given an instrument-flight-rules clearance which was to the Leona omni, via Victor Airway 13 west to the Gulf Coast intersection, direct to Leona, to maintain 2,300 feet altitude to Gulf Coast, then to climb to and maintain 9,000. At approximately 2240 the flight was cleared for takeoff and at 2242 it reported ready for takeoff and was airborne at 2244. After takeoff Houston departure control advised that it had the flight in radar contact and requested it to report when established outbound on the 345-degree radial of the Houston omni. Flight 542 complied and subsequently was cleared to 9,000 feet and advised to contact San Antonio Center on 121.1 mcs. upon passing the Gulf Coast intersection. Flight 542 reported to company radio at 2251 as blocking out of Houston at 37, taking off at 42, to cruise at 15,000 feet when so cleared, estimating Dallas at 2325, and that the Center had this information. At approximately 2252 Flight 542 reported to San Antonio Center as being over Gulf Coast intersection at 9,000 feet. The flight was then issued its destination clearance to the Dallas Airport via direct to Leona, direct to Trinidad, direct to Forney, direct to Dallas, to maintain 15,000 feet. The flight was cleared to climb to its cruising altitude. The next transmission from Flight 542 was to the San Antonio, Center, giving the time over Leona as 05 at 15,000. San Antonio Center acknowledged, and requested Flight 542 to change over and monitor the Fort Worth frequency of 120.8 mcs. at this time. The flight acknowledged. Shortly thereafter Flight 542 contacted company radio with a message for maintenance, advising that the generators were then OK out that there had been insufficient time for maintenance to insulate the terminal strip on No. 3 propeller at Houston and it would like to have it done in Dallas. At this time the flight also said it would give the communication center a Dallas estimate of 25. This was then followed by one other item for maintenance, which was that No. 3 sump pump was inoperative. This was the final transmission from the flight and was logged as completed at 2307. Structural failure of the aircraft occurred at approximately 2309 on course to the next fix, Trinidad intersection. The radial from Leona omni to Trinidad intersection is 344 degrees. The main wreckage was located 19.7 miles 2 north of Leona omni, 3.19 miles east-southeast of Buffalo, Texas. The time, 2309, correlates closely with the information obtained from witnesses to the accident as well as the time indicated on impact-stopped watches recovered at the scene. The aircraft was destroyed upon impact and all 34 occupants were killed.
Probable cause:
The Board determines that the probable cause of this accident was structural failure of the left wing resulting from forces generated by undampened propeller whirl mode.
Final Report:

Crash of a Lockheed L-188A Electra in New York: 65 killed

Date & Time: Feb 3, 1959 at 2356 LT
Type of aircraft:
Operator:
Registration:
N6101A
Survivors:
Yes
Schedule:
Chicago – New York
MSN:
1015
YOM:
1958
Flight number:
AA320
Crew on board:
5
Crew fatalities:
Pax on board:
68
Pax fatalities:
Other fatalities:
Total fatalities:
65
Captain / Total flying hours:
28135
Captain / Total hours on type:
48.00
Copilot / Total flying hours:
10192
Copilot / Total hours on type:
36
Aircraft flight hours:
302
Circumstances:
At approximately 2356LT, the aircraft crashed into the East River while attempting an instrument approach to runway 22 at LaGuardia Airport. There were 73 persons on board, including one infant. The captain and one stewardess were killed; the first officer, flight engineer, and the remaining stewardess survived. Of the 68 passengers, 5 survived. The Board believes that a premature descent below landing minimums was the result of preoccupation of the crew on particular aspects of the aircraft and its environment to the neglect of essential flight instrument references for attitude and height above the approach surface. Contributing factors were found to be: limited experience of the crew with the aircraft type, fealty approach technique in which the autopilot was used in the heading mode to or almost to the surface, erroneous setting of the captain's altimeter, marginal weather in the approach area, possible misinterpretation of altimeter and rate of descent indicator, and sensory illusion with respect to height and attitude resulting from visual reference to the few lights existing in the approach area.
Probable cause:
The Board determines the probable cause of this accident was premature descent below landing minimums which was the result of preoccupation of the crew on particular aspects of the aircraft and its environment to the neglect of essential flight instrument references for attitude and height above the approach surface. Contributing factors were:
- Limited experience of the crew with the aircraft type,
- Faulty approach technique in which the autopilot was used in the heading mode to or almost to the surface,
- Erroneous setting of the captain's altimeter,
- Marginal weather in the approach area,
- Possible misinterpretation of altimeter and rate of descent indicator,
- Sensory illusion with respect to height and attitude resulting from visual reference to the few lights existing in the approach area.
Final Report: