Country
code
Liege
Crash of a Beechcraft 99 Airliner near Liège: 2 killed
Date & Time:
Jun 30, 1999 at 0443 LT
Registration:
D-IBEX
Survivors:
No
Schedule:
Luton - Frankfurt
MSN:
U-45
YOM:
1968
Flight number:
EXT114
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total hours on type:
8200.00
Copilot / Total hours on type:
590
Aircraft flight hours:
34946
Circumstances:
En route from Luton to Frankfurt, while on a night cargo service (flight EXT114), at an altitude of 11,000 feet, the right engine failed and was shut down by the crew. Four minutes later, the left engine failed as well. The crew sent a Pan call and was cleared to divert to Liege-Bierset Airport. Vectored for an approach to runway 23L, the airplane passed FL040 when it entered an uncontrolled descent and crashed in a wooded area located in Seraing, in the south suburb of Liege, 8,3 km southeast of Liege Airport. The aircraft was destroyed by impact forces and both pilots were killed.
Probable cause:
Following the deterioration of the right engine’s turbine blade, one of them broke off, causing significant damage to the turbine and downstream components, which led to the engine shutting down. At that point, in violation of company regulations, the captain decided to continue the flight on one engine while maintaining altitude and a relatively high speed, which required maximum or near-maximum power from the left engine. About four minutes after the right engine shut down, the left engine also failed, following the failure of a compressor turbine blade; the exact cause could not be determined with certainty, but the stress imposed on it at high RPM and temperature certainly contributed to this failure. The crew did not transmit a Mayday call to Air Traffic Control, but did transmit a Pan call on the frequency. The crew did not set the distress code 7700 on their transponder. The controller interpreted this message as a medical issue, which did not strike him as urgent. When the aircraft was transferred to approach control, the problem reported was a medical issue. Immediately, the controller instructed the crew to proceed with a landing procedure to runway 23L at Liege Airport, which was much longer than bringing the aircraft directly in a cross-traffic procedure to runway 05R. When the crew switched frequencies to approach control, the approach controller continued the procedure for runway 23L. The problem reported to him was medical, and, in his mind, there was no reason to clear the crew for a short approach to runway 05R. It was only when the aircraft approached FL040 it was supposed to maintain and the crew told him it was impossible due to a lack of engine power that the approach controller realized the urgency of the situation and directed the aircraft toward the runway at a 90° procedure. At that moment, the aircraft was at such an altitude and distance from the runway that it was impossible for it to reach the runway. At no point did the crew appear to have taken any initiative to attempt to resolve their problem.
The following contributing factors were identified:
- The absence of the seal on the inner guide vane drum of the right engine led to abnormal wear of the guide vanes and subsequently the fracture of a turbine blade, resulting in the engine shutdown.
- At that point, the crew decided to continue the flight, thereby violating the Standard Operating Procedures. An immediate diversion would have subjected the left engine to less stress.
- Approximately four minutes after the right engine shut down, a blade in the left engine’s compressor turbine broke, causing that engine to shut down.
- The crew did not clearly inform ATC about their situation. Sending a Mayday call was fully justified.
- The air traffic controller interpreted the Pan Call as a medical emergency and therefore initiated a standard landing procedure at Liege Airport instead of a cross-traffic emergency procedure. Had the latter been initiated in time and executed correctly, it would have allowed the aircraft to reach the runway.
- The time of day when the events occurred and the lighting conditions contributed to impairing the performance of the crew and the controllers.
- The lack of initiative on part of the crew.
The following contributing factors were identified:
- The absence of the seal on the inner guide vane drum of the right engine led to abnormal wear of the guide vanes and subsequently the fracture of a turbine blade, resulting in the engine shutdown.
- At that point, the crew decided to continue the flight, thereby violating the Standard Operating Procedures. An immediate diversion would have subjected the left engine to less stress.
- Approximately four minutes after the right engine shut down, a blade in the left engine’s compressor turbine broke, causing that engine to shut down.
- The crew did not clearly inform ATC about their situation. Sending a Mayday call was fully justified.
- The air traffic controller interpreted the Pan Call as a medical emergency and therefore initiated a standard landing procedure at Liege Airport instead of a cross-traffic emergency procedure. Had the latter been initiated in time and executed correctly, it would have allowed the aircraft to reach the runway.
- The time of day when the events occurred and the lighting conditions contributed to impairing the performance of the crew and the controllers.
- The lack of initiative on part of the crew.
Final Report:
Crash of a Pilatus PC-6/B1-H2 Turbo Porter in Spa
Date & Time:
Jul 30, 1995 at 1736 LT
Registration:
PH-MEN
Survivors:
No
Schedule:
Spa - Spa
MSN:
707
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The single engine airplane departed Spa-La Sauvenière Aerodrome with eight skydivers and one pilot on board. After all passengers bailed out, the pilot returned to base. On final approach to runway 05, the airplane collided with a private Cessna 172 registered OO-SIW. With three passengers and one pilot on board, the Cessna was also completing an approach to runway 05. Following the collision, both airplanes went out of control and crashed near the airfield. The Cessna 172 was damaged beyond repair and the PC-6 was destroyed by a post crash fire. All four people on board the Cessna were injured while the pilot of the PC-6 was killed.
Probable cause:
The Cessna was on final approach to runway 05 when it was struck on the right side by the PC-6, whose pilot was performing a non standard approach.
Final Report:
Crash of a Cessna 207 Skywagon in Spa
Date & Time:
Aug 8, 1976
Registration:
OO-SPW
Survivors:
Yes
MSN:
207-0211
YOM:
1972
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed in unknown circumstances. No casualties.
Crash of a Miles M.57 Aerovan IV in Spa
Date & Time:
Jun 25, 1961
Registration:
OO-MAP
Survivors:
Yes
MSN:
6397
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed on landing for unknown reason. All four occupants were uninjured while the aircraft was damaged beyond repair.
Crash of an Airspeed AS.10 Oxford II in Liège
Date & Time:
Jun 12, 1958
Registration:
O-11
Survivors:
Yes
Schedule:
Liège - Liège
MSN:
3257
YOM:
1941
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
During the takeoff roll, the left main gear collapsed. The airplane went out of control, veered off runway and came to rest. Both crew members were uninjured while the aircraft was damaged beyond repair.
Probable cause:
Undercarriage collapsed during takeoff roll.
Crash of an Airspeed AS.10 Oxford II in Liège
Date & Time:
Jul 12, 1954
Registration:
O-36
Survivors:
Yes
Schedule:
Liège - Liège
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was performing a local training at Liège-Bierset Airport when on final approach, he was unable to lower the landing gear. The twin engine aircraft belly landed and after a roll of few dozen yards, veered off runway and came to rest. All three crew members were uninjured while the aircraft was considered as damaged beyond repair.
Probable cause:
Failure of the undercarriage to extend on final approach.
Crash of a Douglas C-47A-20-DK near Spa: 4 killed
Date & Time:
Apr 6, 1945 at 1135 LT
Registration:
42-93088
Survivors:
No
Schedule:
Poix – Frankfurt
MSN:
12961
YOM:
1944
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
While cruising in poor weather conditions, the aircraft hit trees and crashed in wooded area located in Fagnes, northwest of Malmedy, near Spa. All four crew members were killed.
Crew:
Cpt James G. Hicks Jr., pilot,
2nd Lt Charles L. Fraser, copilot,
T/Sgt George A. Bishop, flight engineer,
S/Sgt William J. Loughrey, wireless operator.
Crew:
Cpt James G. Hicks Jr., pilot,
2nd Lt Charles L. Fraser, copilot,
T/Sgt George A. Bishop, flight engineer,
S/Sgt William J. Loughrey, wireless operator.