Crash of a Beechcraft 99A Airliner in Killeen

Date & Time: Jan 12, 1971 at 1820 LT
Type of aircraft:
Operator:
Registration:
N12RA
Survivors:
Yes
Schedule:
Dallas – Killeen
MSN:
U-131
YOM:
1969
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
13
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4200
Captain / Total hours on type:
1000.00
Circumstances:
On approach to Killeen Airport, the crew encountered marginale weather conditions with fog and ceiling. He was informed from ATC about a visibility below minima but the captain decided to continue the descent until the aircraft struck the ground short of runway and came to rest. The aircraft was damaged beyond repair and all 15 occupants were injured, nine of them seriously.
Probable cause:
Improper IFR operation on part of crew. The following factors were reported:
- Low ceiling and fog,
- The pilot knew that weather was below VOR minimums from ATC and another pilot who had to divert to alternate airport.
Final Report:

Crash of a Rockwell Aero Commander 560E in Dallas: 7 killed

Date & Time: Sep 27, 1967 at 1536 LT
Operator:
Registration:
N3831C
Survivors:
No
Site:
MSN:
560-747
YOM:
1959
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
13247
Captain / Total hours on type:
2010.00
Circumstances:
While on approach to Dallas-Love Field Airport, the left wing broke away and control was lost. The airplane entered a dive and crashed on the elementary school of Bradfield. All seven occupants on board the airplane were killed while no one on the ground was injured. The school was partially destroyed as well as several vehicles. The airplane was operated on behalf of LTV Electrosystems (Ling-Temco-Vought).
Probable cause:
Uncontrolled descent following the structural failure of the left wing due to fatigue fracture. Two overlapping rivet holes found in aft leg of the spar cap.
Final Report:

Crash of a Beechcraft D18S in Dallas: 3 killed

Date & Time: Feb 10, 1967 at 1607 LT
Type of aircraft:
Operator:
Registration:
N7388
Flight Phase:
Flight Type:
Survivors:
No
MSN:
A-268
YOM:
1946
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
13000
Captain / Total hours on type:
6000.00
Circumstances:
Shortly after takeoff from Dallas-Love Field Airport, while climbing, the pilot lost control of the airplane that stalled and crashed in flames in an open field. The aircraft was destroyed and all three occupants were killed.
Probable cause:
Failure an separation in flight of a propeller blade during initial climb due to fatigue fracture. It was determined that the right engine Hartzell propeller blade separated at shank radius. Crankshaft counterweight liners excessively worn.
Final Report:

Crash of a Douglas C-47A-90-DL in Dallas: 3 killed

Date & Time: Apr 18, 1962 at 1625 LT
Operator:
Registration:
N3588
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Dallas - Dallas
MSN:
20178
YOM:
1944
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Aircraft flight hours:
11996
Circumstances:
Following a major overhaul on engine, a test flight was schedule out from Dallas-Love Field Airport. Two mechanics and the maintenance manager took off at 1625 and while climbing to a height of 300 feet, the aircraft stalled and crashed near the runway end. The aircraft was destroyed and all three occupants were killed.
Probable cause:
It was determined that the maintenance manager was piloting at the time of the accident and he was not raited and hold a private license only. Also, both mechanics were not qualified on type. The aircraft stalled because the climb speed was insufficient.
The following factors were considered as contributing:
- The pilot in command exercised poor judgment,
- Inadequate supervision of flight crew,
- Pilot lack of proficiency and qualification on type,
- The 'pilot' superior approved the flight.

Crash of a Curtiss C-46F-1-CU Commando in Dallas

Date & Time: Jul 19, 1953
Type of aircraft:
Operator:
Registration:
N1697M
Flight Type:
Survivors:
Yes
Schedule:
Miami – Dallas
MSN:
22573
YOM:
1945
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On final approach to Love Field, the aircraft was too low and hit a embankment short of runway threshold. The aircraft crash landed and lost its right wing before coming to rest upside down. Both pilots were injured and the aircraft was written off.

Crash of a Douglas DC-6 in Dallas: 28 killed

Date & Time: Nov 29, 1949 at 0549 LT
Type of aircraft:
Operator:
Registration:
N90728
Survivors:
Yes
Schedule:
New York – Washington DC – Dallas – Mexico City
MSN:
42895
YOM:
1947
Flight number:
AA157
Crew on board:
5
Crew fatalities:
Pax on board:
41
Pax fatalities:
Other fatalities:
Total fatalities:
28
Aircraft flight hours:
5260
Circumstances:
Flight 157 originated at LaGuardia Field, New York, for Mexico City, Mexico, with stops scheduled at Washington, D C., and Dallas, Tex. Departure from LaGuardia was at 2147, November 28 Between LaGuardia and Washington the flight was reported to be uneventful with all of the aircraft's components functioning normally. At Washington, a flight plan was filed with, and approved by, Airway Route Traffic Control It specified Instrument Flight Rules to Dallas, with Wichita Falls, Tex, as the alternate, a cruising altitude of 18,000 feet, and a flight time of 5 hours and 4 minutes The gross height of the aircraft at takeoff was 82,298 pounds, which was 3,577 pounds less than the maximum allowable gross weight of 85,875 pounds, and the disposable load was distributed so that the center of gravity was within prescribed limits. At 0206 the flight requested and received permission to change its flight plan to Visual Flight Rules A posit-,on report was made over Nashville at 16,000 feet at 0254 and a descent was started to 6,000 feet When approaching Nashville, 1 No 1 engine had started backfiring at intervals of about 20 seconds Various corrective measures, including the application of alcohol and carburetor heat, and the richening of fuel mixture, were applied but were not successful and the backfiring continued. The captain and the flight engineer discussed the malfunctioning following which No 1 engine was feathered at a point about 25 miles southwest of Nashville at approximately 0300, however, the feathering was not reported to the company until 0429, where the flight was in the vicinity of Altheimer, Ark, a routine position reporting point about 125 miles beyond Memphis At that time, the crew advised a change of aircraft on arrival at Dallas. When 15 miles northeast of Dallas, at 0536, the flight was given permission to enter the traffic pattern at Love Field, Dallas, with a right-hand turn and instructed to land on Runway 36 The altimeter setting of 29 83 inches and the weather, which included unlimited ceiling, a visibility of 15 miles and a north-northeast wind of 5 mph, were given the flight The captain and the flight engineer conferred regarding returning No 1 engine to service and decided against doing so. The crew then went through the pre-landing cheek The landing lights were turned or and the Plans were lowered to the 20 degree position. The flight turned -flight to final approach when approximately over the Range Station which is 2 2 miles south of the approach end of Runway 36 At this time its altitude was estimated to be 1200 feet AFL 2 by the captain and 800 feet AFL by the first officer At a distance of about 1 1/2 miles from the approach end of the runway, the landing gear was extended. Shortly thereafter the flaps were extended fully, the turn to final placed be aircraft to the left of the runway Accordingly an "S" turn was made to correct the misalignment During this "S" turn the aircraft skidded to Its left, the air speed dropped abruptly and the aircraft settled rapidly. At this point the captain increased power to engines Nos. 2, 3 and 4 in an attempt to maintain control. Control tower operators watching the approach estimated that the aircraft cleared by 75 to 100 feet obstruction lights mounted on 30-foot poles on a power line located 800 feet south of the approach end of the runway. The aircraft continued in a generally northwest direction, across the airport on a heading about 40 degrees to the left of Runway 36, in a tail low attitude. Its air speed continued to fall, its attitude became increasingly nose-high. and a stall developed just prior to striking a hangar and other buildings on the northwest side of the airport. Both pilots and 26 passengers were killed.
Probable cause:
It was determined that the accident was caused by a faulty execution of an engine-out approach on part of the crew.
The following findings were noted:
- The captain failed to align the aircraft with the runway centerline after the final turn,
- After realizing the misalignment, the captain attempted to correct it with a risky "S"-turn at low altitude. There is little room for error if a problem arises during this maneuver because as the angle of the bank increases, so does the probability of stalling the airplane,
- The crew made no attempt to balance the airplane’s fuel load after the No. 1 engine failed. The DC-6 is equipped with four main fuel tanks that serve individual engines, while a network of valves allow fuel to be transferred from one engine’s tank to feed other engines. The crew did not cross feed fuel from the tank serving the failed engine to balance the plane's weight as recommended in the flight operations manual. Flight 157 had flown for almost three hours with the No. 1 engine out, and the CAB concluded that the No. 1 main fuel tank was holding about 1,400 lbs (635 kg) more gasoline than the other three main tanks when the plane arrived at Love Field. The investigators primarily attributed the left wing’s sharp drop to the excessive weight of the fuel at its outboard end,
- The captain applied excessive rudder during the “S”-turn, causing a condition known in aviation terminology as a skid. This maneuver would have caused the plane’s airspeed to drop, and according to the CAB findings, it caused the fuel in the No. 4 main tank to slosh away from the fuel outlet, lowering the engine’s fuel pressure,
- The captain’s application of full throttle to both right-hand engines caused to airplane to turn further to the left due to the relative lack of thrust from the single functioning left-hand engine. This exacerbated his loss of directional control,
- The first officer disobeyed the captain’s order to raise the wing flaps, and did not tell the captain,
- The first officer misinterpreted the No. 4 engine’s fuel pressure drop as a sign of incipient engine failure and feathered the prop. However, the CAB partially exonerated Lewis for this act, concluding that the craft was so close to the ground at that point that his mistake probably had little influence on the final outcome,
- Excessive elevator input by the captain caused the aircraft to stall.
The CAB concluded that the accident could have been avoided if the crew had held the plane straight and level when the misalignment was first noticed, then raised the flaps, climbed to a safe altitude, circled the airport, and attempted another landing. The CAB concluded that there were no factors present that would compel the crew to land immediately despite the sloppy approach, such as rapidly deteriorating weather or a shortage of fuel.
Final Report:

Crash of a Douglas C-54B-1-DC Skymaster in Dallas

Date & Time: Mar 10, 1948
Type of aircraft:
Operator:
Registration:
N90426
Survivors:
Yes
Schedule:
Tulsa – Los Angeles
MSN:
10433
YOM:
1944
Crew on board:
3
Crew fatalities:
Pax on board:
33
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
During the takeoff roll in Tulsa, the nose gear hit a snowdrift. After departure, during initial climb, the crew was unable to raise the nose gear so the captain decided to divert to Dallas-Love Field for a safe landing. After touchdown, the aircraft slid on its nose and came to rest. There were no casualties but the aircraft was written off.
Probable cause:
Collision with a snowdrift on takeoff.

Crash of a Douglas DC-3-277D in Dallas

Date & Time: Sep 15, 1943
Type of aircraft:
Operator:
Registration:
NC33657
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
4803
YOM:
1942
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Shortly after take off, while in initial climb, the aircraft stalled and crashed in an open field. Both pilots were injured and the aircraft was written off.

Crash of a Douglas DC-2-112 in Oklahoma City: 8 killed

Date & Time: Mar 26, 1939 at 0248 LT
Type of aircraft:
Operator:
Registration:
NC13727
Flight Phase:
Survivors:
Yes
Schedule:
Chicago – Kansas City – Wichita – Oklahoma City – Dallas
MSN:
1253
YOM:
1934
Flight number:
BR001
Crew on board:
3
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
9060
Captain / Total hours on type:
1253.00
Copilot / Total flying hours:
2244
Copilot / Total hours on type:
526
Circumstances:
Shortly after takeoff, while in initial climb, the left engine exploded. The crew attempted to return when, during the last turn at 115°, at a speed of 80 knots, the left wing stalled and hit the ground. The aircraft cartwheeled and crashed some 600 metres from the runway end, bursting into flames. The stewardess and seven passengers were killed.
Crew:
Claude H. Seaton, pilot,
Malcolm Wallace, copilot,
Louise Zarr, stewardess.
Probable cause:
A stall, induced by a violent yaw, resulting in loss of control from which the pilot was unable to recover.
Contributing factors are:
Failure of hold down studs on the number six cylinder of the left engine which resulted in the cylinder being forced off, carrying with it the lower third of the engine ring cowling. Displacement of the remaining portion of the left engine ring cowling, which caused buffeting, as a result of disturbances of the air flow over the tail surfaces, and increased the drag on that side of the aircraft. Severe vibration induced by the continued rotation of the propeller. Lack of individual propeller pitch controls which would have permitted the pilot to increase the pitch of the propeller on the inoperative engine, thereby reducing the speed of rotation and consequently the vibration from the effect of "windmilling".
Final Report:

Crash of a Lockheed 10A Electra in Dallas: 6 killed

Date & Time: Dec 23, 1936
Type of aircraft:
Operator:
Registration:
NC14905
Flight Type:
Survivors:
No
Schedule:
Dallas-Love Field - Dallas-Love Field
MSN:
1018
YOM:
1934
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
The crew (two pilots and four engineers of the company) were conducting a local post maintenance flight out from Dallas Love Field. On final approach, the captain elected to make a go around when an engine failed while trying to climb. The aircraft went into a spin and crashed on the north shore of the Bachman Lake, short of runway. All six occupants were killed and the aircraft was destroyed by impact forces and a post crash fire.
Probable cause:
Engine failure for unknown reasons at a critical phase of flight.