Crash of a Boeing B-52H-155-BW Stratofortress off Guam Island: 6 killed

Date & Time: Jul 21, 2008 at 0945 LT
Type of aircraft:
Operator:
Registration:
60-0053
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Andersen AFB - Andersen AFB
MSN:
464418
YOM:
1960
Flight number:
Raider 21
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
The aircraft departed Andersen AFB on a flight around the Guam Island under call sign 'Raider 21' with 6 crew members on board, taking part to the Guam Liberation Day celebrations. About 15 minutes into the flight, while descending from 14,000 to 1,000 feet, the aircraft became uncontrollable and crashed in the sea about 50 km north of Guam Island. The aircraft disintegrated on impact and only few debris were found. All six crew members were killed.
Crew:
Maj Chris Cooper, pilot,
Cpt Michael Dodson, copilot,
1st Lt Robert Gerren, electronic warfare officer,
1st Lt Joshua Shepherd, navigator,
Maj Brent Williams, radar navigator,
Col George Martin, flight surgeon.
Probable cause:
Malfunctioning parts and late recognition of spiraling problems likely led to the fatal crash of a B-52H Stratofortress in July, an Air Force accident investigation board concluded in a report issued Feb. 13. The problem parts, investigators decided, were the bomber’s rear stabilizers — the large horizontal fins at the jet’s tail that help angle the B-52H up or down. Although the inquiry could not determine what led to the stabilizer problem, the board said it believed the stabilizers malfunctioned while the bomber was in a fast descent from 14,000 feet to 1,000 feet. “Even an experienced aircrew could have found it difficult to recognize, assess and recover from the very rapidly developing situation involving the rear stabilizer trim,” board president Brig. Gen. Mark Barrett concluded. The bomber did not carry a flight data recorder, so the investigation team pieced together events leading up to the crash from air traffic control radar information and from parts recovered from the ocean floor by remote-controlled Navy submarines. One recovered part was a component called a jackscrew that helps control the stabilizers. The jackscrew revealed the stabilizer trim was set at 4.5 to 5 degrees nose down, but parts that could have helped determine why the stabilizers were pointed down were not recovered. Based on flight simulations, the investigative team determined the flight was normal until the jet turned left and began to descend about 33 miles west of Guam. As the 48-year-old bomber dove toward the Pacific at a speed of more than 240 mph, the stabilizers suddenly unhinged, putting the jet into a dive with the nose pointed down 30 degrees and more. One of the pilots likely tried to level the stabilizers manually using a control wheel in the cockpit that moves the stabilizer 1 degree every two to three seconds, the report said. However, because the plane was already low, there wasn’t enough time to level the stabilizers. At least three crew members tried to bail out seconds before the plane hit the water, but the plane’s speed, altitude and angle already were past the point where they could survive the ejection.

Crash of a Douglas R4D-5 off Guam Island: 2 killed

Date & Time: Aug 14, 1978 at 1141 LT
Operator:
Registration:
17152
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Agana - Ulithi Atoll
MSN:
12342
YOM:
1942
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
25
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4500
Captain / Total hours on type:
50.00
Circumstances:
The airplane departed Agana at 0949LT to Ulithi Atoll with a crew of five and 25 passengers, among them officers and musicians with their instruments. About 10 minutes after takeoff, while cruising to the southwest at an altitude of 6,000 feet and a speed of 180 knots, the crew reported an oil leak on the right engine but the situation seemed to be under control. About an hour later, at 1046LT, oil pressure fluctuated and the captain decided to return to Andersen Airbase. About 15 minutes later, the right engine was shut down and its propeller was feathered. Unable to maintain a safe altitude, the crew asked the passengers to jettison the cargo but the airplane continued to lost height. Eventually, the captain decided to ditch the airplane about 13 km southwest of the Guam Island coast. The aircraft landed at 1141LT and came to rest on water. The occupants evacuated the cabin and took refuge in dinghies, the airplane sank about 10 minutes later. 28 people, most of them injured, were evacuated about an hour later. Unfortunately, one passenger and the flight engineer drowned.
Source: Seth P. Washburne
Report: http://thirsty13th.com/Images/Guam_Airplane_Crash_1978.pdf
Probable cause:
The starboard engine developed an oil leak or other malfunction, from an undetermined source, of such severity that it caused cockpit indications of low oil pressure, illuminated the oil pressure warning light, and ultimately resulted in a propeller overspeed.
Final Report: