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Crash of a Mitsubishi MU-2B-60 Marquise in Sioux Falls: 1 killed

Date & Time: Jun 7, 2020 at 0415 LT
Type of aircraft:
Operator:
Registration:
N44MX
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Everett – Huron - Kokomo
MSN:
1526
YOM:
1981
Flight number:
MDS44
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
22000
Captain / Total hours on type:
10900.00
Aircraft flight hours:
12104
Circumstances:
The pilot departed on a cross country flight in a turbine-powered, multiengine airplane at night and in visual meteorological conditions. Recovered GPS data revealed that as the airplane accelerated down the runway, it drifted to the right of the runway centerline. A video recording showed that shortly after takeoff, the airplane rolled right, the nose dropped, and the airplane impacted the ground. It came to rest on its left side with both wings separated and the fuselage was highly fragmented forward of the main landing gear. A post-accident examination of the airframe and engines found no mechanical malfunctions or anomalies that would have precluded normal operation. A witness that spoke to the pilot shortly before the accident flight stated that the pilot exhibited difficulty in completing some paperwork; however, no medical reasoning for this difficulty could be determined based upon the available evidence. The investigation determined that at the time of the accident the pilot had been on duty for about 19 hours and 20 minutes, which was contrary to duty and rest regulations. At his estimated arrival time into the destination, the pilot would have accumulated about 20 hours and 54 minutes of duty time. The investigation was unable to determine if the pilot took advantage of the opportunity for rest that existed during the day, and therefore could not determine if fatigue contributed to the accident. Investigators were unable to determine the reason for the loss of control on takeoff with the available information.
Probable cause:
The pilot’s failure to maintain control of the airplane during takeoff for reasons that could not be determined.
Final Report:

Crash of a Mitsubishi MU-2B-36 Marquise in West Memphis: 1 killed

Date & Time: Sep 22, 2005 at 1958 LT
Type of aircraft:
Operator:
Registration:
N103RC
Flight Type:
Survivors:
No
Schedule:
West Memphis - Gainesville
MSN:
673
YOM:
1975
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
12600
Captain / Total hours on type:
1900.00
Aircraft flight hours:
10892
Circumstances:
The twin-engine airplane was destroyed when it impacted an earthmoving scraper and terrain in a field about 2.5 miles north of the departure airport in night visual meteorological conditions. Witnesses reported that the pilot had aborted an earlier flight when he returned to the airport and told the mechanic that he had a right engine fire warning light. The discrepancy could not be duplicated during maintenance, and the airplane departed. About 23 minutes after departure, the pilot reported to air traffic control that he needed to return to the airport to have something checked out. The pilot did not report to anyone why he decided to return to the departure airport, and he flew over four airports when he returned to the departure airport. Radar track data indicated that the airplane flew over the departure end of runway 35 at an altitude of about 1,600 feet agl, and made a descending left turn. The airplane's altitude was about 800 feet agl when it crossed the final approach course for runway 35. The airplane continued the descending left turn, but instead of landing on runway 35, the airplane flew a course that paralleled the runway, about 0.8 nm to the right of runway 35. The airplane continued to fly a northerly heading and continued to descend. The radar track data indicated that the airplane's airspeed was decreasing from about 130 kts to about 110 kts during the last one minute and fifty seconds of flight. The last reinforced beacon return indicated that the airplane's altitude was about 200 feet agl, and the airspeed was about 107 kts. The airplane impacted terrain about 0.75 nm from the last radar contact on a 338-degree magnetic heading. A witness reported that the airplane was going slow and was "extremely low." He reported that the airplane disappeared, and then there was an explosion and a fireball that went up about 1,000 feet. Inspection of the airplane revealed that it impacted the earthmover in about a wings level attitude. The landing gear handle was found to be in the landing gear UP position. The inspection of the left engine and propeller revealed damage indicative of engine operation at the time of impact. Inspection of the right engine revealed damage indicative of the engine not operating at the time of impact, consistent with an engine shutdown and a feathered propeller. No pre-existing conditions were found in either engine that would have interfered with normal operation. The inspection of the right engine fire detection loop revealed that the connector had surface contamination. When tested, an intermittent signal was produced which could give a fire alarm indication to the pilot. After the surface contamination was removed, the fire warning detection loop operated normally.
Probable cause:
The pilot's improper in-flight decision not to land at the departure runway or other available airports during the emergency descent, and his failure to maintain clearance from a vehicle and terrain. Contributing factors were a false engine fire warning light, inadequate maintenance by company personnel, a contaminated fire warning detection loop, and night conditions.
Final Report:

Crash of a Douglas DC-3C in Memphis

Date & Time: Nov 7, 1997 at 1956 LT
Type of aircraft:
Operator:
Registration:
N59316
Flight Type:
Survivors:
Yes
Schedule:
Gulfport - West Memphis
MSN:
18986
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7853
Captain / Total hours on type:
2603.00
Aircraft flight hours:
24516
Circumstances:
The PIC stated he was established on an instrument approach when the left engine fuel pressure dropped to zero and the engine quit. He moved the fuel selector to the right rear fuel tank and the engine started. He continued the approach for about 2 miles when the right engine quit followed by the left engine. He made a forced landing to a sandbar. Examination of the airplane revealed the fuel tanks were not ruptured and the fuel tanks were empty.
Probable cause:
The pilot-in-command's improper management of fuel resulting in a total loss of engine power on both engines during an instrument approach due to fuel exhaustion.
Final Report: