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Crash of a Cessna 208B Super Cargomaster in Lubbock

Date & Time: Jan 18, 1995 at 0903 LT
Type of aircraft:
Operator:
Registration:
N9461R
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Lubbock - Midland
MSN:
208B-0076
YOM:
1988
Flight number:
MRA817
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2542
Captain / Total hours on type:
514.00
Aircraft flight hours:
3984
Circumstances:
During the night before the accident, freezing rain followed later by snow, fell on the ramp where the airplane was parked. A witness reported that while assisting the pilot in removing snow from the airplane, he noted that 80% of the wing was covered with a coarse layer of ice, from 1/16 to 3/16 in thickness, that was not removed before flight. After the accident, a fireman from the city of lubbock fire department noted ice on the wing approximately 1/16th of an inch thick that had a rough texture that looked as if deposited by freezing rain. The pilot reported that shortly after take off she heard a power decrease and felt surges in the aircraft. The pilot then looked for a place to land. A detailed examination of the engine revealed no mechanical deficiencies.
Probable cause:
The pilot's failure to remove ice from the airframe prior to takeoff. Factors were freezing rain the night before and the pilots' incomplete preflight inspection.
Final Report:

Crash of a Cessna 208 Caravan I in Bulverde

Date & Time: Sep 4, 1987 at 2245 LT
Type of aircraft:
Operator:
Registration:
N807LA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
San Antonio – Dallas
MSN:
208-0026
YOM:
1985
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3100
Captain / Total hours on type:
750.00
Aircraft flight hours:
222
Circumstances:
After leveling at 5,500 feet, the standby power annunciator light illuminated, followed by loss of oil pressure. The pilot turned back toward the airport, but there was a progressive loss of engine power and the prop went to a feathered position. During an emergency landing at night, the aircraft hit a power line and trees, then crashed. During an engine teardown, disassembly of the reduction gearbox scavenge pump revealed that a retaining nut and tang washer (w/i the scavenge pump) had backed off and lodged between the spur gears, which resulted in a sheared scavenge pump drive shaft. In turn, this resulted in the loss of oil pressure and allowed the prop to feather.
Probable cause:
Occurrence #1: airframe/component/system failure/malfunction
Phase of operation: cruise - normal
Findings
1. (c) lubricating system, oil scavenge pump - loose
2. (c) lubricating system, oil scavenge pump - jammed
3. (c) lubricating system, oil scavenge pump - failure, total
4. Initiated
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Occurrence #2: loss of engine power (total) - mech failure/malf
Phase of operation: cruise
Findings
5. (c) fluid, oil - starvation
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Occurrence #3: forced landing
Phase of operation: descent - emergency
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Occurrence #4: in flight collision with object
Phase of operation: landing
Findings
6. (f) light condition - night
7. (f) object - wire, transmission
8. (f) object - tree(s)
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Occurrence #5: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Mitsubishi MU-2B-35 Marquise in Austin: 1 killed

Date & Time: Jun 2, 1986 at 2142 LT
Type of aircraft:
Operator:
Registration:
N8CC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Austin - Dallas
MSN:
569
YOM:
1972
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
5268
Captain / Total hours on type:
152.00
Aircraft flight hours:
3293
Circumstances:
About 6 minutes after takeoff, at 2138:31 cdt, the pilot reported level at 9,000 feet msl. At 2140:17, he transmitted that he had trouble and said he could not control or disconnect the autopilot (a/p) which was causing the aircraft to descend. At 2141:14, he stated he was descending at 6,000 feet/min. Another company pilot in another aircraft asked if he could find the breaker, meaning the a/p circuit breaker. At 2141:27, the pilot of N8CC replied, 'call you back.' Seconds later, radio and radar contact with N8CC were lost. A search was initiated, but the aircraft was not found until the following morning. An exam revealed the aircraft impacted in a steep, nose down, inverted attitude while at high speed; much of the wreckage was buried. No preimpact part failure/malfunction was found. With the a/p engaged, back pressure on the control column would have caused the a/p to trim nose down. Subsequently, the manufacturer issued a precautionary advisory to all MU-2 owner/operators regarding proper operation of the a/p and the various ways in which it can be disengaged. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: cruise - normal
Findings
1. (f) light condition - dark night
2. (f) autopilot/flight director - undetermined
3. (c) emergency procedure - inadequate - pilot in command
4. (f) lack of familiarity with aircraft - pilot in command
5. Descent - uncontrolled
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Occurrence #2: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report: