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Crash of a Cessna 207 Stationair 8 in Bethel

Date & Time: Nov 20, 2021 at 1755 LT
Operator:
Registration:
N9794M
Survivors:
Yes
Schedule:
Bethel – Kwethluk
MSN:
207-0730
YOM:
1981
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1480
Captain / Total hours on type:
659.00
Aircraft flight hours:
15727
Circumstances:
The pilot was conducting a scheduled air taxi flight with five passengers onboard. Shortly after departure, the pilot began to smell an electrical burn odor, and he elected to return to the airport. About 1 minute later, the electrical burn smell intensified, which was followed by visible smoke in the cockpit, and the pilot declared an emergency to the tower. After landing and all the passengers had safely departed the airplane, heavy smoke filled the cockpit and passenger compartment, and the pilot saw a candle-like flame just behind the pilot and co-pilot seats, just beneath the floorboards of the airplane. Moments later, the airplane was engulfed in flames. Postaccident examination of the airframe revealed the origin of the fire to be centered behind the pilot’s row of seats, where a wire harness was found improperly installed on top of the aft fuel line from the left tank. Examination of the wire harness found a range of thermal and electrical damage consistent with chafing from the fuel line. It is likely that the installation of the wire harness permitted contact with the fuel line, which resulted in chafing, arcing, and the subsequent fire.
Probable cause:
The improper installation of an avionics wire harness over a fuel line, which resulted in chafing of the wire harness, arcing, and a subsequent fire.
Final Report:

Crash of a Cessna 208B Grand Caravan near Kwethluk: 2 killed

Date & Time: Apr 8, 2014 at 1557 LT
Type of aircraft:
Operator:
Registration:
N126AR
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Bethel - Bethel
MSN:
208B-1004
YOM:
2002
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
593
Captain / Total hours on type:
1.00
Copilot / Total flying hours:
14417
Copilot / Total hours on type:
5895
Aircraft flight hours:
11206
Circumstances:
The check airman was conducting the first company training flight for the newly hired second-in-command (SIC). Automatic Dependent Surveillance-Broadcast (ADS-B) data showed that, after departure, the airplane began a series of training maneuvers, consistent with normal operations. About 21 minutes into the flight, when the airplane was about 3,400 ft mean sea level, it began a steep descent and subsequently impacted terrain. An airplane performance study showed that the airplane reached a nose-down pitch of about -40 degrees and that the descent rate reached about 16,000 ft per minute. Numerous previous training flights conducted by the check airman were reviewed using archived ADS-B data and interviews with other pilots. The review revealed that the initial upset occurred during a point in the training when the check airman typically simulated an in-flight emergency and descent. Postaccident examination for the airframe and control surfaces showed that the airplane was configured for cruise flight at the time of the initial upset. Examination of the primary and secondary flight control cables indicated that the cables were all intact at the time of impact. Trim actuator measurements showed an abnormal trailing-edge-up, nose-down configuration on both trim tabs. The two elevator trim actuator measurements were inconsistent with each other, indicating that one of the actuators was likely moved during the wreckage recovery. Based on the supporting data, it is likely that one of the actuators indicated the correct trim tab position at the time of impact. Simulated airplane performance calculations showed that, during a pitch trim excursion, the control forces required to counter an anomaly increases to unmanageable levels unless the appropriate remedial procedures are quickly applied. Given the simulated airplane performance calculations, the trim actuator measurements, and the check airman's known training routine, it is likely that the check airman simulated a pitch trim excursion and that the SIC, who lacked experience in the airplane type, did not appropriately respond to the excursion. The check airman did not take remedial action and initiate the recovery procedure in time to prevent the control forces from becoming unmanageable and to ensure that recovery from the associated dive was possible.
Probable cause:
The check airman's delayed remedial action and initiation of a recovery procedure after a simulated pitch trim excursion, which resulted in a loss of airplane control.
Final Report: