Crash of a Gulfstream GIII in Biggin Hill

Date & Time: Nov 24, 2014 at 2030 LT
Type of aircraft:
Operator:
Registration:
N103CD
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Biggin Hill - Gander
MSN:
418
YOM:
1984
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4120
Captain / Total hours on type:
3650.00
Circumstances:
On 24 November 2014 the crew of Gulfstream III N103CD planned for a private flight from Biggin Hill Airport to Gander International Airport in Canada. The weather reported at the airport at 2020 hrs was wind ‘calm’, greater than 10 km visibility with fog patches, no significant cloud, temperature 5°C, dew point 4°C and QNH 1027 hPa. At 2024 hrs, the crew was cleared to taxi to Holding Point J1 for a departure from Runway 03. After the crew read back the taxi clearance, the controller transmitted: “we are giving low level fog patches on the airfield, general visibility in excess of 10 km but visibility not measured in the fog patches. it seems to be very low, very thin fog from the zero three threshold to approximately half way down the runway then it looks completely clear”. The crew acknowledged the information. At 2028 hrs, the aircraft was at the holding point and was cleared for takeoff by the controller. The aircraft taxied towards the runway from J1 but lined up with the runway edge lights, which were positioned 3 m to the right of the edge of the runway. The aircraft began its takeoff run at 2030 hrs, passing over paved surface for approximately 248 m before running onto grass which lay beyond. The commander, who was the handling pilot, closed the thrust levers to reject the takeoff when he realized what had happened and the aircraft came to a halt on the grass having suffered major structural damage. The crew shut down the engines but were unable to contact ATC on the radio to tell the controller what had happened. The co-pilot moved from the flight deck into the passenger cabin and saw that no one had been injured. He vacated the aircraft through the rear baggage compartment and then helped the commander, who was still inside, to open the main exit door. The commander and the five passengers used the main exit to vacate the aircraft. The controller saw that the aircraft had stopped but did not realize that it was not on the runway. He attempted to contact the crew on the radio but, when he saw the lights of the aircraft switch off, he activated the crash alarm, at 2032 hrs, declaring an aircraft ground incident. At 2034 hrs the airport fire service reached the aircraft and declared an aircraft accident, after which the airport emergency plan was activated.
Probable cause:
This was a private flight which could not depart in conditions of less than 400 m RVR. RVR cannot be measured at the threshold end of Runway 03 but the prevailing visibility was reported as being more than 10 km. The crew reported that there was moisture on the windscreen from the mist and they could see a “glow” around lights which were visible to them. They were also aware while taxiing that there was some patchy ground fog on the airfield. The ATC controller transmitted that visibility had not been measured in the fog patches but there seemed to be ‘very low, very thin fog from the zero three threshold to approximately half way down the runway’. With hindsight, this piece of information is significant but, at the time, the crew did not consider the fog to be widespread or thick; operating under FAR Part 91 in the United States, they were used to making their own judgments as to whether the visibility was suitable for a takeoff. However, after the aircraft came to a halt following its abortive takeoff attempt, the controller could only see the top of the fuselage and tail above the layer of fog. It is likely, therefore, that the visibility was worse than the crew appreciated at the time N103CD taxied from Holding Point J1. The route from J1 to the runway The information on the aerodrome chart used by the crew, and the source of information in the UK AIP, suggested that the aircraft would be required to taxi in a straight line from J1 to the runway and then make a right turn onto the runway heading. In fact, in order to taxi from J1 onto the runway, an aircraft must: taxi in a straight line; follow a curve to the right onto runway heading but still displaced to the right of the runway itself; turn left towards the runway; and then turn right again onto runway heading. The UK AIP states that there is no centreline lighting on Runway 03, and that the pavement width at the beginning of the runway is twice the normal runway width. It recognizes the potential for confusion and urges crews to ensure that they have lined up correctly. This information was not available to the crew on their aerodrome charts and both crew members believed that the runway had centreline lighting. Further, the light from those left-side runway edge lights covered in fog would have been scattered, making it harder for the crew to perceive them as a distinct line of lights. The situation is likely to have been made worse by the bright lights reflecting off the top of the fog layer, making the underlying runway lights even harder to see, or swamping them completely as shown in Figure 5. The CCTV images in Figure 5 show that peripheral lighting can interact with low fog layers to reduce the visibility of underlying aerodrome lighting. Current standards associated with apron lighting only address the minimum light levels required to make the areas safe and there are no standards relating to light spilling into other areas.
Human and environmental factors Five of the factors identified by the ATSB as being present in misaligned takeoffs were present in this accident:
1. It was dark.
2. It was potentially a confusing taxiway environment given that the aerodrome chart did not reflect the actual layout of the taxiways. Pilots had previously reported having difficulty when vacating the runway near the Runway 03 threshold because of a lack of taxiway lighting.
3. There was an additional paved area (the ORP) near the runway.
4. There was no runway centreline lighting and the runway edge lights before the displaced threshold were recessed.
5. There was reduced visibility.
It appeared that the information available to the crew caused them to develop an incorrect expectation of their route to the runway. Both crew members believed that the runway had centreline lighting and, when the first right turn almost lined the aircraft up with some lights, their incorrect expectation was reinforced and they believed that the aircraft was lined up correctly. Cues to the contrary, such as runway edge lights on the other side of the runway, or the fact that the first three lights ahead of the aircraft were red (indicating that they were edge lights before the displaced threshold), did not appear to have been strong enough to make the crew realize that they had lost situational awareness. Figure 8 indicates that the apparent intensity of the white left-side runway edge lights was significantly less than that of the right-side lights, when viewed from the position where the aircraft lined up. This, along with other visual issues relating to contrast and the fog, is a plausible explanation as to why they were not noticed by the crew. The aircraft began its takeoff roll from a location beyond the first red runway edge light and approximately 46 m short of the next light, as shown in Figure 1. Aircraft structure only obscures approximately the first 13 m of pavement ahead of pilots within a Gulfstream III aircraft and therefore these lights would not have been obscured by the aircraft. However, it is likely that the recessed nature of the red edge lights before the displaced threshold made them less compelling than the elevated white edge lights beyond, which would explain why their significance – that they could only have been runway edge lights – was not appreciated by the flight crew.
Final Report:

Crash of a Cessna 500 Citation I in Biggin Hill: 5 killed

Date & Time: Mar 30, 2008 at 1438 LT
Type of aircraft:
Registration:
VP-BGE
Flight Phase:
Survivors:
No
Site:
Schedule:
Biggin Hill – Pau
MSN:
500-0287
YOM:
1975
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
8278
Captain / Total hours on type:
18.00
Copilot / Total flying hours:
4533
Copilot / Total hours on type:
70
Aircraft flight hours:
5844
Aircraft flight cycles:
5352
Circumstances:
Pilot B arrived at Biggin Hill Airport, Kent, at about 1100 hrs for the planned flight to Pau, France. At about 1130 hrs he helped tow the aircraft from its overnight parking position on the Southern Apron to a nearby handling agent whose services were being used for the flight. A member of staff employed by the handling agent saw Pilot B carry out what was believed to be an external pre-flight check of the aircraft. Pilot B also asked another member of staff to provide a print out of the weather information for the flight. Pilot A arrived at about 1145 hrs and joined Pilot B at the aircraft. Witnesses described nothing unusual in either pilots’ demeanour. Three passengers arrived at the handling agent at about 1300 hrs and waited in a lounge whilst their bags were taken to the aircraft and loaded into the baggage hold in the nose. A member of the handling agency, who later took the passengers to the aircraft, reported that Pilot B met them outside the aircraft. After they had all boarded, the agent heard Pilot B say that he would give them a safety brief. Pilot B then closed the aircraft door. Pilot A called for start at 1317 hrs. He called for taxi at 1320 hrs and the aircraft was cleared to taxi to the holding point A1. No one could be identified as a witness to the aircraft’s start or subsequent taxi to the holding point. At 1331 hrs ATC cleared the aircraft to line up on Runway 21 and at 1332 hrs cleared it to take off. Both clearances were acknowledged by Pilot A. The takeoff was observed by the tower controller who stated that everything appeared normal. No transmissions were made between the aircraft and ATC until one minute after takeoff when, at 1334 hrs, the following exchange was made. Numerous witnesses reported seeing the aircraft at around this time flying over a built-up area, about 2 nm north-north-east of Biggin Hill Airport, where it was observed flying low, passing over playing fields and nearby houses. Witnesses reported that the aircraft was maintaining a normal flying attitude with some reporting that the landing gear was up and others that it was down. Some described seeing it adopt a nose-high attitude and banking away from the houses just before it crashed. Some witnesses stated that there was no engine noise coming from the aircraft whilst others stated that they became aware of the aircraft as it flew low overhead due to the loud noise it was making, as if the engines were at high thrust. Two witnesses described hearing the aircraft make a pulsing, intermittent noise. The location of witnesses and the description of the aircraft noise they heard are also shown in Figure 1. Having flown over several houses at an extremely low height the aircraft’s left wing clipped a house which bordered a small area of woodland. The aircraft then impacted the ground between this and another house and caught fire. There were no injuries to anyone on the ground but all those on board the aircraft were fatally injured.
Probable cause:
The following contributory factors were identified:
1. It is probable that a mechanical failure within the air cycle machine caused the vibration which led to the crew attempting to return to the departure airfield.
2. A missing rivet head on the left engine fuel shut-off lever may have led to an inadvertent shut-down of that engine.
3. Approximately 70 seconds prior to impact neither engine was producing any thrust.
4. A relight attempt on the second engine was probably started before the relit first engine had reached idle speed, resulting in insufficient time for enough thrust to be developed to arrest the aircraft’s rate of descent before ground impact.
Final Report:

Crash of a Rockwell Shrike Commander 500S off Vestmannaeyjar: 2 killed

Date & Time: Sep 23, 1994 at 2102 LT
Registration:
N9082N
Flight Type:
Survivors:
No
Schedule:
Biggin Hill – Reykjavik
MSN:
500-3068
YOM:
1970
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The crew was repatriating the aircraft from Kinshasa, Zaire, to the US. On the leg from Biggin Hill to Reykjavik, while approaching the Icelandic coast, the left engine failed. The crew declared an emergency and was cleared to divert to Vestmannaeyjar Airport. While circling for landing, the right engine failed as well. The crew lost control of the airplane that crashed in the sea few km offshore. Both occupants were killed.
Probable cause:
It was determined that the cause of the dual engine failure was the presence of a foreign material in the airframe fuel filters, causing restriction of the fuel flow and fuel starvation to both engines.

Crash of a Swearingen SA227AC Metro III in Troyes

Date & Time: Sep 19, 1993 at 1240 LT
Type of aircraft:
Operator:
Registration:
F-GILN
Flight Phase:
Survivors:
Yes
Schedule:
Troyes - Biggin Hill
MSN:
AC-458
YOM:
1981
Location:
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
17
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2400
Captain / Total hours on type:
200.00
Copilot / Total flying hours:
640
Copilot / Total hours on type:
220
Aircraft flight hours:
13436
Circumstances:
The aircraft has been chartered to transfer to Biggin Hill, UK, 17 people who suffered a bus accident two days ago. During the takeoff roll from Troyes-Barberey Airport, after a course of 1,100 metres, at a speed of about 100 knots, the right engine power dropped from 93% to 40%. In the meantime, the temperature of the right engine increased. As the aircraft was veered to the right, the captain decided to abort and started an emergency braking procedure. Unable to stop within the remaining distance, the aircraft overran, rolled for about 150 metres, went through a fence and eventually collided with the localizer antenna. All 19 occupants escaped uninjured while the aircraft was written off.
Probable cause:
The accident appears to be due to a combination of a positioning error of the Speed Levers at the time of take-off, leading to the overheating of both engines, which forced the take-off to stop, and to the preparation and insufficient management of the take-off, leading to an underestimation of the acceleration-stop distance and a late decision to reject the take-off.
The following contributing factors were reported:
- The fouling of the brakes, which reduced their performance,
- The failure to update the aircraft's base weight in the operations manual,
- The crew's very limited experience on type of aircraft,
- The aircraft total weight was 300 kg above MTOW.
Final Report:

Crash of a Piper PA-46-310P Malibu in Stockholm: 3 killed

Date & Time: Dec 3, 1992 at 0706 LT
Operator:
Flight Phase:
Survivors:
No
Site:
Schedule:
Stockholm - Biggin Hill
MSN:
46-08118
YOM:
1988
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
386
Captain / Total hours on type:
127.00
Aircraft flight hours:
845
Circumstances:
The single engine aircraft departed Stockholm-Bromma Airport runway 12 at 0703LT on a charter flight to Biggin Hill, carrying two passengers and one pilot. During climbout, at an altitude of 1,500 feet, the pilot was cleared to turn right and to continue to climb to FL040. At an altitude of 2,200 feet, the aircraft entered an uncontrolled descent then partially disintegrated in the air and eventually crashed in a residential area located in Åkeslund, south of the airport, three minutes after takeoff. Several cars and apartments were destroyed but no one on the ground was injured. The aircraft was destroyed and all three occupants were killed. At the time of the accident, weather conditions were marginal with clouds and turbulences.
Probable cause:
It was determined that the aircraft was operated with a speed 30% above the maneuverable speed when, in turbulences, the left wing broke away due to excessive g loads. The aircraft entered an uncontrolled descent and partially disintegrated before final impact. A probable disconnection or malfunction of the gyro horizon/automatic pilot system as well as a wrong trim on part of the pilot were considered as contributing factors.
Final Report:

Crash of a Short 330-200 in Southend

Date & Time: Jan 11, 1988 at 1244 LT
Type of aircraft:
Operator:
Registration:
G-BHWT
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Southend - Biggin Hill
MSN:
3049
YOM:
1980
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After being parked at Southend Airport for a long time without any maintenance and due to hydraulic problems, it was decided to ferry the aircraft from Southend to Biggin Hill. While taxiing, the nosewheel steering system failed and the crew lost control of the aircraft that veered to the left and collided with a parked British Air Ferries Vickers 806 Viscount registered G-APIM. Both pilots escaped uninjured and both aircraft were damaged beyond repair.
Probable cause:
Corrosion within the emergency brake accumulator had allowed nitrogen to enter the main hydraulic system. In the past, the aircraft had been parked in the open for a considerable time without servicing.

Crash of a Douglas A-26C Invader in Biggin Hill: 7 killed

Date & Time: Sep 21, 1980 at 1514 LT
Type of aircraft:
Registration:
N3710G
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Biggin Hill - Biggin Hill
MSN:
18759
YOM:
1943
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
8000
Captain / Total hours on type:
200.00
Circumstances:
The aircraft was taking part to an airshow at Biggin Hill Airport for the Battle of Britain air display. Shortly after take off from runway 21, the pilot made a turn to pass over the airport when the aircraft nosed down and crashed in a huge ball of fire about 500 yards from the airfield. All seven occupants were killed.
Crew:
Don Bullock, pilot.
Passengers:
Peter Warren,
Arthur Heath,
Don Thompson,
Kevin Vince,
Gary French,
Roger Russell.
Probable cause:
The exact cause of the accident could not be determined. The airplane was intact until impact and both engines were running properly.
Final Report:

Crash of a De Havilland DH.104 Dove 5 in Biggin Hill

Date & Time: Apr 18, 1975
Type of aircraft:
Operator:
Registration:
G-ASDD
Flight Phase:
Survivors:
Yes
MSN:
04452
YOM:
1970
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After takeoff from Biggin Hill Airport, the airplane failed to gain sufficient height and struck tree tops located past the runway end. The crew completed a downwind circuit and was able to return for an emergency landing. There were no injuries but the aircraft was considered as damaged beyond repair.

Crash of a De Havilland DH.114 Heron in Biggin Hill: 2 killed

Date & Time: Jul 10, 1961
Type of aircraft:
Registration:
G-AMTS
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Biggin Hill - Biggin Hill
MSN:
14007
YOM:
1956
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The crew was engaged in a local training flight at Biggin Hill. Following a stabilized approach with the engine number four voluntarily inoperative, the crew landed properly on runway, rolled for few dozen yards and increased power to takeoff. After liftoff, while in initial climb, the aircraft encountered difficulties to gain height and struck several trees and the roof of a house before crashing in flames in a field. The aircraft was destroyed and both crew members were killed.
Probable cause:
It was determined that the loss of control during initial climb was caused by a wrong takeoff configuration on part of the crew who forgot to position the flaps in a correct angle for takeoff. At impact, flaps were in the same full down position than during the landing procedure. As a result, the speed of the aircraft during the initial climb was too low, especially since the number four engine was inoperative.

Crash of a Douglas C-47B-5-DK in Le Plessis-Gassot: 18 killed

Date & Time: Jan 18, 1945 at 0930 LT
Operator:
Registration:
43-48611
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Paris-Le Bourget - Biggin Hill
MSN:
25872/14427
YOM:
1944
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
18
Pax fatalities:
Other fatalities:
Total fatalities:
18
Circumstances:
At 0923LT, the airplane departed Paris-Le Bourget Airport on a flight to Biggin Hill. Seven minutes later, it went out of control and crashed in a field located in Le Plessis-Gassot, about 8 km north of the airport. Four passengers were seriously injured while 18 other occupants were killed.
Crew (37th ATG):
2nd Lt Roy J. Shilling, pilot, †
2nd Lt George A. Wood, copilot, †
Cpl Alphonse V. Cogozzo, radio operator, †
Cpl Harold W. Grubb, flight engineer. †
Passengers:
Cpt Roy Greene, †
Cpt John C. Gregg, †
S/Sgt Edward Shufflebotham, †
T/Sgt Ralph E. Hersbergen,
T/Sgt William H. Patterson, †
S/Sgt Frank Schlucker, †
S/Sgt Henry J. Coon, †
S7Sgt Francis T. Cionek,
S/Sgt Matthew J. Hirech, †
S/Sgt Moses J. Hirsch,
S/Sgt Anthony Zalewski, †
S/Sgt Walter D. Domress,
T/Sgt Robert J. Simon, †
T/Sgt Angelo J. Lavenia, †
Pvt Fred W. Bonness, †
M/Sgt Eugene L. Borengasser, †
M/Sgt Roamy Eugene Dandridge. †