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Crash of a Beechcraft A100 King Air in Terrace Bay

Date & Time: Jan 1, 2004
Type of aircraft:
Operator:
Registration:
C-GFKS
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Terrace Bay – Thunder Bay
MSN:
B-247
YOM:
1979
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On take off roll on runway 25 at dusk, left wing struck a snowbank on left side of the runway. Aircraft veered off runway and came to rest in snow with its nose gear sheared off and several damages to the fuselage. Both pilots were uninjured.
Probable cause:
A NOTAM stated that there were windrows four feet high, 10 feet inside the runway lights on both sides of the runway. This NOTAM also stated that the cleared portion of the runway was covered with ¼ inch of loose snow over 60 percent compacted snow and 40 percent ice patches and that braking action was fair to poor. The take-off was being conducted at dusk in conditions of poor lighting and contrast. Crosswind was not a factor.

Crash of a Beechcraft A100 King Air in Thunder Bay

Date & Time: Jun 14, 1999 at 1038 LT
Type of aircraft:
Operator:
Registration:
C-GASW
Flight Phase:
Survivors:
Yes
Schedule:
Thunder Bay – Red Lake
MSN:
B-108
YOM:
1972
Flight number:
THU103
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The Thunder Airlines Limited Beech A100 King Air aircraft, serial number B108, took off at 1034 eastern daylight saving time (EDT) on a charter flight from Thunder Bay, Ontario, for Red Lake, Ontario, with two pilots and three passengers on board. After getting airborne, the aircraft pitched up to approximately 70 degrees, reaching a height estimated to be between 500 and 700 feet above ground level. It then rolled to the left, pitched steeply nose-down, and descended to the ground within the confines of the airport. The aircraft contacted the soft, level ground in a relatively level attitude and covered a distance of about 500 feet before coming to rest in a wooded area immediately beyond an elevated railroad bed and track. The cabin remained intact during the crash sequence, and all occupants escaped without any injuries. The aircraft was damaged beyond repair. An ensuing fuel-fed fire was rapidly extinguished by airport emergency response services (ERS)
personnel.
Probable cause:
The flight crew lost pitch control of the aircraft on take-off when the stabilizer trim actuators became disconnected because they had not been properly reinstalled by the AME during maintenance work conducted before the flight. The crew chief responsible for the inspection did not ensure correct assembly of the stabilizer trim actuators, which contributed to the accident.
Final Report: