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Crash of a Fokker 50 in Tawau: 34 killed

Date & Time: Sep 15, 1995 at 1222 LT
Type of aircraft:
Operator:
Registration:
9M-MGH
Survivors:
Yes
Schedule:
Kota Kinabalu - Tawau
MSN:
20174
YOM:
1990
Flight number:
MH2133
Location:
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
49
Pax fatalities:
Other fatalities:
Total fatalities:
34
Captain / Total flying hours:
4892
Captain / Total hours on type:
427.00
Copilot / Total flying hours:
1162
Copilot / Total hours on type:
962
Aircraft flight hours:
10848
Aircraft flight cycles:
17483
Circumstances:
Flight MH2133 A Fokker 27 mark 050 bearing registration 9M-MGH was a scheduled domestic flight from Kota Kinabalu to Tawau, Sabah. The departure from Kota Kinabalu was delayed by approximately 30 minutes due to late arrival of the aircraft operated by a different set of flight crew from Labuan. The flight took off from Kota Kinabalu at 0419 hrs on an Instrument Flight Rules (IFR) flight plan via Airway W 423 direct to Tawau Very Omni Range (VOR) at flight level (FL) 170 with 53 persons on board. The departure out of Kota Kinabalu was uneventful and the weather en-route was insignificant. At 0442 hrs the flight established radio contact with Tawau Tower “MH 2133 we are maintaining FL 170, TMA 40, VTW 0505, presently at 94 DME VTW”. The controller then passed the weather for Tawau which was, “surface wind calm, visibility more than 10 km, rain north to north east, scattered 1600 feet and scattered 2700 feet, broken at 14000 feet, Temperature 30 degree C and QNH 1009 mb, Runway 17”. At 0443 hrs another aircraft call sign TSE 809 (a Cessna 206) flying along the same route as MH2133 but at 9500ft established radio contact with Tawau Tower, TSE 809 then reported that the flight was 65 DME from Tawau VOR. This was immediately followed by Tawau Tower asking MH2133 to report position from Tawau VOR which MH 2133 replied “57 DME and requested descent”. The controller then cleared MH 2133 to descend to 10500 feet. At this point in time there was also another aircraft MH2135 (a Boeing 737) heading towards Tawau cruising at FL 230 and cleared by the TOWER to descent to FL 180. MH 2135 was also notified by the TOWER of the Expected Approach Time (EAT) of 0530 hrs. At 0457 hrs TSE 809 reported that the flight was 44 DME from Tawau VOR. On hearing this transmission, MH 2133 requested a lower descend clearance, as it was 30 DME from Tawau VOR. It must be noted that at this juncture, MH 2133 was ahead of TSE 809 but at a higher altitude. The controller then asked TSE 809 whether there was any objection for MH2133 to descent through its level and become number One (1). Despite the fact that TSE 809 had no objection for MH 2133 to become number One (1), MH 2133 was asked by the controller to still maintain 10500 feet. At 0458:23 hrs, MH 2133 asked “MH 2133 confirm maintain 10500 feet?”. TOWER then replied “Affirm maintain 10500 number 2 in traffic”. At 0458:36 hrs MH 2133 again asked “MH 2133, 26 DME confirm we are still number 2?” TOWER then replied- “Station calling…. say again - MH 2133 then repeated “2133 Maam, and are 25 DME maintain 10500, confirm we are number 2?”. TOWER – responded “That’s affirm 2133, Expected Approach Time 0520 hrs”. At 0459:05 hrs MH2133 asked TSE 809 to check position and whether there would be any objection for the aircraft to descend through its level. TSE 809 replied that they had no objection and MH 2133 was subsequently cleared to descend to 7000 feet. The descent into Tawau by MH 2133 from the cruising altitude of 10500 feet was initiated at about 21 DME. The flight crew discussed the descent technique they were going to use and were aware of all their action. At 0501:15 hrs, as the flight reported leaving 9000 feet and passing 16 DME, the flight crew advised the controller that they had the airfield visual. MH2133 was then cleared for visual approach runway 17. At 0502:48 hrs, MH 2133 reported passing 3500 feet. The aircraft was then configured for landing where landing gears were selected down and flaps set at 25 degrees. The aircraft speed was still fast and since it was also high on the approach, the commander assured the co-pilot “Runway is long so no problem Eh”. On passing 2000 feet and on short final, the copilot reminded the commander “speed, speed check, speed check Ah”. The rate of descent was in excess of 3000 feet per minute and its pitch angle was around minus 13 degrees. The excessive rate of descent triggered the aircraft Ground Proximity Warning System (GPWS) sink rate and pull up warnings. The commander ignored these warnings and insisted that he should continue with approach for a landing. The aircraft first touched down on the runway at 0505 hrs. Its first tyre marks (nose wheel) on the runway was at approximately 3400 ft from the threshold. It then bounced and at 4500 ft point, its left main wheel made a light contact with the runway surface. It subsequently bounced up again and its main wheels made a firm contact at 4800 ft point, thus leaving only 800 ft of runway remaining. The aircraft continued onto the grass verge, momentarily left the ground and hopped over the runway perimeter fence. It subsequently crashed at 571 feet from the end of the runway at almost right angle to the runway. There were a number of explosions followed by a fire. The aircraft was totally destroyed.
Probable cause:
The most probable cause of the accident was due to the commander’s insistence to continue with an approach despite the fact that the runway available after touchdown was not sufficient enough for the aircraft to stop. The perception regarding economic consideration which put pressure on him to save fuel and adhere to schedules was a contributing factor.
Final Report:

Crash of an Airbus A300B2-120 in Kuala Lumpur

Date & Time: Dec 18, 1983 at 1938 LT
Type of aircraft:
Operator:
Registration:
OY-KAA
Survivors:
Yes
Schedule:
Kuching - Singapore - Kuala Lumpur
MSN:
122
YOM:
1980
Flight number:
MH684
Country:
Region:
Crew on board:
14
Crew fatalities:
Pax on board:
233
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
3907
Circumstances:
Following an uneventful flight from Singapore-Changi Airport, the crew started the approach to Kuala Lumpung-Subang Airport by night and poor weather conditions with heavy rain falls. During an ILS approach to runway 15 with an RVR of 450 meters, the pilot-in-command was unable to establish a visual contact with the runway and eventually decided to make a go-around. Four other attempts to land failed and during the sixth approach procedure, the crew descended below the MDA until the aircraft contacted trees and crashed in a dense wooded area located 1,200 meters short of runway, bursting into flames. All 247 occupants were quickly evacuated, 20 of them were injured. The undercarriage and both engines were torn off while the aircraft was partially destroyed by a post crash fire.
Probable cause:
The flight crew's decision to continue the approach after passing the MDA below the glide without proper visual contact with the ground/runway. Published procedures violation, lack of visibility, poor weather conditions were considered as contributing factors.

Crash of a Britten-Norman BN-2A-8 Islander in Lawas

Date & Time: Jul 6, 1982
Type of aircraft:
Operator:
Registration:
9M-MDD
Survivors:
Yes
Schedule:
Long Semado – Lawas
MSN:
684
YOM:
1973
Location:
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed upon landing at Lawas Airport. There were no casualties.

Crash of a Boeing 737-2H6 near Jalan Tanjung Kupang: 100 killed

Date & Time: Dec 4, 1977 at 2036 LT
Type of aircraft:
Operator:
Registration:
9M-MBD
Flight Phase:
Survivors:
No
Schedule:
Penang - Kuala Lumpur
MSN:
20585/306
YOM:
1972
Flight number:
MH653
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
93
Pax fatalities:
Other fatalities:
Total fatalities:
100
Circumstances:
The airplane departed Penang Airport at 1921LT on scheduled service MH653 to Kuala Lumpur. During the descent, while at an altitude of 4,000 feet, a hijacker entered the cockpit and forced the crew to divert to Singapore. The aircraft then climbed to FL210 and proceeded to Singapore when the hijacker shot both pilots and then himself. Few minutes later, the airplane entered a dive and crashed in a wooded area located in the region of Jalan Tanjung Kupang. The aircraft was totally destroyed and all 100 occupants were killed. The cockpit voice recordings indicate noises suggestive of the cockpit door being broken in, along with a reasonable amount of screaming and cursing. No noises are heard from within the cockpit to indicate any of the three occupants were conscious. The autopilot was then disconnected, possibly due to a pitch input by someone entering the cockpit and trying to control the aircraft. An investigator speculated that someone pulled back on the column, causing a pitch up, followed by an oscillation. This rapidly developed into a high amplitude phugoid oscillation that resulted in a rapid dive.
Probable cause:
The aircraft was hijacked in-flight and both pilots were shot.