Crash of a Beechcraft B90 King Air near San Jon: killed

Date & Time: May 14, 2001 at 2322 LT
Type of aircraft:
Registration:
N221CH
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Tucson – Springdale
MSN:
LJ-436
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
16800
Captain / Total hours on type:
3000.00
Aircraft flight hours:
7557
Circumstances:
The pilot was flying a pressurized airplane at 25,000 feet (cabin altitude of 10,000 feet). For approximately 43 minutes before the accident, ARTCC called the pilot approximately six times and asked him to correct his altitude. Two transmissions from the pilot, between 2305 and 2311, were made with "slurred, and unclear speech." A 2 minute period followed with over 30 hot mike transmissions in which heavy breathing could be heard in some. At 2318:20, the pilot's last transmission was "ah Charlie Hotel, we, we've a little bit of a problem here. We're in a descent, we'll straighten it out in a minute." Witnesses observed the airplane spin into ground. The pilot's autopsy revealed moderate emphysema in his lungs with the presence of air filled bullae measuring up to 3 cm. On the two flights before the accident flight, the owner of the aircraft said that the pilot slept 2 hours out of the 4.5 hours of flight. Several friends of the pilot reported that he was also observed to "easily doze" off while on the ground, but he did so more regularly and for longer time periods while flying.
Probable cause:
The pilot's failure to maintain aircraft control due to his incapacitation for an undetermined reason. A contributing factor was the subsequent inadvertent stall/spin to the ground.
Final Report:

Crash of a Piper PA-31T Cheyenne I in Santa Fe

Date & Time: Dec 16, 1999 at 1515 LT
Type of aircraft:
Registration:
N919RD
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Santa Fe - Olathe
MSN:
31-8104037
YOM:
1981
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1098
Captain / Total hours on type:
401.00
Aircraft flight hours:
3558
Circumstances:
On takeoff during the initiation of a cross-country flight, the pilot raised the landing gear following liftoff and the aircraft settled back onto the ground off the end of the runway. According to the pilot and the FAA inspector who examined the aircraft, both engines were producing normal power. The elevator trim was set at 12 degrees nose up vice 3-6 degrees required, and the aircraft was within weight and balance limits. The pilot lowered the landing gear prior to impact. According to information provided by the aircraft manufacturer, induced drag increases during landing gear retraction and extension due to the landing gear doors being extended into the air stream as the landing gear cycles.
Probable cause:
The pilot initiating lift off at an airspeed insufficient to maintain flight and retracting the landing gear prematurely resulting in a stall mush. A factor was the pilot incorrectly setting the elevator trim.
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601) in Ruidoso: 2 killed

Date & Time: Apr 23, 1999 at 1023 LT
Registration:
N48MD
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Ruidoso – North Las Vegas
MSN:
61-0492-201
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3681
Captain / Total hours on type:
597.00
Aircraft flight hours:
4526
Circumstances:
The pilot departed on runway 06 with zero degrees of flaps. A witness said that she noticed that the airplane appeared to wobble and shudder, and immediately went into a steep right bank turn right after takeoff. The airplane then went into the clouds which were 200 to 400 feet agl. Radar data indicated that the airplane made several 90 degree turns prior to impacting the mountainous terrain 2.55 nm from the departure end of the runway. The pilot normally used 20 degrees of flaps for takeoff. A test pilot said that the airplane handles significantly different during takeoff if zero degrees of flaps are used verses 20 degrees of flaps. The upper cabin's entry door was found, with the locking handle and locking pins, in the closed position. No preimpact engine or airframe anomalies, which might have affected the airplane's performance, were identified.
Probable cause:
The pilot's failure to maintain aircraft control for undetermined reason. A factor was the low ceiling IMC weather condition.
Final Report:

Crash of a Lockheed P2V-7-SP-2H Neptune in Reserve: 2 killed

Date & Time: Jun 27, 1998 at 2024 LT
Type of aircraft:
Operator:
Registration:
N14835
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Silver City - Silver City
MSN:
148358
YOM:
1961
Flight number:
Tanker 08
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
8337
Captain / Total hours on type:
291.00
Aircraft flight hours:
7815
Circumstances:
The airplane had made a dry pass on the fire zone, then circled around to make a second pass and release its load of 2,450 gallons of retardant. According to witnesses, the airplane struck trees while in a nose low, right wing low attitude. Upon ground impact, the airplane exploded and burned. Investigation revealed no evidence of preimpact airframe, engine, propeller, or flight control failure/malfunction. The first officer, an initial attack trainee pilot, was in the left seat and the captain was in the right seat. Toxicology tests of the first officer indicated 0.031 ug/ml brompheniramine, 0.011 ug/ml chlorpheniramine in kidney fluid, and 0.142 brompheniramine, 0.072 chlorpheniramine in liver fluid. Both medications are over-the-counter antihistamines with sedative effects.
Probable cause:
Failure of the copilot to maintain both lateral and vertical clearance from the trees, and failure of the captain to provide adequate supervision of the flight.
Final Report:

Crash of a Cessna 421B Golden Eagle II near Conchas

Date & Time: Aug 30, 1996 at 1830 LT
Operator:
Registration:
N55HU
Flight Phase:
Survivors:
Yes
Schedule:
Albuquerque - Alva
MSN:
421B-0014
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2934
Captain / Total hours on type:
67.00
Aircraft flight hours:
2700
Circumstances:
At 1615, the pilot called FSS for a weather briefing and to file an IFR flight plan. He was told that there was thunderstorm activity, which was building in intensity, extending from Raton, New Mexico, to Garden City, Kansas, with some scattered activity in the Oklahoma panhandle. The briefer further reported that the thunderstorm activity was moving east, southeast. The pilot checked in with Albuquerque Center at 1750 during his departure climb to 21,000 feet. At 1755, convective SIGMET 70C was issued for isolated severe thunderstorms located 10 miles north, northeast, of Las Vegas, New Mexico. FAA Order 7110.65J, Air Traffic Control, section 2-6-2, states that 'controllers shall advise pilots of hazardous weather that may impact operations within 150 NM of their sector or area of jurisdiction.' SIGMET 70C was not given to the pilot by the center controller. Radio contact was lost at 1823. The pilot reported that the airplane was in VMC, approaching precipitation, when they encountered hail and the pilot's windshield was broken out which resulted in the airplane's depressurization.
Probable cause:
The pilot's inadvertent flight into hail which shattered the pilot's windshield and resulted in his incapacitation due to hypoxia.
Final Report:

Crash of a Cessna 421C Golden Eagle III near Taos: 4 killed

Date & Time: Mar 5, 1995 at 1355 LT
Registration:
N421BL
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Oklahoma City - Taos
MSN:
421C-0605
YOM:
1979
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
809
Captain / Total hours on type:
195.00
Circumstances:
The pilot obtained a weather briefing for the IFR flight to Taos, New Mexico, and was advised of forecast conditions for light to moderate rime icing and moderate turbulence at his destination. During descent, about 30 nm east of the Taos VOR, at 15,200 feet, the pilot reported 'light rime icing' and 3 minutes later 'freezing rain.' The airplane was cleared for the VOR DME-B approach to the Taos Airport, and radar services were terminated. The airplane impacted the ground in a steep nose down attitude 7 nm southeast of the VOR and 1 nm right of the inbound approach course. Weather data indicated that the airplane entered clouds about 6 nm east of where 'light rime' was reported and remained in the clouds until it descended below 10,000 feet. Meteorological investigation indicated that the freezing level was about 10,700 feet. Radar data revealed cyclic variations in the airplane's ground speed from 120 to 190 knots, as it crossed the high mountain range east of taos. There was a pirep of severe turbulence on the eastern slope of the mountain range. All four occupants were killed.
Probable cause:
The pilot's decision to continue flight into known adverse weather conditions and the ensuing inadvertent stall due to airframe ice. Factors were the weather conditions.
Final Report:

Crash of a Beechcraft A60 Duke in Hurley: 3 killed

Date & Time: Jan 5, 1995 at 1835 LT
Type of aircraft:
Registration:
N3LP
Survivors:
No
MSN:
P-242
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
2746
Captain / Total hours on type:
209.00
Circumstances:
During climb to cruise the pilot reported a power loss on one engine and received vectors for a return to the departure airport. The pilot was subsequently cleared for the VOR-A approach and reported intercepting the inbound radial. The impact site was right of the inbound radial and short of the extended runway centerline. Weather at the airport was VFR. Post impact fire damaged the airplane. The left engine propeller was in the feather position. Visual and metallurgical examination confirmed the turbocharger shaft separated due to fatigue. The shaft contained chromium. The aircraft overhaul manual states that 'chrome plating...restoration of the shaft...are not permitted.' Metallographics revealed a microstructure of grey iron (automotive application) in the center housing. The turbocharger was overhauled and installed on the left engine in october 1989. All three occupants were killed.
Probable cause:
The pilot's failure to maintain airspeed during a single engine approach resulting in an inadvertent stall. Factors were a fatigue separation of a shaft in the left engine turbocharger due to use of a Federal Aviation Administration approved overhaul procedure that was not consistent with the manufacturer's overhaul procedure, and the resultant loss of power to the left engine.
Final Report:

Crash of a Learjet 25D on Mt Rowe: 7 killed

Date & Time: Sep 5, 1993 at 1715 LT
Type of aircraft:
Registration:
N999BH
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Houston - Santa Fe
MSN:
25-318
YOM:
1980
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
17000
Captain / Total hours on type:
4000.00
Aircraft flight hours:
4973
Circumstances:
While descending to his destination the pilot in command (pic) canceled his IFR clearance and declined VFR flight following. Witnesses observed the aircraft maneuvering at low altitude in the area where the accident occurred, approximately 25 miles from the destination airport. The aircraft impacted rising terrain at 7,300 feet msl. Toxicological testing revealed that the pic and two passengers had cocaine and alcohol in tissue samples. At an unknown time the pic left the cockpit. Based on cockpit voice recorder analysis, he was called back to the cockpit approximately 11 minutes prior to the accident by the copilot. The copilot had no previous Lear experience. Toxicological test results indicated that the pic 'used cocaine in the very recent past, probably while in-flight' and concluded that he 'was impaired by multiple drug use of cocaine and alcohol.' The investigation did not reveal any structural or system failure or malfunction. All seven occupants were killed.
Probable cause:
Physical impairment of the pilot in command from alcohol and drugs. A factor was the first officer's lack of experience in the Learjet.
Final Report: