Crash of a Swearingen SA227AC Metro III in Camilla: 1 killed

Date & Time: Dec 5, 2016 at 2222 LT
Type of aircraft:
Operator:
Registration:
N765FA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Panama City – Albany
MSN:
AC-765
YOM:
1990
Flight number:
LYM308
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
8451
Captain / Total hours on type:
4670.00
Aircraft flight hours:
24233
Circumstances:
The airline transport pilot delayed his scheduled departure for the night cargo flight due to thunderstorms along the route. Before departing, the pilot explained to the flight follower assigned to the flight that if he could not get though the thunderstorms along the planned route, he would divert to the alternate airport. While en route, the pilot was advised by the air traffic controller in contact with the flight of a "ragged line of moderate, heavy, and extreme" precipitation along his planned route. The controller also stated that he did not see any breaks in the weather. The controller cleared the pilot to descend at his discretion from 7,000 ft mean sea level (msl) to 3,000 ft msl, and subsequently, the controller suggested a diversion to the northeast for about 70 nautical miles that would avoid the most severe weather. The pilot responded that he had enough fuel for such a diversion but concluded that he would "see what the radar is painting" after descending to 3,000 ft msl. About 1 minute 30 seconds later, as the airplane was descending through 7,000 ft msl, the controller stated, "I just lost you on radar, I don't show a transponder, it might have to do with the weather." About 40 seconds later, the pilot advised the controller that he intended to deviate to the right of course, and the controller told the pilot that he could turn left and right as needed. Shortly thereafter, the pilot stated that he was going to turn around and proceed to his alternate airport. The controller cleared the pilot direct to his alternate and instructed him to maintain 3,000 ft msl. The pilot acknowledged the instruction, and the controller then stated, "do you want to climb back up? I can offer you any altitude." The pilot responded that he would try to climb back to 3,000 ft msl. The controller then recommended a heading of 180° to "get you clear of the weather quicker," and the pilot responded, "alright 180." There were no further communications from the pilot. Shortly thereafter, radar data showed the airplane enter a right turn that continued through about 540°. During the turn its airspeed varied between 198 and 130 knots, while its estimated bank angles were between 40 and 50°. Examination of the wreckage indicated that airplane experienced an in-flight breakup at relatively low altitude, consistent with radar data that showed the airplane's last recorded altitudes to be around 3,500 ft msl. The symmetrical nature of the breakup, damage to the outboard wings, and damage to the upper fuselage were all signatures indicative that the left and right wings failed in positive overload almost simultaneously. All of the fracture surfaces examined had a dull, grainy appearance consistent with overstress separation. There was no evidence of pre-existing cracking noted at any of the separation points, nor was there evidence of any mechanical anomalies that would have prevented normal operation. Review of base reflectivity weather radar data showed that, while the pilot was maneuvering to divert to the alternate airport, the airplane was operating in an area of light precipitation that rapidly intensified to heavy precipitation, as shown by radar scans completed shortly after the accident. During this time, the flight was likely operating in clouds along the leading edge of the convective line, where the pilot most likely would have encountered updrafts and severe or greater turbulence. The low visibility conditions that existed during the flight, which was conducted at night and in instrument meteorological conditions, coupled with the turbulence the flight likely encountered, were conducive to the development of spatial disorientation. Additionally, the airplane's maneuvering during the final moments of the flight was consistent with a loss of control due to spatial disorientation. The pilot's continued flight into known convective weather conditions and his delayed decision to divert the flight directly contributed to the accident. Although the operator had a system safety-based program, the responsibility for the safe outcome of the flight was left solely to the pilot. Written company policy required completion of a flight risk assessment tool (FRAT) before each flight by the assigned flight follower; however, a FRAT was not completed for the accident flight. The flight followers responsible for completing the FRATs were not trained to complete them for night cargo flights, and the operator's management was not aware that the FRATs were not being completed for night cargo flights. Further, if a FRAT had been completed for the accident flight, the resultant score would have allowed the flight to commence into known hazardous weather conditions without any further review. If greater oversight had been provided by the operator, it is possible that the flight may have been cancelled or re-routed due to the severity of the convective weather conditions present along the planned route of flight.
Probable cause:
The pilot's decision to initiate and continue the flight into known adverse weather conditions, which resulted spatial disorientation, a loss of airplane control, and a subsequent in-flight breakup.
Final Report:

Crash of a Piper PA-61P Aerostar (Ted Smith 601) near Carrollton

Date & Time: Oct 20, 2016 at 1110 LT
Operator:
Registration:
N601UK
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Hampton – Carrollton
MSN:
61-0183-012
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1338
Captain / Total hours on type:
36.00
Aircraft flight hours:
2236
Circumstances:
The pilot reported that the purpose of the flight was to reposition the airplane to another airport for refuel. During preflight, he reported that the airplane's two fuel gauges read "low," but the supplemental electronic fuel totalizer displayed 55 total gallons. He further reported that it is not feasible to visual check the fuel quantity, because the fueling ports are located near the wingtips and the fuel quantity cannot be measured with any "external measuring device." According to the pilot, his planned flight was 20 minutes and the fuel quantity, as indicated by the fuel totalizer, was sufficient. The pilot reported that about 12 nautical miles from the destination airport, both engines began to "surge" and subsequently lost power. During the forced landing, the pilot deviated to land in grass between a highway, the airplane touched down hard, and the landing gear collapsed. The fuselage and both wings sustained substantial damage. The pilot reported no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation. The pilot reported in the National Transportation Safety Board Pilot/ Operator Aircraft Accident Report that there was a "disparity" between the actual fuel quantity and the fuel quantity set in the electronic fuel totalizer. He further reported that a few days before the accident, he set the total fuel totalizer quantity to full after refueling, but in hindsight, he did not believe the fuel tanks were actually full because the wings may not have been level during the fueling. The "Preflight" chapter within the operating manual for the fuel totalizer in part states: "Digiflo-L is a fuel flow measuring system and NOT a quantity-sensing device. A visual inspection and positive determination of the usable fuel in the fuel tanks is a necessity. Therefore, it is imperative that the determined available usable fuel be manually entered into the system."
Probable cause:
The pilot's failure to verify the usable fuel in the fuel tanks, which resulted in an inaccurate fuel totalizer setting during preflight, fuel exhaustion, and a total loss of engine power.
Final Report:

Crash of a Beechcraft Beechjet 400A in Rome

Date & Time: Mar 14, 2016 at 1508 LT
Type of aircraft:
Operator:
Registration:
N465FL
Flight Type:
Survivors:
Yes
Schedule:
Jackson - Rome
MSN:
RK-426
YOM:
2005
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10393
Captain / Total hours on type:
6174.00
Copilot / Total flying hours:
6036
Copilot / Total hours on type:
407
Aircraft flight hours:
7061
Circumstances:
The pilots of the business jet were conducting a cross-country positioning flight. According to the pilot flying (PF), the flight was uneventful until the landing. While completing the descent checklist and while passing through 18,000 ft mean sea level (msl), the pilot monitoring (PM), received the automated weather report from the destination airport and briefed the PF that the wind was variable at 6 knots, gusting to 17 knots. The PF then programmed the flight management system for a visual approach to runway 7 and briefed the reference speed (Vref) as 107 knots and the go-around speed as 129 knots based on an airplane weight. The PF further reported that he knew the runway was over 4,400 ft long (the runway was 4,495 ft long) and he thought that the airplane needed about 2,900 ft of runway to safely land. During the left descending turn to the base leg of the traffic pattern, the PF overshot the final approach and had to turn back toward the runway centerline as the airplane was being “pushed by the winds.” About 500 ft above ground level (agl), both pilots acknowledged that the approach was “stabilized” while the airspeed was fluctuating between 112 and 115 knots. About 200 ft agl, both pilots noticed that the airplane was beginning to descend and that the airspeed was starting to decrease. The PF added power to maintain the descent rate and airspeed. The PF stated that, after adding power and during the last 200 ft of the approach, the wind was “gusty,” that a left crosswind existed, that the ground speed seemed “very fast,” and that excessive power was required to maintain airspeed. When the airplane was between about 75 and 100 ft agl, the PF asked the PM for the wind information, and the PM responded that the wind was variable at 6 knots, gusting to 17 knots. Both pilots noted that the ground speed was “very fast” but decided to continue the approach. Neither pilot reported seeing the windsock located off the right side of the runway. Review of weather data recorded by the airport’s automated weather observation system revealed that about 3 minutes before the landing, the wind was from 240° at 16 knots, gusting to 26 knots, which would have resulted in a 3- to 5-knot crosswind and 16- to 26-knot tailwind. Assuming these conditions, the airplane’s landing distance would have been about 4,175 ft per the unfactored landing distance performance chart. Tire skid marks were found beginning about 1,000 feet from the approach end of runway 7. The PF stated that the airplane touched down “abruptly at Vref+5 and he applied the brakes while the PM applied the speed brakes. Neither pilot felt the airplane decelerating, so the PF applied harder pressure to the brakes with no effect and subsequently applied full braking pressure. When it was evident that the airplane was going to depart the end of the runway, the PM applied the emergency brakes, at which point he felt some deceleration; however, the airplane overran the end of the runway and travelled through grass and mud for about 370 feet before stopping. Examination of the airplane revealed that the nose landing gear (NLG) had collapsed, which resulted in the forward fuselage striking the ground and the airframe sustaining substantial damage. Although the pilots reported that they never felt the braking nor antiskid systems working and that they believed that they should have been able to stop the airplane before it departed the runway, postaccident testing of the brake and antiskid systems revealed no evidence of preaccident mechanical malfunctions or failures that would have precluded normal operation, and they functioned as designed. Given the tire skid marks observed on the runway following the accident, as well as the postaccident component examination and testing results, the brakes and antiskid system likely operated nominally during the landing. Based on the available evidence, the pilots failed to recognize performance cues and use available sources of wind information that would have indicated that they were landing in significant tailwind conditions and conduct a go-around. Landing under these conditions significantly increased the amount of runway needed to stop the airplane and resulted in the subsequent runway overrun and the collapse of the NLG.
Probable cause:
The pilots’ failure to use available sources of wind information before landing and recognize cues indicating the presence of the tailwind and conduct a go-around, which resulted in their landing with a significant tailwind and a subsequent runway overrun.
Final Report:

Ground accident of a Pilatus PC-12/47E in Savannah

Date & Time: Jan 6, 2016 at 0835 LT
Type of aircraft:
Operator:
Registration:
N978AF
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Savannah - Lexington
MSN:
1078
YOM:
2008
Flight number:
Cobalt Air 727
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
23141
Captain / Total hours on type:
534.00
Copilot / Total flying hours:
7900
Copilot / Total hours on type:
5100
Aircraft flight hours:
4209
Circumstances:
The aircraft collided with a ditch during a precautionary landing after takeoff from Savannah/Hilton Head International Airport (SAV), Savannah, Georgia. The pilot and copilot sustained minor injuries, and the airplane was substantially damaged. The airplane was registered to Upper Deck Holdings, Inc. and was being operated by PlaneSense, Inc,. as a Title 14 Code of Federal Regulations Part 91 positioning flight. Visual meteorological conditions prevailed, and an instrument flight rules flight plan was filed for the flight to Blue Grass Airport (LEX), Lexington, Kentucky. The pilot in the left seat was the pilot monitoring and the copilot in the right seat was the pilot flying. The crew had the full length of the runway 1 available (7,002 ft) for takeoff. The pilots reported that the acceleration and takeoff was normal and after establishing a positive rate of climb, the crew received an auditory annunciation and a red crew alerting system (CAS) torque warning. The engine torque indicated 5.3 pounds per square inch (psi); the nominal torque value for the conditions that day was reported by the crew to be 43.3 psi. With about 2,700 ft of runway remaining while at an altitude of 200 ft msl, the copilot elected to land immediately; the copilot pushed the nose down and executed a 90° left descending turn and subsequently landed in the grass. Although he applied "hard" braking in an attempt to stop, the airplane impacted a drainage ditch, resulting in substantial impact damage and a postimpact fire. The pilot reported that, after takeoff, he observed a low torque CAS message and the copilot told him to "declare an emergency and run the checklist." The pilot confirmed that the landing gear were extended and the copilot turned the airplane to the left toward open ground between the runways and the terminal. About 60 seconds elapsed from the start of the takeoff roll until the accident. The airport was equipped with security cameras that captured the airplane from its initial climb through the landing and collision. One camera, pointed toward the west-southwest, recorded the airplane's left descending turn and its landing in the grass, followed by impact and smoke. A second camera, mounted on the control tower, pointed toward the southeast and showed the airplane during the initial climb before it leveled off and entered a descending left turn; it also showed the airplane land and roll through the grass before colliding with the ditch.
Probable cause:
The pilots' failure to follow proper procedures in response to a crew alerting system warning for high engine torque values, which necessitated an off-runway emergency landing during which the airplane sustained substantial damage due to postimpact fire. Contributing to the accident was the erroneous engine torque indication for reasons that could not be determined.
Final Report:

Crash of a Cessna 441 Conquest II in Climax: 2 killed

Date & Time: Nov 9, 2015 at 1016 LT
Type of aircraft:
Operator:
Registration:
N164GP
Flight Phase:
Survivors:
No
Schedule:
Lakeland - Cairo
MSN:
441-0164
YOM:
1980
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1150
Captain / Total hours on type:
150.00
Aircraft flight hours:
18422
Circumstances:
The purpose of the flight was for the commercial pilot/owner to pick up passengers at the destination airport and return to the departure airport. The airplane was 33 miles from its destination in cruise flight at 3,300 ft mean sea level (msl) and above a solid cloud layer when the pilot declared to air traffic control (ATC) that he had the destination airport "in sight" and cancelled his instrument flight rules (IFR) clearance. During the 13 minutes after cancellation of the IFR clearance, the airplane's radar track made an erratic sequence of left, right, and 360° turns that moved the airplane away from the destination airport in a westerly direction. The altitudes varied between about 4,000 and 900 ft msl. Later, the pilot reestablished communication with ATC, reported he had lost visual contact with the airport, and requested an instrument approach to the destination airport. The controller then provided a sequence of heading and altitude assignments to vector the airplane onto the approach, but the pilot did not maintain these assignments, and the controller provided several corrections. The pilot expressed his inability to identify the initial approach fix (IAF) and asked the controller for the correct spelling. The radar target then climbed and subsequently entered a descending right turn at 2,500 ft msl and 180 knots ground speed near the IAF, before radar contact with the airplane was lost. Although a review of airplane maintenance records revealed that the airplane was overdue for several required inspections, examination of the wreckage revealed signatures consistent with both engines being at high power at impact, and no evidence of any preimpact mechanical anomalies were found that would have precluded normal operation. Examination of the airplane's panel-mounted GPS, which the pilot was using to navigate the flight, revealed that the navigation and obstruction databases were expired. During a weather briefing before the flight, the pilot was warned of low ceilings and visibility. The weather conditions reported near the destination airport about the time of the accident also included low ceilings and visibilities. The restricted visibility conditions and the high likelihood of inadvertent entry into instrument meteorological conditions were conducive to the development of spatial disorientation. The flight's erratic track, which included altitude and directional changes inconsistent with progress toward the airport, were likely the result of spatial disorientation. After reestablishing contact with ATC and being cleared to conduct an instrument approach to the destination, the airplane's flight track indicated that the pilot was not adequately prepared to execute the controller's instructions. The pilot's subsequent loss of control was likely the result of spatial disorientation due to his increased workload and operational distractions associated with his attempts to configure his navigation radios or reference charts. Postaccident toxicological testing of samples obtained from the pilot revealed the presence of ethanol; however, it could not be determined what percentage was ingested or produced postmortem. The testing also revealed the presence of amphetamine, an opioid painkiller, two sedating antihistamines, and marijuana. Although blood level quantification of these medications and drugs could not be made from the samples provided, their combined effects would have directly impacted the pilot's decision-making and ability to fly the airplane, even if each individual substance was only present in small amounts. Based in the reported weather conditions at the time the pilot reported the airport in sight and canceled his IFR clearance, he likely was not in a position to have seen the destination airport even though he may have been flying between cloud layers or may have momentarily observed the ground. His decision to cancel his IFR clearance so far from the destination, in an area characterized by widespread low ceilings and reduced visibility, increased the pilot's exposure to the hazards those conditions posed to the successful completion of his flight. The pilot showed other lapses in judgment associated with conducting this flight at the operational, aircraft, and the personal level. For example, 1) the pilot did not appear to recognize the significance of widespread low ceilings and visibility along his route of flight and at his destination (nor did he file an alternate airport even though conditions warranted); 2) the accident airplane was being operated beyond mandatory inspection intervals; and 3) toxicological testing showed the pilot had taken a combination of multiple medications and drugs that would have likely been impairing and contraindicated for the safe operation of an airplane. The pilot's decision-making was likely affected by the medications and drugs.
Probable cause:
The pilot's loss of airplane control due to spatial disorientation. Also causal to the accident was the pilot's impairment by the combined effects of multiple medications and drugs.
Final Report:

Crash of a Socata TBM-850 in Fayetteville

Date & Time: Oct 5, 2014 at 1255 LT
Type of aircraft:
Operator:
Registration:
N536EM
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Atlanta – Pine Mountain
MSN:
536
YOM:
2010
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4244
Captain / Total hours on type:
411.00
Aircraft flight hours:
719
Circumstances:
The private pilot was conducting a personal cross-country flight. The pilot reported that, during cruise flight at 6,000 ft mean sea level, he observed a crew alerting system oil pressure message, followed by a total loss of engine power. An air traffic controller provided vectors to a local airport; however, the pilot reported that the airplane would not reach the runway. He did not attempt to restart the engine. He feathered the propeller and placed the power lever to "idle" and the condition lever to "cut off." The pilot subsequently attempted a forced landing to a sports field with the gear and flaps retracted. The airplane collided with trees and the ground and then came to rest upright. Examination of the engine revealed that it displayed contact signatures to its internal components and evidence of ingested unburned organic debris, consistent with the engine likely being unpowered and the engine gas generator and power sections wind-milling at the time of impact. No evidence of any preimpact mechanical anomalies or malfunctions to any of the engine components was found that would have precluded normal operation. Recorded GPS flight track and systems data showed that the loss of engine power was preceded by about 5 minutes of flight on a constant heading and altitude with an excessive lateral g force of about 0.17 g and a bank angle between about 8 and 10 degrees, consistent with a side-slip flight condition. The airplane then entered a right turn with the autopilot engaged, and it lost power at the end of the turn. The data indicated that, even though the autopilot was engaged, the lateral g forces increased as the airplane leveled off and accelerated, indicating that the automatic rudder trim feature of the yaw damper system was not engaged. Given that the yaw damper system operated normally after the flight, it is likely that the pilot inadvertently and unknowingly disengaged the yaw damper during flight with the autopilot engaged. During a postaccident interview, the pilot stated that he was not aware of a side-slip condition before the loss of engine power. Although the fuel tank system was designed to prevent unporting of the fuel lines during momentary periods of uncoordinated flight, it was not intended to do so for extended periods of uncoordinated flight. Therefore, the fuel tank feed line likely unported during the prolonged uncoordinated flight, which resulted in the subsequent loss of engine power. If the pilot had recognized the side-slip condition, he could have returned to coordinated flight and prevented the engine power loss. Also, once the airplane returned to coordinated flight, an engine restart would have been possible.
Probable cause:
The pilot's inadvertent deactivation of the yaw damper in flight, which resulted in a prolonged side-slip condition that led to fuel starvation and the eventual total loss of engine power. Contributing to the accident was the pilot's failure to attempt to restart the engine.
Final Report:

Crash of a Piper PA-46-310P Malibu in Clayton: 1 killed

Date & Time: Jul 26, 2014 at 0850 LT
Operator:
Registration:
N248SP
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Clayton - Aurora
MSN:
46-8608024
YOM:
1986
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4200
Aircraft flight hours:
3593
Circumstances:
The pilot was departing the private, fly-in community airport on a personal flight. He was familiar with the airport/fly-in community and was instrumental in its development. Fog was present at the time, and, according to witnesses, it was "rolling up the valley," which was a frequent event at the airport. The witnesses observed the airplane lift off the runway, drift to the left, and disappear into the fog with the landing gear extended. They heard the engine running normally, with no change in sound, until the crash. They heard two distinct "booms" about 4 to 6 seconds apart. They ran down to the departure end of the runway to look for a crash site and could not see the wreckage or any smoke or fire due to the fog. The wreckage was located on elevated terrain in a heavily wooded area, about 1,500 feet north of the departure end of the runway. The elevation at the crash site was about 250 feet higher than the elevation at the departure end of runway. A swath through the treetops leading to the main wreckage was indicative of a near-level flight path at impact. An examination of the airframe and engine did not reveal any evidence of a preexisting mechanical malfunction or failure. A review of the weather by a NTSB meteorologist revealed that the departure airport was at the edge of an area of low-topped clouds. Airport remarks included "Mountainous terrain all quadrants."
Probable cause:
The pilot's decision to begin a flight with fog and low clouds present at the airport, which resulted in an encounter with instrument meteorological conditions immediately after takeoff and a controlled flight into terrain.
Final Report:

Crash of a Raytheon 390 Premier I in Atlanta: 2 killed

Date & Time: Dec 17, 2013 at 1924 LT
Type of aircraft:
Operator:
Registration:
N50PM
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Atlanta - New Orleans
MSN:
RB-80
YOM:
2003
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
7200
Captain / Total hours on type:
1030.00
Aircraft flight hours:
713
Circumstances:
The pilot and passenger departed on a night personal flight. A review of the cockpit voice recorder (CVR) transcript revealed that, immediately after departure, the passenger asked the pilot if he had turned on the heat. The pilot subsequently informed the tower air traffic controller that he needed to return to the airport. The controller then cleared the airplane to land and asked the pilot if he needed assistance. The pilot replied "negative" and did not declare an emergency. The pilot acknowledged to the passenger that it was hot in the cabin. The CVR recorded the enhanced ground proximity warning system (EGPWS) issue 11 warnings, including obstacle, terrain, and stall warnings; these warnings occurred while the airplane was on the downwind leg for the airport. The airplane subsequently impacted trees and terrain and was consumed by postimpact fire. Postaccident examination of the airplane revealed no malfunctions or anomalies that would have precluded normal operation. During the attempted return to the airport, possibly to resolve a cabin heat problem, the pilot was operating in a high workload environment due to, in part, his maneuvering visually at low altitude in the traffic pattern at night, acquiring inbound traffic, and being distracted by the reported high cabin temperature and multiple EGPWS alerts. The passenger was seated in the right front seat and in the immediate vicinity of the flight controls, but no evidence was found indicating that she was operating the flight controls during the flight. Although the pilot had a history of coronary artery disease, the autopsy found no evidence of a recent cardiac event, and an analysis of the CVR data revealed that the pilot was awake, speaking, and not complaining of chest pain or shortness of breath; therefore, it is unlikely that the pilot's cardiac condition contributed to the accident. Toxicological testing detected several prescription medications in the pilot's blood, lung, and liver, including one to treat his heart disease; however, it is unlikely that any of these medications resulted in impairment. Although the testing revealed that the pilot had used marijuana at some time before the accident, insufficient evidence existed to determine whether the pilot was impaired by its use at the time of the accident. Toxicology testing also detected methylone in the pilot's blood. Methylone is a stimulant similar to cocaine and Ecstasy, and its effects can include relaxation, euphoria, and excited calm, and it can cause acute changes in cognitive performance and impair information processing. Given the level of methylone (0.34 ug/ml) detected in the pilot's blood, it is likely that the pilot was impaired at the time of the accident. The pilot's drug impairment likely contributed to his failure to maintain control of the airplane.
Probable cause:
The pilot's failure to maintain airplane control while maneuvering the airplane in the traffic pattern at night. Contributing to the accident was the pilot's impairment from the use of illicit drugs.
Final Report:

Crash of a Raytheon 390 Premier I in Thomson: 5 killed

Date & Time: Feb 20, 2013 at 2006 LT
Type of aircraft:
Operator:
Registration:
N777VG
Flight Phase:
Survivors:
Yes
Schedule:
Nashville - Thomson
MSN:
RB-208
YOM:
2007
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
13319
Captain / Total hours on type:
198.00
Copilot / Total flying hours:
2932
Copilot / Total hours on type:
45
Aircraft flight hours:
635
Circumstances:
Aircraft was destroyed following a collision with a utility pole, trees, and terrain following a go-around at Thomson-McDuffie Regional Airport (HQU), Thomson, Georgia. The airline transport-rated pilot and copilot were seriously injured, and five passengers were fatally injured. The airplane was registered to the Pavilion Group LLC and was operated by the pilot under the provisions of 14 Code of Federal Regulations Part 91 as a business flight. Night visual meteorological conditions prevailed, and an instrument flight rules flight plan was filed. The flight originated at John C. Tune Airport (JWN), Nashville, Tennessee, about 1828 central standard time (1928 eastern standard time). The purpose of the flight was to transport staff members of a vascular surgery practice from Nashville to Thomson, where the airplane was based. According to initial air traffic control information, the pilot checked in with Augusta approach control and reported HQU in sight. About 2003, the pilot cancelled visual flight rules flight-following services and continued toward HQU. The last recorded radar return was observed about 2005, when the airplane was at an indicated altitude of 700 feet above mean sea level and 1/2 mile from the airport. There were no distress calls received from the crew prior to the accident. Witnesses reported that the airplane appeared to be in position to land when the pilot discontinued the approach and commenced a go-around. The witnesses observed the airplane continue down the runway at a low altitude. The airplane struck a poured-concrete utility pole and braided wires about 59 feet above ground level. The pole was located about 1/4 mile east the departure end of runway 10. The utility pole was not lighted. During the initial impact with the utility pole, the outboard section of the left wing was severed. The airplane continued another 1/4 mile east before colliding with trees and terrain. A postcrash fire ensued and consumed a majority of the airframe. The engines separated from the fuselage during the impact sequence. On-scene examination of the wreckage revealed that all primary airframe structural components were accounted for at the accident site. The landing gear were found in the down (extended) position, and the flap handle was found in the 10-degree (go-around) position. An initial inspection of the airport revealed that the pilot-controlled runway lights were operational. An examination of conditions recorded on an airport security camera showed that the runway lights were on the low intensity setting at the time of the accident. The airport did not have a control tower. An inspection of the runway surface did not reveal any unusual tire marks or debris. Weather conditions at HQU near the time of the accident included calm wind and clear skies.
Probable cause:
The pilot's failure to follow airplane flight manual procedures for an antiskid failure in flight and his failure to immediately retract the lift dump after he elected to attempt a go-around on the runway. Contributing to the accident were the pilot's lack of systems knowledge and his fatigue due to acute sleep loss and his ineffective use of time between flights to obtain sleep.
Final Report:

Crash of a Beechcraft Beechjet 400A in Macon

Date & Time: Sep 18, 2012 at 1003 LT
Type of aircraft:
Operator:
Registration:
N428JD
Survivors:
Yes
Schedule:
Charleston - Macon
MSN:
RJ-13
YOM:
1986
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7000
Captain / Total hours on type:
4000.00
Copilot / Total flying hours:
2500
Copilot / Total hours on type:
450
Aircraft flight hours:
5416
Circumstances:
The aircraft was substantially damaged when it overran runway 28 during landing at Macon Downtown Airport (MAC), Macon, Georgia. The airplane departed from Charleston Air Force Base/International Airport (CHS), Charleston, South Carolina, about 0930. Visual meteorological conditions prevailed and an instrument flight rules (IFR) flight plan was filed. Both Airline Transport Pilots (ATP) and one passenger sustained minor injuries. The airplane was owned by Dewberry, LLC and operated by The Aviation Department. The corporate flight was conducted under the provisions of Title 14 Code of Federal Regulations (CFR) Part 91. According to an interview with the pilots, they arrived at DeKalb-Peachtree Airport (PDK), Atlanta, Georgia, which was their home base airport, about 0400, and then drove about 4 1/2 hours to CHS for the 0930 flight. The flight departed on time, the airspeed index bug was set on the co-pilot's airspeed for a decision takeoff speed (V1) of about 102 knots and a single engine climb speed (V2) on the pilot's side of 115 knots. The flight climbed to 16,000 feet prior to beginning the descent into MAC. When the flight was about 11 miles from the airport the flight crew visually acquired the airport and cancelled their IFR clearance with the Macon Radar Approach controller and proceeded to the airport visually. The second-in-command activated the runway lights utilizing the common traffic advisory frequency for the airport. Both crew members reported that about 3 seconds following activation of the lights and the precision approach path indicator (PAPI) lights, the PAPI lights turned off and would not reactivate. During the approach, the calculated reference speed (Vref) was 108 knots and was set on both pilots' airspeed indicator utilizing the index bug that moved around the outside face of the airspeed instrument. The landing was within the first 1,000 feet of the runway and during the landing roll out the airplane began to "hydroplane" since there was visible standing water on the runway and the water was "funneling into the middle." Maximum reverse thrust, braking, and ground spoilers were deployed; however, both pilots reported a "pulsation" in the brake system. The airplane departed the end of the runway into the grass, went down an embankment, across a road, and into trees. They further added that the airplane "hit hard" at the bottom of the embankment. They also reported that there were no mechanical malfunctions with the airplane prior to the landing. According to an eyewitness statement, a few minutes prior to the airplane landing, the airport experienced a rain shower with a "heavy downpour." The witness reported observing the airplane on approach, heard the engine thrust reverse, and then observed the airplane "engulfed in a large ball of water vapor." However, he did not observe the airplane as it departed the end of the runway. Another witness was located in a hangar on the west side of the airport and heard the airplane, looked outside and then saw the airplane with the reverse thrusters deployed. He watched it depart the end of the runway and travel into the nearby woods.
Probable cause:
The pilot’s failure to maintain proper airspeed, which resulted in the airplane touching down too fast on the wet runway with inadequate runway remaining to stop and a subsequent runway overrun. Contributing to the landing overrun were the flight crew members’ failure to correctly use the appropriate performance chart to calculate the runway required to stop on a contaminated runway and their general lack of proper crew resource management.
Final Report: