Crash of a Vickers 745D Viscount in Chase: 31 killed

Date & Time: May 12, 1959 at 1613 LT
Type of aircraft:
Operator:
Registration:
N7463
Flight Phase:
Survivors:
No
Schedule:
New York – Atlanta
MSN:
287
YOM:
1957
Flight number:
CA075
Location:
Crew on board:
4
Crew fatalities:
Pax on board:
27
Pax fatalities:
Other fatalities:
Total fatalities:
31
Captain / Total flying hours:
22260
Captain / Total hours on type:
1945.00
Copilot / Total flying hours:
4073
Copilot / Total hours on type:
2033
Aircraft flight hours:
4180
Circumstances:
Flight 75 taxied away from the terminal at 1520, 20 minutes late. The last-minute delay occurred when Captain Paddack found an error in the aircraft gross weight computation and questioned the weight for the existing runway restriction. At 1455 the flight radioed for runway temperature. The senior operations agent came aboard and he and the captain rechecked the computations to make sure the weight was correct and below maximum allowable for the runway length, the existing surface wind, and temperature. The problem was satisfied and it was determined that the gross weight was 60,507 pounds, 103 pounds less than the maximum allowable of 60,610 pounds. During taxi Flight 75 was issued an instrument clearance according to an instrument flight rules flight plan filed earlier. At 1529 a no takeoff from runway 22 was observed. Executing the clearance, Flight 75 made numerous radio communications in the New York area and proceeded uneventfully to its assigned cruising altitude. 14,000 feet, and onto the assigned airway Victor 3. Regular position reports were made as the flight progressed. At 1602 Flight 75 contacted the Washington Center. It reported that it was over Westchester on the hour, 1600, at 14,000, estimating Westminster at 1617, with Herndon next. In the same message it advised, ". . . ah, we've got a pretty good string of thunderstorms along that course . . . ah, if we could stay in the clear and stay a little bit south of Westminster, is that O. K. with you?" The center controller replied "Capital 75, that'll be all right and report passing Westminster." The flight acknowledged. At 1610 the flight advised, "Ah, Washington Center, this is Capital 75, we've reduced to one seven zero knots account rough air." This was the last message from the flight on the center recorders and the last which could be determined as having been made. The aircraft entered a near vertical dive, partially disintegrated at an altitude between 3,000 and 7,000 feet and eventually crash in Chase, two miles northeast of Martin Airport. The aircraft was totally destroyed and all 31 occupants were killed.
Probable cause:
The Board determines that the probable cause of this accident was a loss of control of the aircraft in extreme turbulence resulting in an involuntary steep descent following which aerodynamic loads from high airspeed, recovery, and turbulence exceeded the design strength of the aircraft.
Final Report:

Crash of a Convair CV-240-0 in Chicago

Date & Time: Mar 15, 1959 at 0053 LT
Type of aircraft:
Operator:
Registration:
N94273
Flight Type:
Survivors:
Yes
Schedule:
New York – Chicago
MSN:
150
YOM:
1949
Flight number:
AA2815
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8500
Captain / Total hours on type:
2500.00
Copilot / Total flying hours:
1800
Copilot / Total hours on type:
800
Aircraft flight hours:
22720
Circumstances:
The crew was completing a cargo flight from LaGuardia Airport to Midway Airport in Chicago. On final approach to runway 31, the captain considered his position was incorrect and decided to make a go around. Few minutes later, during a second attempt to land, he failed to realized his altitude was insufficient when the airplane struck a 96-foot steel tower, stalled and crashed in flames on a railroad located about 0,9 mile short of runway 31 threshold. The aircraft and the cargo were destroyed by a post crash fire while both pilots were uninjured.
Probable cause:
The Board determines that the probable cause of this accident was the pilot’s descent below his allowable minimum altitude and his inattention to flight instruments while attempting to locate the runway visually. The Board concludes that this accident was brought about by the captain’s disregard of the minimum altitude during instrument flight. It is evident that he was attempting visually to locate the runway tile flying at a low altitude under conditions of restricted visibility.
Final Report:

Crash of a Lockheed L-188A Electra in New York: 65 killed

Date & Time: Feb 3, 1959 at 2356 LT
Type of aircraft:
Operator:
Registration:
N6101A
Survivors:
Yes
Schedule:
Chicago – New York
MSN:
1015
YOM:
1958
Flight number:
AA320
Crew on board:
5
Crew fatalities:
Pax on board:
68
Pax fatalities:
Other fatalities:
Total fatalities:
65
Captain / Total flying hours:
28135
Captain / Total hours on type:
48.00
Copilot / Total flying hours:
10192
Copilot / Total hours on type:
36
Aircraft flight hours:
302
Circumstances:
At approximately 2356LT, the aircraft crashed into the East River while attempting an instrument approach to runway 22 at LaGuardia Airport. There were 73 persons on board, including one infant. The captain and one stewardess were killed; the first officer, flight engineer, and the remaining stewardess survived. Of the 68 passengers, 5 survived. The Board believes that a premature descent below landing minimums was the result of preoccupation of the crew on particular aspects of the aircraft and its environment to the neglect of essential flight instrument references for attitude and height above the approach surface. Contributing factors were found to be: limited experience of the crew with the aircraft type, fealty approach technique in which the autopilot was used in the heading mode to or almost to the surface, erroneous setting of the captain's altimeter, marginal weather in the approach area, possible misinterpretation of altimeter and rate of descent indicator, and sensory illusion with respect to height and attitude resulting from visual reference to the few lights existing in the approach area.
Probable cause:
The Board determines the probable cause of this accident was premature descent below landing minimums which was the result of preoccupation of the crew on particular aspects of the aircraft and its environment to the neglect of essential flight instrument references for attitude and height above the approach surface. Contributing factors were:
- Limited experience of the crew with the aircraft type,
- Faulty approach technique in which the autopilot was used in the heading mode to or almost to the surface,
- Erroneous setting of the captain's altimeter,
- Marginal weather in the approach area,
- Possible misinterpretation of altimeter and rate of descent indicator,
- Sensory illusion with respect to height and attitude resulting from visual reference to the few lights existing in the approach area.
Final Report:

Crash of a Convair CV-240-2 in Nantucket: 25 killed

Date & Time: Aug 15, 1958 at 2334 LT
Type of aircraft:
Operator:
Registration:
N90670
Survivors:
Yes
Schedule:
LaGuardia – Nantucket
MSN:
90
YOM:
1948
Flight number:
NE258
Crew on board:
3
Crew fatalities:
Pax on board:
31
Pax fatalities:
Other fatalities:
Total fatalities:
25
Captain / Total flying hours:
5603
Captain / Total hours on type:
1416.00
Copilot / Total flying hours:
614
Copilot / Total hours on type:
132
Aircraft flight hours:
18019
Circumstances:
During a night approach to Nantucket, the aircraft went through an area of fog. The crew decided to continue the approach when the airplane struck the ground, crashed and burned about 1,450 feet short of runway 24. All three crew members and 22 passengers were killed while nine others were injured, some of them seriously.
Probable cause:
The Board determines that the probable cause of this accident was the deficient judgment and technique of the pilot during an instrument approach in adverse weather conditions in failing to abandon the approach when a visibility of one-eights mile was reported, and descending to a dangerously low altitude while still a considerable distance from the runway.
Final Report:

Crash of a Douglas DC-6A in New York: 20 killed

Date & Time: Feb 1, 1957 at 1802 LT
Type of aircraft:
Operator:
Registration:
N34954
Flight Phase:
Survivors:
Yes
Schedule:
New York – Miami
MSN:
44678
YOM:
1955
Flight number:
NE823
Crew on board:
6
Crew fatalities:
Pax on board:
95
Pax fatalities:
Other fatalities:
Total fatalities:
20
Captain / Total flying hours:
16630
Captain / Total hours on type:
85.00
Copilot / Total flying hours:
8943
Copilot / Total hours on type:
17
Aircraft flight hours:
8317
Circumstances:
Northeast Airlines Flight 8232 a DC-6A, N34954, was scheduled to originate at La Guardia Field, a nonstop to Miami, Florida, with a departure time of 1445. This aircraft and the same crew operating as Flight 822, had arrived at LaGuardia from Miami at 1250. The crew consisted of Captain Alva V. R. Marsh, First Officer Basil S. Dixwell, Flight Engineer Angelo V. Andon, and Stewardesses Doris Steele, Catherine Virchow, and Emily Gately. A short time before the scheduled departure time the crew and passengers boarded the aircraft. Snow, which had started at LaGuardia at 1202, began to accumulate on the aircraft's horizontal surfaces after its arrival at the LaGuardia ramp position. Snow removal by ground personnel, during preflight, was ineffective because of the continuing snowfall. Accordingly, about 1600 the aircraft was taxied, with all occupants aboard, to a nose hangar on the west side of the airport for snow removal. This was accomplished and at 1745 the crew advised LaGuardia ground control that they were ready to taxi from the nose hangar for the IFR, departure to Miami. Flight 823 was then cleared to runway 4 and was advised that the wind was northeast 10, the altimeter setting 30.12, and a time check of 1747-1/2. Air Route Traffic Control cleared the flight as follows. "Cleared to Bellemead, maintain 7,000 feet." A supplementary climb-out clearance was then given: "After takeoff, a left turn direct Paterson, direct Chatham, cross 081-degree radial of Caldwell 4,000 feet or above, cross Paterson between 5,000 and 6,000 feet and cross the northwest course of Idlewild not above 6,000 feet." Both clearances were repeated and acknowledged. Takeoff clearance was issued at 1800 and a tower controller saw the aircraft airborne at approximately 1801.2 The controller advised the flight to contact LaGuardia radar departure control on 120.4 mcs. This message was acknowledged but the radar controller did not receive a call from the flight; however, he did observe a target on the scope that indicated an aircraft over the runway. The next two sweeps on the scope disclosed the target beyond the end of the runway. A subsequent sweep indicated that the target was turning left. The target then disappeared from the scope. The LaGuardia tower controllers observed a large flash at approximately 1802 in the vicinity of Rikers Island, the approximate center of which is about one mile north of the point where the aircraft left the runway. It was learned at 1819, by telephone, that Northeast Airlines Flight 823 had crashed on Rikers Island. The airplane was destroyed by a post crash fire and 20 passengers were killed.
Probable cause:
The Board determines that the probable cause of the accident was the failure of the captain to (1) properly observe and interpret his flight instruments and (2) maintain control of his aircraft. The following findings were reported:
- The weather at the time of takeoff was above the prescribed company minimums,
- The aircraft, immediately following takeoff, made a left turn of approximately 119 degrees and a descent,
- The pilot and flight crew did not observe or interpret any instrument indication of a left turn or descent,
- The heading indications of both fire-seized course indicators corresponded closely to the impact heading of the aircraft,
- These instruments had been functioning properly until the time of impact,
- There was no failure or malfunction of the powerplants,
- There was no airframe failure or control malfunction,
- There was no electrical power failure or malfunction of instruments prior to ground impact,
- There was no fire prior to ground impact,
- As a result of fuselage deformation the main cabin door jammed, hindering evacuation of passengers,
- The main cabin lighting system became Inoperative during deceleration and the emergency inertia lights did not actuate.
Final Report:

Crash of a Douglas DC-6 in Ronkonkoma: 3 killed

Date & Time: Apr 4, 1955 at 1555 LT
Type of aircraft:
Operator:
Registration:
N37512
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
New York-Idlewild – Ronkonkoma – LaGuardia
MSN:
43001
YOM:
1947
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
9763
Captain / Total hours on type:
549.00
Copilot / Total flying hours:
9018
Copilot / Total hours on type:
1156
Aircraft flight hours:
22068
Circumstances:
N37512, under the command of Captain S. C. Hoyt, UAL New York area flight manager, departed New York International Airport at 1428 on a Visual Flight Rules flight plan for an estimated two-hour flight in the vicinity of MacArthur Field, Islip. The aircraft was properly dispatched on a routine check flight, and Captains V. H. Webb and H. M. Dozier were aboard for the purpose of receiving their periodic instrument proficiency check. Upon completion of the checks, the flight was scheduled to return to LaGuardia Airport. At 1501 the flight reported to the company by radio that they were “doing air work around Hempstead.” Another message was received by the company at 1527 reporting that the flight was going to make an ILS (Instrument Landing System) approach at Islip (MacArthur Field). Shortly thereafter, the flight contacted the MacArthur tower, requesting approval for an ILS approach and landing. Permission was granted by the tower, and a normal landing was made on runway 32. The aircraft was taxied to the intersection of runways 28 and 32 and the crew prepared for takeoff. The 1532 MacArthur weather observation showed scattered clouds at 20,000 feet, broken clouds at 25,000; visibility over 15 miles; temperature 53; dew-point 30; wind NNW at 20 knots, gusts to 30 knots. When the flight departed New York International Airport, weather was approximately the same and the forecast for the New York area indicated that it would be similar over the area for the duration of the flight. At 1548, the MacArthur controller cleared the flight to take position on runway 32 and take off. The aircraft took position on the runway but did not immediately take off, hence a second takeoff clearance was transmitted at 1550. The gross weight of the aircraft at takeoff from MacArthur Field was approximately 61,050 pounds, which was well below the maximum allowable. The load was correctly distributed with respect to center of gravity limits. The aircraft became airborne approximately, 1,500 to 1,800 feet down the runway. The takeoff appeared normal, as did the initial portion of the climb, and the aircraft remained on the runway heading. When about 50 feet high, the right wing lowered and the aircraft started turning to the right, at which time the landing gear was retracting. The aircraft continued a climbing turn and the degree of bank increased to approximately vertical by the time the heading changed about 90 degrees and the aircraft had attained an estimated altitude of 150 feet. The nose dropped sharply and the aircraft dived into the ground, striking on the right wing and nose. It then cartwheeled and came to rest right side up. An intense fire started and consumed a large portion of the wreckage in spite of the prompt arrival of fire fighting equipment on the field.
Probable cause:
The Board determines that the probable cause of this accident was unintentional movement of No. 4 throttle into the reverse range just before breaking ground, with the other three engines operating at high power output, which resulted in the aircraft very quickly becoming uncontrollable once airborne. The following findings were reported:
- No evidence of failure or malfunctioning of the structure powerplants, propellers, or electrical system was found,
- In reducing power to zero thrust during an instrument takeoff with a simulated engine out, No. 4 propeller was unintentionally reversed before the aircraft became airborne,
- Evidence indicated that No. 4 throttle was moved out of reverse by the pilot into the forward position in an attempt to unreverse, but the reverse warning flag was not lifted, resulting in increased reverse thrust,
- An outboard propeller on a DC-6 reversing as the aircraft becomes airborne, in conjunction with high power output of the other three engines, at takeoff configuration and airspeed causes the aircraft to become almost immediately uncontrollable,
- There was insufficient time and altitude for any pilot corrective measures to become effective.
Final Report:

Crash of a Lockheed 18-56-24 LodeStar in Marlborough: 1 killed

Date & Time: Nov 5, 1954 at 1942 LT
Type of aircraft:
Operator:
Registration:
N9201H
Flight Type:
Survivors:
Yes
Schedule:
LaGuardia – Boston
MSN:
2353
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
8700
Captain / Total hours on type:
200.00
Copilot / Total flying hours:
1600
Copilot / Total hours on type:
600
Aircraft flight hours:
1500
Circumstances:
At approximately 1845, N9201H departed LaGuardia Airport, New York, on a VFR (Visual Flight Rules) flight to Logan Airport, Boston, Massachusetts. The crew consisted of Captain John K. MacKenzie and Copilot Whitney H. Welch. The passengers were Robert W. Mudge, Raymond J. Halloran, both airline pilots, and Mathew C. Abbott, an electrical engineer. Climbing to an altitude of 3,500 feet m. s. l. (mean sea level), the flight proceeded toward Boston. Approximately 12 miles southeast of Hertford, Connecticut, the right engine became very rough and backfired frequently. The captain was unable to correct this condition and later feathered the right propeller when in the vicinity of Willimantic, Connecticut. A wide right turn was made from a northeasterly to a northwesterly heading toward Bradley Field, Windsor Locks, Connecticut. Communication was established with Bradley Field and the flight was cleared for a straight-in approach to runway 33. The aircraft descended to 2,500 feet m. s. l. during the turn and thereafter continued descending on a northwest heading until it struck trees and crashed. Nearby residents quickly reached the scene, gave assistance and notified authorities. The Bradley Field 1930 weather was: Scattered clouds at 4,500 feet, visibility 15 miles plus, temperature 40 degrees, dewpoint 32, wind northwest 6 m. p. h. La Guardia weather at the time of departure was: Ceiling unlimited, visibility 15 miles plus. Conditions en route were clear with excellent visibility. The twin engine airplane was the property of Mr. John Fox.
Probable cause:
The Board determines that the probable cause of this accident was that after failure of the right engine, accepted single-engine procedure was not followed, which resulted in the aircraft losing altitude and striking the ground. The following findings were reported:
- Weather was not a factor in the accident,
- A structural failure occurred in the power section of the right engine that necessitated feathering of the right propeller,
- Failure to attain single-engine performance resulted in loss of altitude,
- Mechanical difficulties in the left engine reduced power but remaining available power was sufficient for single-engine performance.
Final Report:

Crash of a Convair CV-240-13 in New York-La Guardia

Date & Time: Jan 14, 1952 at 0903 LT
Type of aircraft:
Operator:
Registration:
N91238
Survivors:
Yes
Schedule:
Boston – New York
MSN:
158
YOM:
1949
Flight number:
NE801
Crew on board:
3
Crew fatalities:
Pax on board:
33
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
13849
Captain / Total hours on type:
2382.00
Copilot / Total flying hours:
5100
Copilot / Total hours on type:
700
Aircraft flight hours:
5962
Circumstances:
Flight 801 originated at Boston, Massachusetts, for LaGuardia Field, nonstop, with a crew of Captain A. V. R. Marsh, First Officer Austin Officer Austin E. Briggs, and Stewardess Carolyn Mc Hull. It departed Boston at 0745, as schedules, in accordance with Instrument Flight Rules, via Airways Amber 7 and Red 3 to LaGuardia, Idlewild (New York International) Airport was the specified alternate. Upon departure from Boston the aircraft's gross weight was 38, 23 pounds, with a maximum allowable weight of 39,650 pounds, and the center of gravity was within prescribed limits. The flight proceeded uneventfully at its assigned altitude of 6,000 feet MSL in instrument weather with almost continuous rain. No actual icing occurred although the aircraft's de-icing equipment was used as a precaution because of the near freezing air temperatures. All required position reports were routine. At approximately 0845, the flight contacted LaGuardia approach control and advised, "Northeast 801 over New Canaan - cleared to New Rochelle." (The flight had been cleared to New Rochelle by ARTC.) Approach control then requested the flight to report over the Port Chester, New York, fan marker, and gave it an expected approach clearance time of an the hour (0900), Runway 22, and the 0828 LaGuardia weather, as follows: "estimated 3,000 overcast, one end one-half miles, rain and smoke, Wind southeast six, altimeter zero-zero-zero" (30.00). The light reported over Port Chester at 0849 and was successively cleared to descend to 4,500 foot, to 3,500 foot, and to 2,500 foot altitudes. At 0855 it was cleared to leave New Rochelle, inbound, and shortly was instructed to make a 360-degree turn to assure separation from a preceding aircraft. The flight acknowledged and complied. At 0858 it reported leaving New Rochelle and was cleared for an approach to Runway 22, and at 0859, was told that Ground Control Approach advisories were available on a frequency of 109.9 megacycles. The flight acknowledged, and then was given the 0900 LaGuardia weather, ceiling 1,700 feet and visibility 1 1/2 miles. Flight 801 reported leaving the LaGuardia range at 0900 and was cleared to land on Runway 22. There was no further message from the flight. At 0903 it struck the water of Flushing Bay some 3,600 feet from the approach end of Runway 22. A motorboat operated by the Edo Corporation, docked about one-half mile away, reached the site approximately four minutes later. Passengers and crew, who had climbed out through the emergency exits and who were standing on and holding to the fat sinking aircraft, were taken aboard and then transferred to a tugboat that arrived shortly. All occupants were taken ashore and hospitalized.
Probable cause:
The Board determined that the probable cause of this accident was the failure of the captain in command to monitor the copilot's approach and take corrective action when the aircraft first went appreciably below a normal approach path. The following findings were pointed out:
- The weather data included a coiling of 1,700 feet and visibility of 1 1/2 miles,
- Authorized minimum ceiling and visibility for the subject approach were 500 feet and one mile, respectively,
- Instrument weather was encountered during the approach,
- The approach was continued visually, despite the instrument weather,
- Air speed was decreased and the aircraft settled rapidly to the water at 0903,
- There was no malfunctioning or failure of the aircraft, or any of its components.
Final Report:

Crash of a Douglas DC-3-201D in Chesterfield: 15 killed

Date & Time: Jul 30, 1949 at 1030 LT
Type of aircraft:
Operator:
Registration:
N19963
Flight Phase:
Survivors:
No
Schedule:
Boston – New York – Wilmington – Memphis
MSN:
2260
YOM:
1940
Flight number:
EA557
Crew on board:
3
Crew fatalities:
Pax on board:
12
Pax fatalities:
Other fatalities:
Total fatalities:
15
Captain / Total flying hours:
10013
Captain / Total hours on type:
5595.00
Copilot / Total flying hours:
1397
Aircraft flight hours:
37840
Circumstances:
The DC-3 was on a regularly scheduled flight en route from La Guardia Field, N Y., to Wilmington, Del., having originated at Boston, Mass., with Memphis, Tenn., as the destination. Takeoff from La Guardia was at 1000, with 12 revenue passengers and a fresh crew consisting of Captain L. R. Matthews, Pilot J. B. Simmons, and Flight Attendant Peter Gobleck. The aircraft was loaded within the prescribed limits for weight and location of center of gravity. The clearance was in accordance with Visual Flight Rules. The flight reported its position as over Freehold, N J., at 1017 and estimated arrival over Philadelphia, Pa., at 1037 and Wilmington, Del., at 1045. This was the last radio contact with the DC-3. The F-6-F-5 was en route from the Naval Air Station Anacostia, DC, to the Naval Air Station, Quonset Point R. I., on a training, or proficiency flight. Takeoff from Anacostia was at 0937 with the aircraft piloted by Lieutenant (j g) Robert V. Poe, USN. Clearance was in accordance with Visual Flight Rules, specifying a cruising speed of 160 knots (184 statute miles per hour) and an estimated time en route of two hours. There is no record of any position report or other radio contact from the F-6-F-5 after it was cleared for takeoff by the Anacostia tower. Weather conditions existing over the route of both aircraft were good. The visibility was 10 miles and there were scattered clouds at 12,000 feet. At about 1030 the F-6-F-5 was observed to perform acrobatics and to "buzz" a small civil aircraft in the neighborhood of Chesterfield, N. J. These maneuvers terminated in collision between the F-6-F-5 and the DC-3. Upon collision the fighter plane lost its left wing and the DC-3 lost the outer portion of its left wing. Both aircraft then fell in erratic paths, losing various parts while falling. The DC-3 burned when it struck the ground. The fighter's pilot was either seriously injured or killed at the time of the collision and was thrown clear of the aircraft during the descent. There was no indication that he attempted to use his parachute. The fighter did not burn on impact. All 16 occupants in both aircraft were killed.
Probable cause:
The Board determines that the probable cause of this accident was the reckless conduct of the Navy pilot in performing acrobatic maneuvers on a Civil Airway and his failure to notice the presence of an air carrier aircraft with which he collided.
The following findings were noted:
- The Navy pilot was performing acrobatics on the airway immediately prior to and at the time of collision,
- Neither aircraft was seen by the crew of the other in time to avoid collision.
Final Report:

Crash of a Douglas DC-6 in Mount Carmel: 43 killed

Date & Time: Jun 17, 1948 at 1241 LT
Type of aircraft:
Operator:
Registration:
NC37506
Flight Phase:
Survivors:
No
Schedule:
San Diego – Los Angeles – Chicago – New York
MSN:
42871
YOM:
1947
Flight number:
UA624
Crew on board:
4
Crew fatalities:
Pax on board:
39
Pax fatalities:
Other fatalities:
Total fatalities:
43
Captain / Total flying hours:
7310
Captain / Total hours on type:
30.00
Copilot / Total flying hours:
3289
Copilot / Total hours on type:
129
Aircraft flight hours:
1245
Circumstances:
The airplane arrived in Chicago at 0952LT, en route from Los Angeles to New York City. At Chicago, the airplane was given a routine station inspection, serviced, loaded, and the flight departed for New York with a new crew at 1044. Aboard were 39 passengers, a crew of four, 2,568 pounds of cargo and 1,800 gallons of fuel, all properly loaded. The resulting total airplane weight was within the certificated gross weight. The airplane climbed en route to its planned altitude of 17,000 feet, proceeding on course, and at 1155 the captain reported to the company radio at LaGuardia Field, that the airplane was mechanically "okay” for a return trip. A routine report was made over Phillipsburg, PA, approximately 500 miles east of Chicago, at 1223, and at 1227 the crew made a routine acknowledgment of a clearance to descend en route to an altitude between 13,000 and 11,000 feet. Four minutes later, at 1231, the company radio operator at LaGuardia Field heard a voice which did not identify itself calling loudly and urgently. Another United crew in a DC-3, flying over the same route behind Flight 624 and at a different altitude, heard what they termed “screaming voices” calling "New York." Then, after an unintelligible transmission, “This is an emergency descent." Inasmuch as all other air carrier flights in the vicinity at this time were accounted for, this transmission undoubtedly emanated from Flight 624. The airplane was first observed by ground witnesses 31 miles northwest of the scene of the accident flying a southeasterly heading toward Shamokin, PA. The airplane flew over the Sunbury Airport, at approximately 4,000 feet above the ground on a southeasterly heading. Immediately north of Shamokin the airplane, then only 500 to 1,000 feet above the ground, described a shallow left turn. The course was toward constantly rising terrain, the hills around Sunbury being 900 feet in elevation and the hills around Shamokin being approximately 1,600 feet in elevation. Five miles east or beyond Shamokin the airplane, flying only 200 feet above the ground, entered a right climbing turn. As it passed to the north of Mount Carmel, the climbing turning attitude increased sharply. The airplane then struck a hillside at an elevation of 1,649 feet. The aircraft disintegrated on impact and all 43 occupants were killed.
Probable cause:
The Board determines that the probable cause of this accident was the incapacitation of the crew by a concentration of CO2 gas in the cockpit.
The following factors were considered as contributing:
- A fire warning caused the crew to discharge at least one bank of the CO2 fire extinguisher bottles in the forward cargo pit (the forward underfloor baggage compartment),
- Six 15-pound CO2 bottles and six discharge valves were found in the wreckage, however, both the bottles and the valves (which had become separated from their respective bottles upon impact) were so damaged that no conclusions could be drawn as to how many of such bottles had been discharged prior to impact,
- At the time of impact, the emergency cabin pressure relief valves were closed, and the control mechanism for such valves was in the closed position,
- Except for the apparent failure of the fire detection instrument referred to in finding No. 5, supra, the investigation revealed no mechanical failure of the aircraft or fire in flight,
- The emergency procedure for the operation of the DC-6 fire extinguisher system was established after flight tests were conducted in a descent configuration of 300 miles per hour, with landing gear and flaps up, no flight tests were conducted prior to the accident in a descent configuration of 160 miles per hour with gear and flaps down, which configuration was also approved for DC-6 operations,
- At the time of impact the landing gear was in the “up" position, thus indicating that the aircraft had descended in the configuration of 300 miles per hour. The extensive breakage of the aircraft precluded any positive determination as to the position of the flaps,
- After the release of CO2 gas hazardous concentrations of the gas entered into the cockpit,
- Due to the physiological and toxic effects of high concentrations of CO2 gas in the cockpit, which would probably not have occurred had the cabin pressure relief valves been open, the members of the flight crew of the aircraft were rendered physically and mentally incapable of performing their duties.
The following comment was added to the conclusion:
A fire in flight permits little opportunity for the exercise of detached and thoughtful consideration of emergency procedure. Immediate action is required if a fire is to be controlled. Too little consideration has been given to the psychological and physical limitations of crew members in time of stress and danger as related to the complexity of emergency fire procedure. It is not safe to assume that the pilot and co-pilot, under emergency pressure, will always adhere rigidly to the sequence of steps outlined in the CAA Approved Airplane Operating Manual. The possibility of human error under great mental stress is well documented in air transport experience and the design of aircraft controls, especially those of an emergency character, should take into consideration the natural limitations of human nature. These limitations argue against involved procedures applicable in emergencies. In harmony with this objective, the Douglas Aircraft Company has designed and is testing a modified fire extinguishing system which will permit all necessary steps to be executed by the movement of one control. An additional vent is also being designed to reduce CO2 concentration in the cockpit. Seven days after the Mt Carmel accident, the Director of Aviation Safety of the CAA directed telegrams to all CAA regional administrators calling attention to his telegram of June 10, 1948, referred to above, and advising that further investigation had disclosed the existence of the CO2 concentration condition found in Constellation aircraft by the Chillicothe tests in other makes of aircraft. The telegram concluded "Hence, flight crews of all aircraft should be advised to wear oxygen masks and utilize emergency cockpit smoke clearance procedures when carbon dioxide is released into any fuselage compartment from other than portable extinguishers.” All scheduled U S air carriers operating DC-6s have equipped the airplanes with demand type full face oxygen masks for the use of the crew.
Final Report: