Crash of a Boeing 737-291 near Toacaso: 3 killed

Date & Time: Aug 30, 2008 at 2103 LT
Type of aircraft:
Operator:
Registration:
YV102T
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Caracas – Latacunga
MSN:
21545/525
YOM:
1978
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
9018
Captain / Total hours on type:
5915.00
Copilot / Total flying hours:
3000
Copilot / Total hours on type:
989
Aircraft flight hours:
60117
Aircraft flight cycles:
52091
Circumstances:
The aircraft was parked at Caracas Airport for a while and had just been sold to an Ecuadorian operator. A crew of three departed Caracas-Maiquetía-Simón Bolívar Airport in the evening on a delivery flight to Latacunga, Ecuador. After being cleared to descend to FL180, FL150 then FL130, the crew was flying over a mountainous area when the GPWS alarm sounded. The crew apparently elected to gain height but the alarm sounded for 22 seconds when the aircraft collided with the Iliniza Volcano. The aircraft disintegrated on impact and all three occupants were killed. The wreckage was found the following day at an altitude of 3,992 metres.
Probable cause:
Non-compliance by the crew of the technical procedures, configuration, speed and bank angle of the aircraft required for the completion of the initial turn of the Instrument Approach Procedure n°4 published in the AIP Ecuador, to Latacunga Airport, a failure that placed the aircraft outside of the protected area (published pattern), leading to high elevation mountainous terrain.
Contributing factors:
- Ignorance of the crew of the area which was under the approach path.
- Lack of documentation and procedures of the airline that govern the conduct of flights to non-scheduled and special airports.

Crash of a Piper PA-31T Cheyenne II in Zweibrücken: 1 killed

Date & Time: Feb 12, 2007 at 1020 LT
Type of aircraft:
Operator:
Registration:
N160TR
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Zweibrücken – Split – Athens
MSN:
31-7920036
YOM:
1979
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The pilot departed Zweibrücken Airport on a flight to Athens with an intermediate stop in Split as the aircraft should be delivered to its new owner based in Greece. After takeoff from runway 21 at Zweibrücken Airport, while in initial climb, the aircraft deviated to the left while the standard departure route was a straight climb until 7 nm. The pilot was contacted by ATC and reported problems. Shortly later, the altitude of the aircraft fluctuated from 1,500 to 3,200 feet and again, the pilot was contacted by ATC to check the situation. Few seconds later, the aircraft entered an uncontrolled descent and crashed in an open field located in Rieschweiler, about 6 km northeast of the airport. The aircraft was totally destroyed upon impact and the pilot, sole on board, was killed. It was reported that, prior to departure, the pilot encountered difficulties to close the main cabin door and had to be shown how to operate it. A member of the FBO staff then asked the pilot if he should explain the aircraft's avionics and, after the pilot replied yes, went on to describe how to operate the RNAV system. The pilot then had difficulty in starting the right engine and was directed to the 'ignition switch' on the overhead panel.

Crash of a Beechcraft 200 Super King Air in Kaduna: 2 killed

Date & Time: Nov 28, 2005 at 1038 LT
Operator:
Registration:
N73MW
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Farnborough - Paris - Oued Isara - Kaduna - Abuja
MSN:
BB-22
YOM:
1975
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The crew took delivery of the aircraft in Farnborough and was supposed to transfer it in Abuja following fuel stop in Paris-Le Bourget, Oued Isara and Kaduna. Shortly after takeoff from Kaduna Airport runway 05, while in initial climb, one of the engine caught fire. The pilot-in-command lost control of the airplane that stalled and crashed, bursting into flames. Both occupants were killed.
Probable cause:
Engine fire/failure for unknown reasons.

Crash of a Cessna 421C Golden Eagle III in El Questro: 2 killed

Date & Time: Aug 30, 2004 at 1200 LT
Operator:
Registration:
HB-LRW
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
El Questro – Broome
MSN:
421C-0633
YOM:
1974
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2128
Captain / Total hours on type:
975.00
Aircraft flight hours:
3254
Circumstances:
On 30 August 2004, shortly before 1200 Western Standard Time, the owner-pilot of a twin-engine Cessna Aircraft Company 421C Golden Eagle (C421) aircraft, registered HB-LRW, commenced his takeoff from runway 32 at El Questro Aircraft Landing Area (ALA). The private flight was to Broome, where the pilot intended resuming the aircraft delivery flight from Switzerland to Perth. The available documentation indicated that the flight segments en route to Australia had all been to international or major aerodromes. The pilot of a Cessna Aircraft Company 210 (C210) and his two passengers in the runway 32 parking area witnessed the takeoff. Those witnesses reported that the C421 pilot carried out a pre-flight inspection of the aircraft prior to boarding for the takeoff. During that inspection, he was observed preparing for, and conducting a fuel drain check under the left wing, and to have removed some weed-like material from the right main wheel. He then loaded a small amount of personal luggage into the aircraft cabin, before he and the sole passenger boarded. The C210 pilot witness, who reported having observed a number of twin-engine aircraft operations at another aerodrome, did not comment on the nature of the pilot's start and engines run-up checks. The passenger witnesses reported that the pilot of the C421 made a number of unsuccessful attempts to start the left engine, before reverting to starting the right engine. He then started the left engine and moved the aircraft clear of the C210 in order to conduct his engine run-up checks. The passenger witnesses reported that during those checks they heard a 'frequency vibration' as the C421 pilot manipulated the engines' controls. The witnesses at the parking area reported that the C421 pilot taxied the aircraft onto the runway and applied power to commence a rolling takeoff. They, together with a hearing witness located to the north of the ALA indicated that the engines sounded 'normal' throughout the takeoff. Witnesses who observed the takeoff reported that the aircraft accelerated away 'briskly'. The pilot witness stated that the take-off roll and lift-off from the runway appeared similar to other twin-engine aircraft takeoffs that he had observed. The witnesses at the parking area also stated that, shortly after lift-off from the runway, the aircraft banked slightly to the left at an estimated 10 to 15 degrees angle of bank and drifted left before striking the trees along the side of the runway and impacting the ground. There was no report of any objects falling from the aircraft, or of any smoke or vapour emanating from the aircraft during the takeoff. The aircraft was destroyed by the impact forces and post-impact fire. The pilot and passenger were fatally injured.
Probable cause:
For reasons that could not be determined, the aircraft commenced a slight left angle of bank and drifted left after lift-off at a height from which the pilot was unable to recover prior to striking trees to the left of the runway.
Final Report:

Crash of a PZL-Mielec AN-28 in Beni

Date & Time: Jul 29, 2004
Type of aircraft:
Registration:
ES-ELI
Flight Type:
Survivors:
Yes
MSN:
1AJ002-06
YOM:
1985
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The twin engine aircraft crashed upon landing, lost its right and came to rest. There were apparently no casualties.

Crash of a PAC 750XL in the Pacific Ocean: 1 killed

Date & Time: Dec 26, 2003 at 0601 LT
Operator:
Registration:
ZK-UAC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Hamilton – Pago Pago – Christmas Island – Kiribati – Hilo – Oakland
MSN:
103
YOM:
2003
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
16564
Captain / Total hours on type:
180.00
Aircraft flight hours:
65
Circumstances:
The pilot was ferrying the aircraft from Hamilton, New Zealand to Davis, California, via Pago Pago, American Samoa; Christmas Island, Kiribati; and Hilo, Hawaii. On the final leg, following a position report 858 nm from San Francisco, he reported a problem with his fuel system, indicating a probable ditching. Under the observation of a US Coast Guard HC-130 crew, the pilot ditched the aircraft at 1701 UTC, 341 nm from San Francisco, the aircraft nosing over on to its back as it touched down. The pilot did not emerge as expected and was later found by rescue swimmers, deceased, still in the cockpit. His body could not be recovered and was lost with the aircraft.
Probable cause:
The following findings were reported:
- The pilot was appropriately licensed, rated and experienced for the series of flights undertaken.
- The aeroplane had a valid airworthiness certificate and had been released to service.
- There was nothing (other than the item in 3.5) to suggest that the aeroplane was operating abnormally on the final flight.
- The aeroplane was being operated at 14 000 feet pressure altitude without supplementary oxygen as required by CAR 91.209 and 91.533.
- The left front fuel filler orifice was observed to be leaking fuel before departure.
- There was no attempt made to further investigate or correct this fuel leak and the pilot stated that it would stop once he departed.
- On most other aircraft this would be true, once the fuel level dropped away from the filler orifice and was no longer affected by aerodynamic suction.
- On the 750XL, the fuel system design was such that the front tanks were continuously topped up.
- The fuel loss would continue until all fuel in the rear tanks and the ferry system was consumed.
- The front fuel caps are thus critical items to be checked before flight.
- The fuel quantity uplifted at Hilo indicated that the problem had existed on the previous leg with a loss rate of up to 125 litres (33.2 US gallons) per hour.
- A comparison of the uplift figure with the expected consumption on the previous leg should have provided sufficient warning to the pilot that a problem existed.
- The existence of the problem could have been detected on the final flight by the shortened top-up intervals and by comparing fuel used by the engine with fuel remaining.
- Cumulative delays, especially including the longer than normal final refuelling time, probably influenced the pilot’s decision to depart without further checking the reason for the fuel leak or the apparent discrepancy between fuel figures.
- Cumulative fatigue, circadian rhythm and hypoxia were probably significant factors in the pilot’s failure to detect the fuel problem in flight, in time to make a safe return.
- By the time the pilot announced that he had a fuel problem, the only course of action open to him was ditching the aeroplane.
- The search and rescue facilities were activated appropriately, and had the potential to effect a successful rescue.
- The water entry impact on ditching was reasonably severe and probably incapacitated the pilot before he could vacate the cockpit.
Final Report:

Crash of a Beechcraft C-12C Huron near Charallave: 2 killed

Date & Time: Oct 10, 2003
Type of aircraft:
Registration:
N48JA
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Caracas – Charallave
MSN:
BC-51
YOM:
1978
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
Lost without trace on a delivery flight from Caracas to Charallave. The wreckage was not found. Both occupants are presumed dead.

Crash of an Antonov AN-26B in Ndjolé: 7 killed

Date & Time: Jan 17, 2003
Type of aircraft:
Operator:
Registration:
ER-AFT
Flight Type:
Survivors:
No
Schedule:
Brazzaville - Douala
MSN:
134 03
YOM:
1984
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
7
Circumstances:
The aircraft departed Brazzaville on a delivery flight to Douala. While cruising by night over Gabon, the crew informed ATC about technical problems, declared an emergency and elected to divert to the nearest airport which was Ndjolé. This airfield was not equipped with any runway or approach lights nor any navigation aids. The crew completed several circuits over the city then people parked their cars along the airstrip so the crew was able to land. After four unsuccessful attempts, the crew tried to land but the aircraft flew over the runway without landing, passed over the Ogooué River and eventually crashed in a wooded and swampy area. The crew of two helicopters from the Gabonese Air Force found the wreckage the following day. The aircraft was destroyed and all seven occupants were killed. Until few days prior to the accident, the aircraft was operated by Pont Aviation which bankrupted, so it was transferred to another operator in Cameroon.
Probable cause:
It is believe that the crew was forced to make an emergency landing following a general failure of the navigation instruments in flight.

Crash of a Piper PA-60 Aerostar (Ted Smith 602P) in Fortingall: 1 killed

Date & Time: Nov 30, 2000 at 1635 LT
Operator:
Registration:
N64719
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Linz – Newcastle – Keflavik – Narsarsuaq – Goose Bay – New York
MSN:
60-8365-006
YOM:
1983
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1860
Circumstances:
Start-up, taxi and take-off were apparently normal with an IFR clearance for a noise abatement right turn-out on track towards the Talla VOR beacon. Soon afterwards the pilot was given clearance to join controlled airspace on track towards Talla at FL 140 and to expect the flight planned level of FL 200 when cleared by Scottish Radar. As the aircraft was climbing through FL 120 the Talla sector controller first cleared the pilot to climb to FL140 and then almost immediately re-cleared him to climb to FL 200. The pilot replied "ER NEGATIVE I WOULD LIKE TO MAINTAIN ONE FOUR ZERO FOR THE TIME BEING" and the controller granted his request. At 16:21 hrs the pilot transmitted "SCOTTISH NOVEMBER SIX FOUR SEVEN ONE NINE ER REQUESTING HIGHER TO GET OUT OF SOME ICING". Initially the controller offered FL 160 but the pilot replied "IF POSSIBLE TWO ZERO ZERO". Immediately he was given clearance to climb to FL 205, the correct quadrantal cruising altitude. Recorded radar data showed that for the next six minutes, the aircraft's rate of climb and airspeed were erratic. The pilot made one brief transmission of "SCOTTISH" at about 16:30 hrs but nothing more was said by him or the controller for another 20 seconds. Then the controller said "NOVEMBER SIX FOUR SEVEN ONE NINE ER I SEE YOU'RE IN THE TURN DO YOU HAVE A PROBLEM". There was no reply and so the controller repeated his message, eventually receiving the reply "YES I HAVE ER AN EMERGENCY". The controller asked the pilot to "SQUAWK SEVEN SEVEN ZERO ZERO" but the pilot replied "HANG ON". By this time the aircraft was descending rapidly in a gentle right turn. The controller twice asked the pilot for the nature of his problem but the pilot asked the controller to 'HANG ON FOR A MOMENT". The controller could see the aircraft was near high ground and losing altitude rapidly. He twice passed messages to this effect to the pilot but he did not receive an immediate reply. At 16:33 hrs the pilot transmitted "CAN YOU GET ME ER SOMEWHERE WHERE I CAN LAND I CAN'T MAINTAIN ALTITUDE AT ALL". Immediately the controller instructed the pilot to take up an easterly heading and gave him the aircraft's position relative to the airport at Perth. The controller then asked the pilot for his flight conditions (twice) to which the pilot eventually replied "I'M COMING OUT OF ER THE CLOUDS NOW" followed by "JUST BREAKING OUT". The controller then said "ROGER DO YOU HAVE ANY POWER AT ALL OR HAVE YOU LOST THE ENGINE". The pilot replied "I GOT POWER AGAIN BUT I HAVE NO CONTROL". That was his last recorded RTF transmission made at 16:34:40 hrs. The final radar return placed the aircraft at an altitude of 3,150 feet overhead Drummond Hill which is on the north bank of Loch Tay, near the village of Fortingall, and rises to 1,500 feet amsl.
Probable cause:
On vacating FL140, the aircraft's climb rate was so erratic at 140 KIAS that it seems likely that by then, the aircraft had already gathered sufficient ice to seriously affect its performance. If all the
turbocharger inlets had become partially blocked, then manually selecting both engines to alternate air induction should have introduced warmer air into the turbochargers and restored power. The description of engine operation in the Superstar manual states:
'If manifold pressure continues to decrease after opening the manual alternate air, it is an indication that turbocharger inlets are still restricted and the engine may become normally aspirated through the automatic alternate air door located below the induction air filter'.
Normal aspiration reduces the manifold pressure to ambient or less and at FL140 the ambient pressure is about 17.6 inches which is less than half the climb rated manifold pressure. That might explain the inability to climb above FL 160 but it would also have deprived the pilot of pressurisation. There was no change in his voice consistent with donning an oxygen mask so he may not have lost pressurisation completely. Nevertheless, since he lost control at around FL160 and 110 KIAS, and because the aircraft initially turned to the right, a combination of airframe icing and asymmetric power loss seem the most likely explanation for the sustained loss of control. The split in the EDP diaphragm which almost certainly occurred during this flight may have contributed to an asymmetric power problem. Alternatively, the pilot might have become mildly hypoxic and decided to begin an emergency descent. If so, he did not declare an emergency at the time he started to descend, although he did utter the word "SCOTTISH" after control was lost, so he was conscious even if his mental abilities had been impaired by hypoxia. On balance, the tone of his voice and his initial failure to respond to ATC messages suggested that the descent was begun through loss of control rather than a deliberate act followed by loss of control. At the time of the accident the aircraft had been flying below the freezing level (8,000 feet) for about five minutes and much of the airframe and induction system ice may have melted. The would-be rescuers would have taken at least five minutes to reach the crash site and so the fact that none of them reported seeing or treading on any ice was not surprising. Witness and propeller evidence indicated that power had been restored on at least one engine but there seemed to be insufficient power to climb out of Glen Lyon. The aircraft was out of control when it crashed at low speed from a sharp turning manoeuvre. Before this manoeuvre the pilot may have had partial control, albeit with a power problem which prevented him from climbing, and he finally lost control totally when he attempted to turn around within the confines of the Glen. He had no choice but to attempt the turn since, had he not turned, he would have flown into the side of the hill above the crash site.
Final Report:

Crash of a Rockwell Grand Commander 690B in São Tomé

Date & Time: Nov 1, 2000 at 1745 LT
Operator:
Registration:
N6900K
Flight Type:
Survivors:
Yes
Schedule:
Luanda - São Tomé
MSN:
690-11441
YOM:
1978
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The pilot, sole on board, was completing a delivery flight from South Africa to the US via Luanda and São Tomé. Upon landing at São Tomé Airport, the left main gear collapsed. The aircraft slid on its belly for few dozen metres and came to rest. The pilot was uninjured.
Probable cause:
It was reported that the aircraft was unstable on final approach and not properly aligned with the runway centerline. This caused the aircraft to land hard in 'crab' configuration, causing the left main gear to collapse upon touchdown.