code

NY

Crash of a Beechcraft B60 Duke in Farmingdale

Date & Time: Nov 5, 2022 at 1349 LT
Type of aircraft:
Operator:
Registration:
N51AL
Flight Type:
Survivors:
Yes
Schedule:
Burlington – Farmingdale
MSN:
P-247
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
While descending to Farmingdale-Republic Airport, following a flight from Burlington, the twin engine airplane crashed in the Beth Moses Cemetery located two km east of the airport. Both occupants escaped with minor injuries and the aircraft was damaged beyond repair.

Crash of a Cessna 421B Golden Eagle II in Old Bethpage

Date & Time: Jan 10, 2021 at 1302 LT
Registration:
N421DP
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Farmingdale – Bridgeport
MSN:
421B-0353
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1893
Captain / Total hours on type:
12.00
Aircraft flight hours:
5331
Circumstances:
The pilot reported that, during the initial climbout, about 1,000 ft above ground level, one of the engines stopped producing power. He confirmed that all engine controls were full forward and the main fuel tanks were selected. Immediately thereafter, the remaining engine began to surge, then stopped producing power. He established best glide speed and looked for an area to perform a forced landing. The airplane crashed into a solid waste disposal facility, about 2.3 nautical miles northwest of the departure airport. First responders arrived immediately after the accident and found only a trace amount of fuel within the confines of the accident site or in the fuel tanks. The only postaccident fire was centered on a small, localized area near the right engine turbocharger. Both main fuel tanks were empty, and the auxiliary bladder tanks were ruptured by impact forces. Examination of both engines revealed no evidence of a pre accident malfunction or anomaly. A surveillance video showed no evidence of smoke or mist training the airplane seconds prior to impact. The pilot reported that he departed the airport with 112 gallons of fuel on board. The pilot did not provide evidence of the latest refueling when requested by investigators. The available evidence is consistent with a total loss of engine power to both engines due to fuel exhaustion.
Probable cause:
The pilot’s inadequate preflight fuel planning, which resulted in a total loss of engine power due to fuel exhaustion and a forced landing.
Final Report:

Crash of a Hawker 800XP in Farmingdale

Date & Time: Dec 20, 2020 at 2035 LT
Type of aircraft:
Operator:
Registration:
N412JA
Flight Type:
Survivors:
Yes
Schedule:
Miami - Farmingdale
MSN:
258516
YOM:
2001
Flight number:
TFF941
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4188
Captain / Total hours on type:
2060.00
Copilot / Total flying hours:
10000
Copilot / Total hours on type:
4100
Aircraft flight hours:
12731
Circumstances:
The flight crew were conducting an instrument landing system (ILS) approach in night instrument meteorological conditions when they were advised by the tower controller that the weather had deteriorated below minimums. The captain was the pilot monitoring, and the first officer was the pilot flying during the approach. Since the airplane was inside the final approach fix and stabilized, both pilots agreed to continue with the approach. Both pilots stated that they had visual contact with the runway approach lighting system at the 200 ft above ground level (agl) decision altitude, and they decided to continue the approach. The first officer said he then returned to flying the airplane via instruments. As the first officer continued the approach, the captain told him the airplane was drifting right of the runway centerline. The first officer said that he looked outside, saw that the weather had deteriorated, and was no longer comfortable with the approach. The first officer said he pressed the takeoff and go-around switch, while at the same time, the captain called for a go-around. The captain said that he called for the go-around because the airplane was not aligned with the runway. Although both pilots stated that the go-around was initiated when the airplane was about 50 to 100 ft agl, the cockpit voice recorder (CVR) recording revealed that the first officer flew an autopilot-coupled approach to 50 ft agl (per the approach procedure, a coupled approach was not authorized below 240 ft agl). As the airplane descended from 30 to 20 ft agl, the captain told the first officer three times to “flare” then informed him that the airplane was drifting to right and he needed to make a left correction to get realigned with the runway centerline. Three seconds passed before the first officer reacted by trying to initiate transfer control of the airplane to the captain. The captain did not take control of the airplane and called for a go-around. The first officer then added full power and called for the flaps to be retracted to 15º; however, the airplane impacted the ground about 5 seconds later, resulting in substantial damage to the fuselage. Data downloaded from both engines’ digital electronic engine control units revealed no anomalies. No mechanical issues with the airplane or engines were reported by either crew member or the operator. The sequence of events identified in the CVR recording revealed that the approach most likely became unstabilized after the autopilot was disconnected and when the first officer lost visual contact with the runway environment. The captain, who had the runway in sight, delayed calling for a go-around after the approach became unstabilized, and the airplane was too low to recover.
Probable cause:
The flight crew’s delayed decision to initiate a go-around after the approach had become unstabilized, which resulted in a hard landing.
Final Report:

Crash of a Socata TBM-850 in Corfu: 2 killed

Date & Time: Oct 2, 2020 at 1144 LT
Type of aircraft:
Operator:
Registration:
N965DM
Flight Type:
Survivors:
No
Schedule:
Manchester - Buffalo
MSN:
527
YOM:
2009
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
960
Captain / Total hours on type:
239.00
Aircraft flight hours:
1181
Circumstances:
The airplane was in cruise flight at FL280 when the instrument-rated pilot failed to contact air traffic control (ATC) following a frequency change assignment. After about 25 minutes, and when 30 miles east of the destination airport, the pilot contacted ATC on a frequency other than the one that was assigned. He requested the instrument landing system (ILS) approach at his intended destination, and the controller instructed the pilot to descend to 8,000 ft and to expect vectors for the ILS approach at the destination airport. The controller asked the pilot if everything was “okay,” to which the pilot replied, “yes sir, everything is fine.” The controller then observed the airplane initiate a descent. About 2 minutes later, the controller asked the pilot where he was headed, and the pilot provided a garbled response. The controller instructed the pilot to stop his descent at 10,000 ft, followed by an instruction to stop the descent at any altitude. The pilot did not respond, and additional attempts to contact the pilot were unsuccessful. The airplane impacted terrain in a heavily wooded area 17 miles from the destination airport. Rhe aircraft disintegrated on impact and both occupants were fatally injured.
Probable cause:
The pilot’s failure to maintain control of the airplane for undetermined reasons during the descent to the destination airport.
Final Report:

Crash of a Cessna T303 Crusader in Lagrangeville: 2 killed

Date & Time: Aug 17, 2019 at 1613 LT
Type of aircraft:
Registration:
N303TL
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Sky Acres - Farmingdale
MSN:
303-00286
YOM:
1984
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1586
Captain / Total hours on type:
358.00
Aircraft flight hours:
2932
Circumstances:
After flying one flight leg earlier in the day, the pilot flew to an intermediate stop on the way to his home base to purchase fuel. A surveillance video recording from the fueling airport showed the airplane land and taxi to the self-serve fuel pump where the engines were shut down for about 10 minutes while the airplane was fueled. The pilot then had difficulty starting both engines over several minutes. After the engines were running, the airplane taxied to the runway and did not appear to stop for an engine run-up. The pilot performed a rolling takeoff, and the airplane lifted off after a roll of about 2,100 ft, slightly more than half the available runway length. A passenger reported that after liftoff, at an altitude of about 50 to 100 ft above ground level (agl), both engines lost partial power and began “stuttering,” which continued for the remainder of the flight. He further reported that the engines did not stop, but they were “not producing full RPM.” The airplane drifted left of centerline, which a witness described as a left yawing motion. The pilot corrected the drift and flew the runway heading over the grass on the left side of the runway; however, the airplane would not climb. After crossing the end of the runway, the pilot pitched the airplane up to avoid obstacles. Automatic dependent surveillance-broadcast data indicated that the airplane climbed from about 20 to 120 ft agl in a gradual left turn. During this time the groundspeed decreased from about 80 knots to about 69 knots. The altitude then decreased to about 50 ft agl, the groundspeed decreased to about 66 knots, and the left turn decreased in radius until the recorded data ended about 100 ft west of the accident site. The airplane descended and
impacted a house. Witness descriptions of the airplane yawing to the left while over the runway and again during its final left turn suggest that the loss of engine power may not have been symmetric (that is, one engine may have suffered more of a loss than the other).
Probable cause:
A partial loss of engine power in both engines during initial climb for reasons that could not be determined based on the available information.
Final Report:

Crash of a Piper PA-46-310P Malibu in Poughkeepsie

Date & Time: Jul 19, 2019 at 1440 LT
Operator:
Registration:
N811SK
Flight Type:
Survivors:
Yes
Schedule:
Akron – Pawtucket
MSN:
46-8508046
YOM:
1985
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1300
Captain / Total hours on type:
300.00
Aircraft flight hours:
2641
Circumstances:
The pilot was in cruise flight at an altitude of 19,000 feet mean sea level (msl) for about 1 hour and 10 minutes on an easterly heading when he requested a diversion from his filed destination to an airport along his route of flight to utilize a restroom. Two miles west of his amended destination at 12,000 ft msl, the pilot advised the controller that he had a “fuel emergency light" and wanted to expedite the approach. The controller acknowledged the low fuel warning and cleared the airplane to descend from its assigned altitude. Instead of conducting the descent over the airport, the airplane continued its easterly heading past the airport for nearly 8 miles before reversing course. After reversing course, instead of assuming a direct heading back to the airport, the pilot assumed a parallel reciprocal track and didn’t turn for the airport until the airplane intercepted the extended centerline of the landing runway. The pilot informed the controller that he was unable to make it to the airport and performed a forced landing less than 1 mile from the landing runway. Both fuel tanks were breached during the accident sequence, and detailed postaccident inspections of the airplane’s fuel system revealed no leaks in either the supply or return sides of the system. A computer tomography scan and flow-testing of the engine-driven fuel pump revealed no leaks or evidence of fuel leakage. The engine ran successfully in a test cell. Data recovered from an engine and fuel monitoring system revealed that, during the two flights before the accident flight, the reduction in fuel quantity was consistent with the fuel consumption rates depicted at the respective power settings (climb, cruise, etc). During the accident flight, the reduction in fuel quantity was consistent with the indicated fuel flow throughout the climb; however, the fuel quantity continued to reduce at a rate consistent with a climb power setting even after engine power was reduced, and the fuel flow indicated a rate consistent with a cruise engine power setting. The data also showed that the indicated fuel quantity in the left and right tanks reached 0 gallons within about 10 minutes of each other, and shortly before the accident. Given this information, it is likely that the engine lost power due to an exhaustion of the available fuel supply; however, based on available data and findings of the fuel system and component examinations, the disparate rates of indicated fuel flow and fuel quantity reduction could not be explained.
Probable cause:
A total loss of engine power due to fuel exhaustion as the result of a higher-than-expected fuel quantity reduction. Contributing was the pilot’s continued flight away from his selected precautionary landing site after identification of a fuel emergency, which resulted in inadequate altitude and glide distance available to complete a successful forced landing.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain off Amagansett: 4 killed

Date & Time: Jun 2, 2018 at 1433 LT
Registration:
N41173
Flight Type:
Survivors:
No
Schedule:
Newport – East Hampton
MSN:
31-8452017
YOM:
1984
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
3000
Aircraft flight hours:
5776
Circumstances:
The commercial pilot of the multiengine airplane was the first of a flight of two airplanes to depart on the cross-country flight, most of which was over the Atlantic Ocean. The pilot of the second airplane stated that he and the accident pilot reviewed the weather for the route and the destination before departing; however, there was no record of the accident pilot receiving an official weather briefing and the information the pilots accessed before the flight could not be determined. The second pilot departed and contacted air traffic control, which advised him of thunderstorms near the destination; he subsequently altered his route of flight and landed uneventfully at the destination. The second pilot stated that he did not hear the accident pilot on the en route air traffic control frequency. Two inflight weather advisories were issued for the route and the area of the destination about 42 and 15 minutes before the accident flight departed, respectively, and warned of heavy to extreme precipitation associated with thunderstorms. It could not be determined whether the accident pilot received these advisories. Review of air traffic control communications and radar data revealed that, about 5 miles from the destination airport, the pilot of the accident airplane reported to the tower controller that he was flying at 700 ft and "coming in below" the thunderstorm. There were no further communications from the pilot. The airplane's last radar target indicated 532 ft about 2 miles south of the shoreline. The airplane was found in about 50 ft of water and was fragmented in several pieces. Postaccident examination revealed no preimpact anomalies with the airplane or engines that would have precluded normal operation. A local resident about 1/2 mile from the accident site took several photos of the approaching thunderstorm, which documented a shelf cloud and cumulus mammatus clouds along the leading edge of the storm, indicative of potential severe turbulence. Review of weather imagery and the airplane's flight path showed that the airplane entered the leading edge of "extreme" intensity echoes with tops near 48,000 ft. Imagery also depicted heavy to extreme intensity radar echoes over the accident site extending to the destination airport. It is likely that the pilot encountered gusting winds, turbulence, restricted visibility in heavy rain, and low cloud ceilings in the vicinity of the accident site and experienced an in-flight loss of control at low altitude. Such conditions are conducive to the development of spatial disorientation; however, the reason for the pilot's loss of control could not be determined based on the available information.
Probable cause:
The pilot's decision to fly under a thunderstorm and a subsequent encounter with turbulence and restricted visibility in heavy rain, which resulted in a loss of control.
Final Report:

Crash of a Piper PA-31-310 Navajo C near Colton: 1 killed

Date & Time: May 3, 2017 at 2030 LT
Type of aircraft:
Operator:
Registration:
C-GQAM
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Quebec - Montreal
MSN:
31-7912093
YOM:
1979
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
5250
Captain / Total hours on type:
1187.00
Circumstances:
The commercial pilot departed on a planned 1-hour cargo cross-country flight in the autopilot-equipped airplane. About 3 minutes after departure, the controller instructed the pilot to fly direct to the destination airport at 2,000 ft mean sea level (msl). The pilot acknowledged the clearance, and there were no further radio transmissions from the airplane. The airplane continued flying past the destination airport in straight-and-level flight at 2,100 ft msl, consistent with the airplane operating under autopilot control, until it was about 100 miles beyond the destination airport. A witness near the accident site watched the airplane fly over at a low altitude, heard three "pops" come from the airplane, and then saw it bank to the left and begin to descend. The airplane continued in the descending left turn until he lost sight of it as it dropped below the horizon. The airplane impacted trees in about a 45° left bank and a level pitch attitude and came to rest in a heavily wooded area. The airplane sustained extensive thermal damage from a postcrash fire; however, examination of the remaining portions of the airframe, flight controls, engines, and engine accessories revealed no evidence of preimpact failure or malfunction. The fuel selector valves were found on the outboard tanks, which was in accordance with the normal cruise procedures in the pilot's operating handbook. Calculations based on the airplane's flight records and the fuel consumption information in the engine manual indicated that, at departure, the outboard tanks of the airplane contained sufficient fuel for about 1 hour 10 minutes of flight. The airplane had been flying for about 1 hour 15 minutes when the accident occurred. Therefore, it is likely that the fuel in the outboard tanks was exhausted; without pilot action to switch fuel tanks, the engines lost power as a result of fuel starvation, and the airplane descended and impacted trees and terrain. The overflight of the intended destination and the subsequent loss of engine power due to fuel starvation are indicative of pilot incapacitation. The pilot's autopsy identified no significant natural disease:however, the examination was limited by the severity of damage to the body. Further, there are a number of conditions, including cardiac arrhythmias, seizures, or other causes of loss of consciousness, that could incapacitate a pilot and leave no evidence at autopsy. The pilot's toxicology results indicated that the pilot had used marijuana/tetrahydrocannabinol (THC) at some point before the accident. THC can impair judgment, but it does not cause incapacitation; therefore, the circumstances of this accident are not consistent with impairment from THC, and, the pilot's THC use likely did not contribute to this accident. The reason for the pilot's incapacitation could not be determined.
Probable cause:
The pilot's incapacitation for unknown reasons, which resulted in an overflight of his destination, a subsequent loss of engine power due to fuel starvation, and collision with terrain.
Final Report:

Crash of a Swearingen SA226T Merlin IIIB in Farmingdale

Date & Time: Jun 20, 2016 at 1758 LT
Operator:
Registration:
N127WD
Flight Type:
Survivors:
Yes
Schedule:
White Plains - Farmingdale
MSN:
T-297
YOM:
1978
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11450
Captain / Total hours on type:
410.00
Copilot / Total flying hours:
1300
Copilot / Total hours on type:
5
Aircraft flight hours:
4500
Circumstances:
According to the pilot in command (PIC), he was conducting an instructional flight for his "new SIC (second in command)," who was seated in the left seat. He reported that they had flown two previous legs in the retractable landing gear-equipped airplane. He recalled that, during the approach, they discussed the events of their previous flights and had complied with the airport control tower's request to "keep our speed up." During the approach, he called for full flaps and retarded the throttle to flight idle. The PIC asserted that there was no indication that the landing gear was not extended because he did not hear a landing gear warning horn; however, he was wearing a noise-cancelling headset. He added that the landing gear position lights were not visible because the SIC's knee obstructed his view of the lights. He recalled that, following the flare, he heard the propellers hit the runway and that he made the decision not to go around because of unknown damage sustained to the propellers. The airplane touched down and slid to a stop on the runway. The airplane sustained substantial damage to the fuselage bulkheads, longerons, and stringers. The SIC reported that the flight was a training flight in visual flight rules conditions. He noted that the airspace was busy and that, during the approach, he applied full flaps, but they failed to extend the landing gear. He added that he did not hear the landing gear warning horn; however, he was wearing a noise-cancelling headset. The Federal Aviation Administration Aviation Safety Inspector that examined the wreckage reported that, during recovery, the pilot extended the nose landing gear via the normal extension process. However, due to significant damage to the main landing gear (MLG) doors, the MLG was unable to be extended hydraulically or manually. He added that an operational check of the landing gear warning horn was not accomplished because the wreckage was unsafe to enter after it was removed from the runway. The landing gear warning horn was presented by an aural tone in the cockpit and was not configured to be heard through the pilots' noise-cancelling headsets. When asked, the PIC and the SIC both stated that they could not remember who read the airplane flight manual Before Landing checklist.
Probable cause:
The pilot-in-command's failure to extend the landing gear before landing and his failure to use the Before Landing checklist. Contributing to the accident was the pilots' failure to maintain a sterile cockpit during landing.
Final Report:

Crash of a Piper PA-46-500TP Malibu Meridian in Saranac Lake: 4 killed

Date & Time: Aug 7, 2015 at 1750 LT
Operator:
Registration:
N819TB
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Saranac Lake – Rochester
MSN:
46-97117
YOM:
2001
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
4620
Captain / Total hours on type:
230.00
Circumstances:
The private pilot, who was experienced flying the accident airplane, was conducting a personal flight with three passengers on board the single-engine turboprop airplane. Earlier that day, the pilot flew uneventfully from his home airport to an airport about 1 hour away. During takeoff for the return flight, the airplane impacted wooded terrain about 0.5 mile northwest of the departure end of the runway. There were no witnesses to the accident, but the pilot's radio communications with flight service and on the common traffic advisory frequency were routine, and no distress calls were received. A postcrash fire consumed a majority of the wreckage, but no preimpact mechanical malfunctions were observed in the remaining wreckage. Examination of the propeller revealed that the propeller reversing lever guide pin had been installed backward. Without the guide pin installed correctly, the reversing lever and carbon block could dislodge from the beta ring and result in the propeller blades traveling to an uncommanded feathered position. However, examination of the propeller components indicated that the carbon block was in place and that the propeller was in the normal operating range at the time of impact. Additionally, the airplane had been operated for about 9 months and 100 flight hours since the most recent annual inspection had been completed, which was the last time the propeller was removed from and reinstalled on the engine. Therefore, the improper installation of the propeller reversing lever guide pin likely did not cause the accident. Review of the pilot's autopsy report revealed that he had severe coronary artery disease with 70 to 80 percent stenosis of the right coronary artery, 80 percent stenosis of the left anterior descending artery, and mitral annular calcification. The severe coronary artery disease combined with the mitral annular calcification placed the pilot at high risk for an acute cardiac event such as angina, a heart attack, or an arrhythmia. Such an event would have caused sudden symptoms such as chest pain, shortness of breath, palpitations, or fainting/loss of consciousness and would not have left any specific evidence to be found during the autopsy. It is likely that the pilot was acutely impaired or incapacitated at the time of the accident due to an acute cardiac event, which resulted in his loss of airplane control.
Probable cause:
The pilot's loss of airplane control during takeoff, which resulted from his impairment or incapacitation due to an acute cardiac event.
Final Report: