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Crash of a Cessna 207A Stationair 7 near Jabiru

Date & Time: Jan 7, 1991 at 1523 LT
Operator:
Registration:
VH-MNN
Flight Phase:
Survivors:
Yes
Schedule:
Jabiru - Jabiru
MSN:
207-0439
YOM:
1978
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft was nearing the completion of a scenic flight, maintaining about 800 feet above ground level, when the engine power reduced to 20 inches hg manifold pressure. The engine continued to run smoothly but failed to respond when the pilot advanced the throttle. All other means attempted by the pilot to restore the lost power were unsuccessful. The aircraft, which had a full compliment of persons on board, was too heavy to maintain height under these conditions. As it was flying over forest the pilot turned the aircraft towards the south-west where a more favourable open area, with a road and an airstrip, was available. This entailed having to cross an escarpment, but due to the aircraft's rate of descent insufficient height remained, committing the pilot to a forced landing in an unsuitable area. The pilot transmitted a distress call, gave the passengers a thorough briefing and prepared the aircraft for the forced landing. The aircraft was slowed down and allowed to sink slowly into the forest, contacting the first tree about seven metres above ground level. It then continued through the trees for 40 metres before coming to rest inverted on the forest floor. All passengers evacuated from the aircraft and were rescued by a helicopter which had responded to the distress call.
Probable cause:
Inspection of the engine determined that it was capable of developing full power at the time of the accident. The throttle cable was found to have separated from the cast bronze throttle control lever at the fuel/air metering unit on the intake manifold. The serrated steel bush in the throttle control lever at the cable attachment had become loose, causing the hole to wear elongated which reduced the edge distance from the hole to the end of the control lever sufficiently for it to fail when the throttle was opened. This probably occurred during the last takeoff. During flight, the bush, which was still attached to the cable ball end by the bolt, was probably in such a position as to operate the lever when the throttle control was moved to reduce power for climb and cruise. As the flight progressed and the cable separated from the lever, in-flight movement and vibration would have moved the throttle towards the closed position, with the subsequent reduction in power. Further inspection found that the assembly of the cable to the lever was incorrect, with the washer from under the bolt head being omitted. This reduced the bearing area at the bolt head to the control lever, with the possibility that the bolt may have only been clamped to the bush assisting any movement of the bush in the lever. Once the steel bush started moving in the softer bronze material the rate of wear would have been rapid. The aircraft had flown 85 hours since the last periodic inspection, at which time it may have been possible to detect the first signs of wear between the bush and the control lever if information advising of this type of fault had been available.
The following factors were considered relevant to the development of the accident:
- Incorrect assembly of the washers on the control cable attachment bolt may have allowed the bush to start moving in the lever.
- The bush became loose in the control lever, with the subsequent wear elongating the hole allowing the control lever end to fail.
- The throttle control cable separated from the throttle control lever.
- The throttle closed sufficiently during flight to reduce engine power.
- The aircraft was too heavy to maintain flight.
- The aircraft was operating over an area unsuitable for a forced landing.
- Wear between the bush and the lever may have been detectable during the previous periodic inspection if advisory information had been available.
Final Report:

Crash of a Beechcraft E90 King Air in Wondai: 5 killed

Date & Time: Jul 26, 1990 at 2248 LT
Type of aircraft:
Operator:
Registration:
VH-LFH
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Cairns – Wondai – Camden
MSN:
LW-255
YOM:
1978
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
2654
Captain / Total hours on type:
285.00
Circumstances:
Beech E90 VH-LFH was being flown by the owner as pilot-in-command for the flight. The pilot had submitted a flight plan nominating a private category, single pilot, instrument flight rules (IFR) flight, from Cairns to Wondai and thence to Camden. VH-LFH, with six passengers on board, departed Cairns at 1830 hours EST and arrived at Wondai at 2142 hours after an uneventful flight. One passenger left the aircraft at Wondai. The aircraft was refuelled with 800 litres of aviation turbine fuel and the pilot reported taxying for Runway 36 at Wondai to Brisbane Flight Service at 2243 hours EST. The aircraft was issued an airways clearance at 2245 hours which the pilot acknowledged correctly. The last radio contact with the aircraft was at 2248 hours when the pilot reported airborne. Witnesses observed the aircraft take-off and a short time later heard the sound of impact. The aircraft struck a line of small trees slightly left of the runway extended centreline and 600 metres from the end of the runway in a wings level attitude and in a very shallow descent. Forty-eight metres beyond this point, the aircraft impacted the ground and began to break up. It then contacted a number of large trees and caught fire, finally coming to rest 90 metres further on. A passenger was seriously injured while five other occupants were killed.
Probable cause:
The circumstances leading to the development of this accident could not be established conclusively. However, the evidence supports the following as probable factors:
- The pilot might not have been aware of the human factors aspects associated with dark night take-offs.
- The pilot could have been influenced by stress and/or fatigue.
- The aircraft was taking off towards dark textureless terrain and no visible horizon.
- By transmitting his airborne call very soon after lift-off, the pilot was not devoting his full attention to flying the aircraft.
- The pilot became disoriented and placed the aircraft in a shallow descent as it accelerated after take-off.
Final Report:

Crash of a Cessna 501 Citation I/SP in Lord Howe Island

Date & Time: Apr 22, 1990 at 1225 LT
Type of aircraft:
Operator:
Registration:
VH-LCL
Flight Type:
Survivors:
Yes
Schedule:
Sydney - Lord Howe
MSN:
501-0145
YOM:
1979
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft was being used for a pleasure flight for the owner and some friends. The Captain calculated the landing distances required for both runway 28 and 10, based on weather reports obtained at briefing, which indicated a strong northerly wind component. An updated report received some 30 minutes before descent confirmed the wind as 290 degrees at 7 knots. Approaching the island and becoming visual, the crew noted the windsock near the western end of the runway to be indicating a slight headwind component in the 10 direction and decided on a straight in approach to runway 10, to avoid an approaching squall/shower. The aircraft touched down firmly a short distance beyond the threshold. Speed brakes were immediately extended and wheel braking applied. About four seconds later the Captain called for the drag chute to be deployed. Although the co-pilot correctly activated the handle, it became obvious that the chute had not deployed as no increase in retardation occurred. When the Captain realised that the aircraft could not be stopped on the runway remaining he attempted to turn the aircraft towards a clear grass area to the right. However, the aircraft was aquaplaning on the wet surface and did not respond to steering inputs for some distance. The aircraft left the bitumen tracking to the right. It collided with a gable marker, passed through a fence, continued down an embankment, across a road, through a second fence and came to rest approximately 90 metres from the runway end and 70 metres to the right of the extended centreline. The left main and nose gear legs were torn off. Witnesses to the accident said that when the aircraft landed, the runway was very wet and the wind was westerly at 5 to 10 knots.
Probable cause:
It was determined that the Captain had made some miscalculations in his pre-flight assessments. He had noted the landing distance available as being the same for both runways, whereas runway 28 has a reduced length due to terrain clearance requirements on the approach. Under the conditions both forecast and prevailing, and using the criteria applicable at the time for an aircraft fitted with an alternate means of retardation, i.e. drag chute, the landing distances required for both runways were greater than the landing distances available. The Captain had also evidently applied incorrect techniques during the landing. He had not attempted to deploy the drag chute immediately the nose wheel was on the ground, and had not applied unmodulated pressure to the anti-skid braking system. These measures are required by the manufacturer to obtain maximum performance. It was found that the drag chute canister lid had been sealed with tank sealant and painted over. The latch assembly had operated but the drogue chute spring was insufficiently strong to break the seal. When the sealant was prised away from around the lid, the system operated normally. This error had not been found during a check of the aircraft immediately following repainting. The lid had the appearance of an oblong radio antenna and was not marked in any distinguishing manner. The problem should also have been noticed during a subsequent inspection of the drag chute for moisture. The inspection is required every 90 days if the drag chute has
not been deployed, and requires the removal of the lid and drogue chute in order to feel the main chute for moisture. The condition of the sealant would indicate that this had not been carried out.
The following factors were considered relevant to the development of the accident:
- Inadequate pre-flight planning and preparation by the flight crew. The runway distance required was in excess of the distance available on either runway.
- Adverse runway and weather conditions - wet surface and downwind component.
- Improper sealing of drag chute canister.
- Inadequate maintenance of the drag chute system.
- Improper operation of wheel brakes.
Final Report:

Crash of a Fletcher FU24-950 in Frogmore: 1 killed

Date & Time: Nov 29, 1989 at 1150 LT
Type of aircraft:
Operator:
Registration:
VH-HTB
Flight Phase:
Survivors:
No
Schedule:
Frogmore - Frogmore
MSN:
174
YOM:
1971
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The aircraft was engaged in superphosphate spreading operations. An aerial survey of the property had been conducted by the pilot in company with the property owner. Power poles in the valley ahead and to the left of the airstrip were marked. When operations started the wind was a light north-easterly and ambient temperature was 16° Celsius. By the time the aircraft had refuelled and was ready for the thirty-sixth flight of the day, the ambient temperature had increased to 28° Celsius and the wind direction had changed to a south-westerly. Shortly after takeoff, the aircraft was observed to sink after overflying the high-voltage power lines between the marked poles. On the next flight the aircraft was observed to make a tight left turn and fly down the valley adjacent to the left marked powerpole. On the next and final flight, the aircraft was apparently attempting to follow the track of the previous flight. While crossing the power lines south-west of the marked power pole, the aircraft's landing gear and left wing tip struck the powerlines. With the broken powerline jammed behind the left aileron washout plate, the aircraft impacted the ground 100 metres beyond the powerpole. Ground impact forces destroyed the aircraft and reduced the cockpit area to non-survivable dimensions.
Probable cause:
On-site examination of the aircraft and subsequent laboratory examination and testing of components did not reveal any pre-existing mechanical defects or abnormalities which could be considered as factors in, or contributory to, this accident. Powerline impact marks on the aircraft were consistent with the aircraft being in a left banked attitude when it struck the wire. The investigation revealed that the loader driver's truck bucket load gauge had no conversion/calibration chart, and that the aircraft was being operated in excess of the maximum allowable weight for takeoff. It is considered probable that the pilot had elected to fly down the valley, (thus taking advantage of the downslope), to compensate for a degradation of aircraft performance whilst operating overweight in the changed ambient conditions. The absence of a superphosphate trail before wire impact indicates that the pilot did not dump any of the load and was either unaware
of, or had forgotten about, the existence of powerlines to the south-west of the marked powerpole.
The following factors were considered relevant to the development of the accident:
1. The aircraft was being operated in an overweight configuration for takeoff.
2. The pilot did not adjust the takeoff weight of the aircraft to give an acceptable climb performance.
3. The pilot was unaware of, or had forgotten about, the powerlines to the south-west of the marked pole; or,
4. the pilot misjudged the clearance between the powerlines and the aircraft whilst trying to overfly them.
Final Report:

Crash of a Cessna 414A Chancellor near Wonthaggi

Date & Time: Oct 27, 1989 at 0833 LT
Type of aircraft:
Operator:
Registration:
VH-SDV
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Melbourne – Port Welshpool
MSN:
414A-0261
YOM:
1979
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The pilot reported that whilst enroute from Essendon to Wonthaggi he descended to the lowest safe altitude of 3600 feet above sea level, lowered the landing gear, reduced power and airspeed to counter the effect of turbulence and entered a holding pattern to the south south west of the Wonthaggi navigation aid. During the holding pattern the aircraft descended until it collided with trees that were 865 feet above sea level. The weather at the time included gale force winds, rain and low cloud. There were no thunderstorms or microbursts in the area, however, other aircraft reported a very low cloud base and severe turbulence. A few minutes prior to the accident ground witnesses, south south west of the accident site, reported an aircraft matching the description of VH-SDV, flying below a low, misty, ragged cloud base. There was no record of another aircraft in the area at the time. Information was available which indicated that the aircraft had descended below 3600 feet during the approach to Wonthaggi. The passengers reported that the pilot gave no indication of any problem or danger. Until the impact, they believed the aircraft was descending normally for a landing at Port Welshpool.
Probable cause:
No aircraft defects were found which may have been factors in the accident. The investigation indicates that the pilot attempted to fly under the low cloud base, in order to reach the Port Welshpool destination where weather conditions were earlier reported to have been partially sunny. Port Welshpool is not serviced by an approved navigation aid. The pilot attempted to descend below the cloud base, hoping to achieve visual flight conditions to continue to his destination.
Final Report:

Crash of a Piper PA-31-310 Navajo in Carnarvon

Date & Time: Aug 18, 1989 at 1856 LT
Type of aircraft:
Operator:
Registration:
VH-DEG
Flight Type:
Survivors:
Yes
Schedule:
Geraldton – Carnarvon
MSN:
31-7812098
YOM:
1978
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
At approximately 1809, (23 minutes before last light) during final approach to landing at Carnarvon, the pilot noticed that the landing gear had not extended correctly. The aircraft remained in the circuit area whilst the pilot attempted to lower the landing gear using both manual and emergency methods. He also sought assistance from the company's, Perth based, duty pilot and Carnarvon based engineers. After exhausting all possible methods of lowering the gear the pilot decided to land with the landing gear and flaps retracted. The pilot rejected a landing on the sealed runways because he was apprehensive that it would cause unnecessary damage to the aircraft and could result in a fire. He considered landing in a riverbed (rejected by the Senior Operational Controller), alongside one of the sealed runways (the surface was unsuitable) and on one of the dirt strips. The pilot was offered a flare path on dirt runway 27 however, he declined and indicated that he would try to land using the available light. At 1856 (last light was at 1832) the pilot attempted a landing on runway 27. On late final approach the aircraft collided with a one and a half metre high levy bank, 270 metres short and 115 metres to the right of the threshold. The pilot was trapped in the wreckage for some time after the aircraft came to a stop. While the passenger was slightly injured, the pilot was seriously wounded.
Probable cause:
The landing gear problem arose when the left main landing gear would not lower. Examination of the aircraft revealed that both hinges fitted to the inboard landing gear door had fractured. The forward hinge had fractured as a result of fatigue and the rear hinge as a result of overload. The fatigue crack initiation had occurred at a sharp edged, prominent forging flash on the inner radius of the hinge and had grown over approximately 4000 load cycles. A similar fatigue problem had been identified on an earlier version of the hinge (part number 46653-00), however, regular inspections for fatigue cracking were discontinued when hinges with part number 47529-32 (as fitted to VH-DEG) were introduced in 1980. Similar fatigue cracking was found in the forward door hinge of another PA31 during the investigation. The fractured hinges jammed the left main landing gear mechanism and neither the normal or emergency extension systems could extend the gear. The pilot was apprehensive about wheels up landings. Much of his decision making was aimed at reducing the risk of fire and minimising the damage the aircraft would sustain during the landing. eg. Selection of a dirt runway instead of the sealed strip, landing with flaps retracted etc. During the pilot's attempts to rectify the landing gear problem, and up until the time of his touchdown, he was subjected to considerable radio transmission traffic involving questions, directions and suggestions which distracted him from his primary tasks. The pilot indicated on at least two occasions that he was ready to land, however, each time advice and questions from the ground personnel involved overrode his intentions. When the pilot was asked if he wanted a flare path on runway 27 there was still some natural light available and he was intending to land. However, by the time he was able to make his final approach it was dark and he was unable to see the ground. Studies have shown that aircrew subjected to high levels of stress can suffer skill fatigue and cognitive task saturation, which in turn can lead to a breakdown in the decision making process. It was apparent from the pilot's radio transmissions and the quality of the decisions made in the latter part of the flight that his information processing and decision making abilities had been degraded by the stress of continuous radio transmissions and continuous, and sometimes conflicting, instructions. As a result, what should have been a relatively simple wheels up landing in daylight was turned into an extremely difficult wheels up landing at night. With the landing gear retracted the aircraft's taxi and landing lights were not available to the pilot.
The following factors were considered relevant to the development of the accident:
1. Manufacturing defect. A forging flash created a stress concentration which led to fatigue cracking.
2. Inadequate inspection procedures. Previous inspection procedures introduced to disclose similar cracking were withdrawn on the introduction of later part numbered hinges.
3. Apprehension of the pilot. The pilot was apprehensive about apparently significant dangers of landing an aircraft, wheels up, on a sealed runway.
4. Inordinate interference in aircraft operations by ground based advisors. The ground advisors input overrode the pilot's decision on a number of occasions with the result that a simple exercise became very complicated.
5. Cognitive task saturation and skill fatigue. The amount of information, advice and suggestions being passed via the radio communications system overloaded the pilot decision making abilities.
6. Improper in-flight decisions. As a result of task saturation the final decision made by the pilot to attempt a night landing on an unlighted strip was incorrect.
7. The pilot did not see and therefore was unable to avoid the levy bank.
Final Report:

Crash of a De Havilland DHC-2 Beaver in Lake Monduran: 3 killed

Date & Time: Dec 5, 1988 at 1200 LT
Type of aircraft:
Operator:
Registration:
VH-BSL
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Bundaberg - Bundaberg
MSN:
1618
YOM:
1966
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The aircraft reported departing Bundaberg for Monduran Dam on a no SAR flight at 1135 hrs EST with three persons on board and an endurance of 270 minutes. The purpose of the flight was to complete the endorsement of the pilot under check and to assess the suitability of an area of water on the coast to where the passenger, who was the regular pilot of the aircraft, was to fly the aircraft the following day. The pilot in command had flown 27 hours in the previous three months, of which 9 were on type. The pilot under check had flown only one hour in the last three months. This flight had been in VH-BSL. At approximately 1200 hrs, the aircraft was observed in the Lake Monduran area. It flew two left hand circuits, landing into wind towards the dam wall each time. After the second takeoff, it turned left and was seen heading north from the lake. Nothing further was heard or seen of the aircraft. Following an extensive search, the wreckage was located six days later lying inverted in 15 metres of water approximately 2 km WNW of the dam wall in the area of the junction of the main east-west channel and a northsouth channel of the lake. Both floats had separated from the aircraft and the right float was severely torn for about half its length. There was substantial water impact damage to the windshield frame/cockpit roof area and to the upper leading edge surfaces of both wings.
Probable cause:
No fault was found with the aircraft or its systems which might have contributed to the accident. It could not be determined who was manipulating the controls of the aircraft at the time of the accident. Evidence was obtained that it was the habit of the check pilot to have pilots undergoing endorsement or check to fly two circuits landing into wind and then to carry out crosswind landings. The check pilot and the pilot under check had previously operated at the dam and alighted on to both the east/west and the north/south channels. Having been observed to fly two into wind circuits and then head north and not be sighted again, it is possible that the aircraft then commenced crosswind operations onto the north/south arm of the lake, landing in a southerly direction with a crosswind from the left. Information from the Bureau of Meteorology indicated that the surface wind in the area at the time of the accident was 090` magnetic at 15 knots. This information was confirmed by witnesses at the dam wall who observed white caps on the surface of the dam. The north/south channel of the lake was bounded on its east side by steep hills rising to 70 metres above water level. The effect of this high ground was to partially blanket the north/south channel from the easterly wind. The position of the wreckage was in the area where the wind shadow effect would have ended and where the wind would have blown at full strength along the main east/west channel of the lake. The crosswind limitation for the aircraft as stated in the flight manual was 8.7 knots. Commenting in early 1988 on an enquiry regarding the raising of this limit, the aircraft manufacturer emphasised the 8.7 knot limit and advised that any test work to raise the limit should proceed cautiously starting at or below the current (8.7 knot) limit. If the aircraft was conducting crosswind operations in the north/south channel, and suddenly encountered a 15 knot crosswind on exiting the wind shadow area, the control difficulties confronting the pilot could have been significant. The aircraft wreckage was intact except for the floats which had been torn off by water impact forces. The right float was severely damaged while the left was intact. The forward tip of the right float had been severed by the propeller. The remaining forward section had then been forced upwards and outboard and had broken off. This weakened the float support structure, causing it to fail, and allowing the remaining section of the right float to strike the right side of the fuselage just aft of the cabin. Damage of this type an magnitude was most probably caused by the nose of the right float digging into the surface of the lake at relatively high speed. For this to occur, the aircraft was banked to the right at float impact - a possible consequence of encountering a strong crosswind from the left. There was no evidence that the aircraft had hit a submerged object. The factors associated with the development of this accident could not be determined.
Final Report:

Crash of a Partenavia P.68B Victor in Kolane

Date & Time: Oct 14, 1988 at 1845 LT
Type of aircraft:
Operator:
Registration:
VH-PFQ
Flight Type:
Survivors:
Yes
Schedule:
Kolane - Taroom - Kolane
MSN:
95
YOM:
1977
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The Taroom aerodrome had recently been equipped with a pilot activated lighting (PAL) system which was due to be commissioned on the evening of 15 October 1988. The pilot, who is a local Council member had flown from his property "Kolane" to Taroom late in the afternoon, to check that the PAL system was functional. He had intended to fly to Taroom the following evening to activate the lights for the official opening celebration, which was planned to be held at the aerodrome. After checking that the system was working the pilot decided to take the opportunity to practice some night circuits and landings before returning to his property. Before departing Taroom he arranged to have two vehicles positioned at his property landing area to illuminate the strip which is 850 metres long, aligned 235/055 degrees magnetic, and 1000 feet above sea level. He apparently intended to check the suitability of the strip for a night landing on his return. The aircraft was observed to fly over the strip in a north-easterly direction and then make a left turn. The aircraft was then seen to descend and the sound of impact was heard by the occupant of a vehicle near the strip. The aircraft had impacted the ground whilst in a descending left turn at a ground speed of approximately 125 knots. Initial impact was in a clearing near trees. The aircraft slid 91 metres before the left wing struck a large tree and was torn off. The aircraft slid another 45 metres before coming to rest and catching fire. The pilot was thrown from the aircraft while still strapped to his seat and was able to move himself away from the immediate vicinity of the fire before help arrived.
Probable cause:
The pilot has no recollection of events immediately prior to the accident. There is no indication that the aircraft was not functioning normally at the time of the accident. The weather was fine, there was a light northerly breeze, and there was no moonlight. Indications are that the pilot may have become disorientated whilst attempting to carry out a visual circuit when there was no visual horizon. The landing area did not meet the requirements for night operations published in the Visual Flight Guide.
The following factor was considered relevant to the development of the accident:
The pilot was attempting to carry out a night visual circuit when there was no visual horizon.
Final Report:

Crash of a Fletcher FU-24-950 near Werris Creek: 1 killed

Date & Time: Jul 19, 1988 at 1045 LT
Type of aircraft:
Operator:
Registration:
VH-HPP
Flight Phase:
Survivors:
No
Schedule:
Werris Creek - Werris Creek
MSN:
162
YOM:
1970
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The pilot was conducting superphosphate spreading operations in fine and clear weather conditions. The paddock being treated sloped uphill, and there were heavily timbered peaks beyond the paddock. The pilot had spread the paddock the previous day under similar conditions. On this occasion the aircraft was apparently performing normally as the first swath run was completed, but the aircraft did not appear to gain any appreciable height as it approached the hills. It was then seen to adopt a steep nose-up attitude and commence a wingover type manoeuvre. During this manoeuvre the aircraft struck trees and then impacted the ground. A fierce fire broke out and engulfed the wreckage. The pilot, sole on board, was killed.
Probable cause:
Although the investigation was hampered by the extensive fire damage, no defect or malfunction was discovered which might have contributed to the accident. The reason the pilot, who had extensive agricultural experience, chose to conduct swath runs towards steeply rising ground was not determined. The wind direction had changed since the previous day, and the aircraft was likely to have been affected by downdrafts on the lee side of the hills. When the pilot realised the aircraft was not performing as expected, he evidently attempted to dump the remaining load and reverse the direction. However, there was insufficient aircraft performance available to successfully complete this manoeuvre.
Significant Factors:
The following factors were considered to be relevant to the development of the accident:
1. The pilot elected to conduct spreading runs towards steeply rising ground, when safer alternatives were available.
2. It was likely that downdraft conditions existed on the lee side of the hills.
3. The pilot evidently misjudged the climb performance of the aircraft.
4. The pilot delayed attempting a reversal of direction beyond the point where such a manoeuvre could be safely accomplished.
Final Report:

Crash of a Piper PA-60 Aerostar (Ted Smith 600) near Cassilis: 2 killed

Date & Time: Dec 22, 1987 at 1620 LT
Operator:
Registration:
VH-IGV
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Bankstown – Coolah
MSN:
60-0054-123
YOM:
1971
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The pilot was conducting a freight charter flight, and witness evidence confirmed that on DEPARTURE he was occupying the left-hand seat. The pilot was accompanied by a friend who was also a commercial pilot, but not endorsed on this type of aircraft. Approximately 18 minutes prior to the estimated time of arrival at the destination, the pilot reported leaving the cruising altitude of 6500 feet on descent. Several minutes after the descent report had been made, a witness about 50 kilometres from the destination reported seeing the aircraft pull-up into a very steep climb from an extremely low height with its wings level, and then become inverted. It then entered what was described by the witness as a spin or spiral dive, before impacting the ground in a near vertical descent. The pilot was found in the right-hand seat, and the passenger had been thrown clear of the wreckage. It was established that neither seat belt had been fastened at the time of the impact. Although it could not be determined which pilot was flying the aircraft at the time of the pull-up, medical evidence suggested that the pilot occupying the right-hand seat position was handling the controls at the time of ground impact. The weather at the time of the accident was fine and clear, with 10-15 knot winds.
Probable cause:
A thorough examination of the aircraft wreckage did not reveal any malfunction or mechanical failure which may have caused a sudden and severe loss of control. Investigation showed that at the
moment of impact the aircraft was in a near vertical descent, without any rotation about the vertical axis, and the wings were in a stalled condition. No reason was found which could have explained either the low flying, or the steep pull-up. During the investigation it was established that with this aircraft type, a considerable degree of sustained elevator force would need to be applied by a pilot in order to achieve the type of flight path reported by the witness. It is considered that such a control input would need to be deliberately executed.
Significant Factors:
It was considered that the following factors were relevant to the development of the accident:
1. The pilot, or passenger, performed what was apparently a deliberate steep pull-up from low-level. The reason for the pull-up was not established.
2. Loss of control occurred as a consequence of the aircraft becoming stalled.
3. There was insufficient height for the pilot to effect recovery following the loss of control.
Final Report: