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Qeqqata Kommunia

Crash of a Piaggio P.180 Avanti near Kangerlussuaq

Date & Time: Oct 16, 2009 at 1140 LT
Type of aircraft:
Operator:
Registration:
N108GF
Flight Type:
Survivors:
Yes
Schedule:
Kuwait – Antalya – Vienna – Stornoway – Keflavik – Narsarsuaq – Goose Bay – Bangor – Denton
MSN:
1086
YOM:
2004
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total hours on type:
105.00
Aircraft flight hours:
1035
Aircraft flight cycles:
716
Circumstances:
The accident flight was a part of a ferry flight from Kuwait to USA. The flight departed from Keflavik, Iceland with planned destination Narsarsuaq, Greenland. The commander did not get visual contact with the runway on the instrument approach to Narsarsuaq and the flight diverted towards Kangerlussuaq, Greenland. During the flight towards Kangerlussuaq, the amount of fuel became critical low and the aircraft landed on the Greenlandic icecap. The aircraft was destroyed during the landing attempt. The commander suffered minor injuries. The accident occurred in daylight and under visual meteorological conditions (VMC).
Probable cause:
After the flight was airborne from BIKF, the flight was restricted by ATC to cruise at FL200 instead of FL280. The lower flight altitude and the power setting used resulted in a reduction of the final reserve to approximately zero minutes. At that time the commander was not concerned about the final reserve because the flight to BGBW was only a two hours flight and as the aircraft before take-off from BIKF had fuel for more than three hours and 40 minutes of flight. During the approach to BGBW the flight never came below the clouds and was in IMC during the entire final approach. The most likely cause was that the aircraft was not following the NDB DME 07 approach procedure descent profile. Consequently the commander did not get visual contact during the approach and he had to make a missed approach. During the diversion to the alternate aerodrome, BGSF the flight was altitude restricted by ATC to FL190. One engine was intentionally stopped during the diversion to BGSF. The consequence was a reduction of the aircraft range. A shallow descent was initiated approximately 57 minutes before ETA over BGSF. The shallow descent profile did consume more fuel than a steeper descent profile. The commander decided to make a precautionary landing in the terrain. The aircraft was destroyed during the landing attempt on the rugged and bumpy surface of the icecap.
Final Report:

Crash of a Lockheed C-141A-LM Starlifter in Søndre Strømfjord: 23 killed

Date & Time: Aug 28, 1976 at 1145 LT
Type of aircraft:
Operator:
Registration:
67-0008
Flight Type:
Survivors:
Yes
Schedule:
Thule - Söndreströmfjord
MSN:
300-6257
YOM:
1967
Country:
Region:
Crew on board:
8
Crew fatalities:
Pax on board:
19
Pax fatalities:
Other fatalities:
Total fatalities:
23
Aircraft flight hours:
15228
Circumstances:
The aircraft departed Thule Air Base on Greenland for a two-hour flight to Sonderstromfjord Air Base. From Sonderstromfjord it was to return to Thule and continue back home to McGuire AFB. The flight carried enough fuel for the flight to McGuire. Following a PAR approach the airplane landed slightly long on the 9235 feet long runway 11. The aircraft rolled for 1,500 to 2,000 feet with no thrust reverse or spoiler deployment. A go around was commenced. The plane then rotated abruptly and lifted off the runway with a pitch attitude as high as 45°. The aircraft stalled. The left wing struck the ground and burst into flames. The aircraft became airborne again with portions of the left wing missing. It flew for 650 feet before striking the ground with the right wing, causing it to catch fire. It then bounced once more and disintegrated 500 feet from runway centerline.
Source: C-141 Lifetime Mishap Summary / Lt. Col. Paul M. Hansen
Probable cause:
Investigation revealed that the crew were very inexperienced (a captain with less than 100 hours in command). The were probably affected by an optical illusion. The first 3,000 feet of runway 11 has an upslope of 1.51%; it rises 59 feet from the threshold. At touchdown, the last two-thirds of the runway disappears, giving the impression of a very short runway.

Crash of a De Havilland DHC-3 Otter near Søndre Strømfjord: 1 killed

Date & Time: Aug 29, 1961 at 1523 LT
Type of aircraft:
Operator:
Registration:
CF-MEX
Flight Phase:
Survivors:
Yes
Schedule:
Søndre Strømfjord – Egedesminde
MSN:
332
YOM:
1960
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4000
Captain / Total hours on type:
1500.00
Aircraft flight hours:
750
Circumstances:
Few minutes after takeoff from Søndre Strømfjord Airport, en route for Egedesminde (Aasiaat), the aircraft caught fire. The crew reduced his altitude and attempted an emergency landing when the airplane crashed. A crew member was killed while five other occupants were injured, some of them seriously. The aircraft was destroyed.
Probable cause:
An in-flight fire, initiated and sustained by a severe fuel leak. The fuel leak was caused by the locking of a carburetor drain plug to unscrew.
Final Report: