Crash of a Piper PA-61P Aerostar (Ted Smith 601P) in Philadelphia

Date & Time: Jan 16, 2012 at 1242 LT
Operator:
Registration:
N700PS
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Philadelphia – Meridian
MSN:
61-0427-157
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
6200
Aircraft flight hours:
2857
Circumstances:
On the day of the accident, a mechanic taxied the airplane onto the runway and performed a full power check of both engines, exercised both propellers, and checked each magneto drop with no discrepancies reported. Following the engine run, the mechanic taxied the airplane to the fuel ramp where the fuselage fuel tank was filled; after fueling, the fuselage tank had 41.5 gallons of usable fuel. The mechanic then taxied the airplane to the ramp where the engines were secured and the fuel selector switches were placed to the off position. The mechanic reported that, at that time, the left fuel tank had 4 to 5 gallons of fuel, while the right fuel tank had about 2 to 3 gallons of fuel; the unusable fuel amount for each wing tank is 3 gallons. The pilot taxied the airplane to the approach end of runway 18 and was heard to apply takeoff power. A pilot-rated witness noted that, at the point of rotation, the airplane pitched up fairly quickly to about 20 degrees and rolled left to about 10 to 15 degrees of bank. The airplane continued rolling left to an inverted position and impacted the ground in a 40 degree nose-low attitude. A postcrash fire consumed most of the cockpit, cabin, both wings, and aft fuselage, including the vertical stabilizer, rudder, and fuselage fuel tank. Postaccident inspection of the flight controls, which were extensively damaged by impact and fire, revealed no evidence of preimpact failure or malfunction. Although the flap actuators were noted to be asymmetrically extended and no witness marks were noted to confirm the flap position, a restrictor is located at each cylinder’s downline port by design to prevent a rapid asymmetric condition. Therefore, it is likely that the flap actuators changed positions following impact and loss of hydraulic system pressure and did not contribute to the left roll that preceded the accident. Examination of the engines and propellers revealed no evidence of preimpact failure or malfunction that would have precluded normal operation. Postaccident examination of the fuselage fuel sump revealed the left fuel selector was in the crossfeed position, while the right fuel selector was likely positioned to the on position. (The as-found positions of the fuel selector knobs were unreliable due to postaccident damage.) The starting engines checklist indicates that the pilot is to move both fuel selectors from the on position to the crossfeed position, and back to the on position while listening for valve actuation/movement. The before takeoff checklist indicates that the pilot is to verify that the selectors are in the on position. Although the left engine servo fuel injector did not meet flow tests during the postaccident investigation, this was attributed to postaccident heat damage. Calculations to determine engine rpm based on ground scars revealed that the left engine was operating just above idle, and the right engine was operating about 1,315 rpm, which is consistent with a left engine loss of power and the pilot reducing power on the right engine during the in-flight loss of control. Examination of both propellers determined that neither was feathered at impact. Although the as-found position of the left fuel selector knob could be considered unreliable because of impact damage during the accident sequence, given that right wing fuel tank had no usable fuel, it is unlikely that the experienced pilot would have moved the left fuel selector to the crossfeed position in response to the engine power loss. It is more likely that the pilot failed to return the left fuel selector to the on position during the starting engines checklist and also failed to verify its position during the before takeoff checklist; thus, the left engine was being fed only from the right fuel tank, which had very little fuel. There was likely enough fuel in the right tank and lines for the pilot to taxi and takeoff before the left engine failed, causing the airplane to turn to the left, from which the pilot did not recover.
Probable cause:
The pilot’s failure to maintain directional control during takeoff following loss of power to the left engine due to fuel starvation. Contributing to the loss of control was the pilot’s failure to feather the left propeller following the loss of left engine power.
Final Report:

Crash of a Beechcraft 65 Queen Air in Meridian

Date & Time: Jul 17, 1991 at 1702 LT
Type of aircraft:
Registration:
N711SF
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Meridian – Tuscaloosa
MSN:
LC-139
YOM:
1962
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
943
Captain / Total hours on type:
34.00
Aircraft flight hours:
9200
Circumstances:
The pilot reported that shortly after takeoff the aircraft yawed to the right, left then right again. The passenger in the copilot seat stated the right engine rpm gauge indication needle was fluctuating. The pilot positioned the right engine mixture control to idle cutoff and the propeller control to feather. The propeller continued to windmill. Unable to maintain altitude, the pilot attempted to land on a highway but the aircraft collided with an unmarked power line, light pole, then the ground and was destroyed by a post crash fire. The right engine was recovered and due to impact damage, the propeller and fuel servo were replaced. The engine was placed on a test stand and was started and found to operate normally. The prop governor and damaged fuel servo were tested and found to operate normally. The damaged propeller was inspected and found to be free of preimpact failure or malfunction. No determination could be made as to the reason for the reported power fluctuation from the right engine. A witness stated gear retraction was delayed after takeoff.
Probable cause:
Loss of power from the right engine due to undetermined reasons. The failure of the propeller to feather was a factor in the accident.
Final Report:

Crash of a Grumman T-2C Buckeye in Meridian

Date & Time: Apr 13, 1989
Type of aircraft:
Operator:
Registration:
159724
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Meridian - Meridian
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
While completing a local training flight, the US Navy Buckeye collided with a second Buckeye registered 156694. Both aircraft crashed and were destroyed. While both pilots on board 156694 were killed, the crew on 159724 was able to eject in time.

Crash of a Grumman T-2C Buckeye in Meridian: 2 killed

Date & Time: Apr 13, 1989
Type of aircraft:
Operator:
Registration:
156694
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Meridian - Meridian
MSN:
326
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
While completing a local training flight, the US Navy Buckeye collided with a second Buckeye registered 159724. Both aircraft crashed and were destroyed. While both pilots on board 156694 were killed, the crew on 159724 was able to eject in time.

Crash of a Convair VT-29D off Newport News: 7 killed

Date & Time: Jan 9, 1975 at 1836 LT
Type of aircraft:
Operator:
Registration:
52-5826
Flight Type:
Survivors:
No
Schedule:
Meridian - Langley
MSN:
52-25
YOM:
1954
Flight number:
M32
Crew on board:
5
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
6840
Captain / Total hours on type:
1332.00
Aircraft flight hours:
14473
Circumstances:
While approaching Langley AFB by night on a flight from Meridian, Massachusetts, the airplane collided with a Cavalier Flyers Cessna 150 registered N50430 and carrying two people. Following the collision, both aircraft crashed into the James River, about four miles west of Newport News. Both aircraft were destroyed and all nine people were killed.
Probable cause:
The human limitation inherent in the see-and-avoid concept, which can be critical in a terminal area with a combination of controlled and uncontrolled traffic. A possible contributing factor was the reduced nighttime conspicuity of the Cessna against a background of city lights. The following findings were reported:
- No controlling agency,
- Not under radar contact,
- No traffic advisory issued,
- Continued versus uncontrolled traffic.
Final Report:

Crash of a Douglas DC-3-454 in Meridian

Date & Time: Nov 10, 1946 at 1717 LT
Type of aircraft:
Operator:
Registration:
NC20750
Survivors:
Yes
Schedule:
Fort Worth – Dallas – Shreveport – Monroe – Jackson – Meridian – Birmingham – Atlanta
MSN:
4993
YOM:
1942
Flight number:
DL010
Crew on board:
3
Crew fatalities:
Pax on board:
19
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3725
Captain / Total hours on type:
3100.00
Copilot / Total flying hours:
3207
Copilot / Total hours on type:
301
Aircraft flight hours:
8819
Circumstances:
The aircraft left Jackson at 1630LT bound for Meridian and the crew obtained the permission to continue at an altitude of 3,000 feet in IFR mode. The approach to Meridian was started in the following weather conditions: ceiling 800 feet, overcast, visibility 3 miles, thunder storm, light rain showers, surface wind northeast 10, thunder storms overhead moving east-northeast, frequent vivid lightning all quadrants. The aircraft was seen to make contact with the runway within the first 1,000 feet, however. it continued rolling down the entire length of the runway with little apparent deceleration. Its forward motion continued beyond the end of the runway and up the western slope of a ditch adjoining the highway adjacent to the airport. on striking this ditch, the aircraft left the ground and bounced over the highway, coming to rest with its nose extended partially over a railroad right-of-way. All 22 occupants escaped unhurt while the aircraft was damaged beyond repair.
Probable cause:
The Board determines that the probable cause of this accident was the poor judgement of the pilot in landing on a wet runway under conditions of varying winds without ascertaining visually the direction of the wind. A contributory factor was the error of the company radio communicator in transmitting the wind direction.
Final Report: