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Crash of a Beechcraft C90 King Air in Rockford

Date & Time: Dec 5, 2017 at 1802 LT
Type of aircraft:
Registration:
N500KR
Flight Type:
Survivors:
Yes
Schedule:
Kissimmee - Rockford
MSN:
LJ-708
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2500
Aircraft flight hours:
9856
Circumstances:
The private pilot departed on a cross-country flight in his high-performance, turbine-powered airplane with full tanks of fuel. He landed and had the airplane serviced with 150 gallons of fuel. He subsequently departed on the return flight. As the airplane approached the destination airport, the pilot asked for priority handling and reported that the airplane "lost a transfer pump and had a little less fuel than he thought," and he did not want to come in with a single engine. When asked if he needed assistance, he replied "negative." The pilot was cleared to perform a visual approach to runway 19 during night conditions. As the airplane approached the airport, the pilot requested the runway lights for runway 25 be turned on and reported that the airplane lost engine power in one engine. The controller advised that the lights on runway 25 were being turned on and issued a landing clearance. The airplane impacted terrain before the threshold for runway 25. During examination of the recovered wreckage, flight control continuity was established. No useable amount of fuel was found in any of the airplane's fuel tanks; however, fuel was observed in the fuel lines. All transfer pumps and boost pumps were operational. The engine-driven fuel pumps on both engines contained fuel in their respective fuel filter bowls. Both pumps were able to rotate when their input shafts were manipulated by hand. Disassembly of both pumps revealed that their inlet filters were free of obstructions. Bearing surfaces in both pumps exhibited pitting consistent with pump operation with inadequate fuel lubrication and fuel not reaching the pump. The examination revealed no evidence of airframe or engine preimpact malfunctions or failures that would have precluded normal operation of the airplane. Performance calculations using a flight planning method described in the airplane flight manual indicated that the airplane could have made the return flight with about 18 gallons (119 lbs) of fuel remaining. However, performance calculations using a fuel burn simulation method developed from the fuel burn and data from the airplane flight manual indicated that the airplane would have run out of fuel on approach. Regulations require that a flight depart with enough fuel to fly to the first point of intended landing and, assuming normal cruising speed, at night, to fly after that for at least 45 minutes. The calculated 45-minute night reserves required about 56 gallons (366 lbs) of fuel using a maximum recommended cruise power setting or about 37.8 gallons (246 lbs) of fuel using a maximum range power setting. Regardless of the flight planning method he could have used, the pilot did not depart on the accident flight with the required fuel reserves and exhausted all useable fuel while on approach to the destination. The airplane was owned by Edward B. Noakes III.
Probable cause:
The pilot's inadequate preflight planning and his decision to depart without the required fuel reserve, which resulted in fuel exhaustion during a night approach and subsequent loss of engine power.
Final Report:

Crash of a Cessna 550 Citation II in Dillon: 2 killed

Date & Time: May 3, 2007 at 1037 LT
Type of aircraft:
Operator:
Registration:
N22HP
Flight Type:
Survivors:
No
Schedule:
Rockford - Dillon
MSN:
550-0103
YOM:
1986
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
5057
Captain / Total hours on type:
1200.00
Aircraft flight hours:
10526
Circumstances:
Radar data indicated that the airplane descended on a straight track from flight level (FL) 380 in accordance with the pilot's clearance to descend to 13,000 feet and begin the VOR (very high frequency omni-directional radio range) approach to the destination airport. The last transmission from the pilot was an acknowledgment of the cancellation of radar service and an instruction to switch to the airport advisory frequency. At that time, the airplane was at a mode C reported altitude of 14,000 feet. The airplane maintained a steady descent rate for the next minute and leveled off at 13,000 feet. About 2 1/2 minutes later, the airplane began a turn to the right to head outbound for the procedure turn on the approach and descended to 12,900 feet. The approach procedure specified a minimum altitude of 8,200 feet in the procedure turn. The airplane lost 1,600 feet in the next 10 seconds, and this was the last radar contact. A witness working in his office at the airport heard a loud engine noise, and then a “plop” noise. He said that the engine noise was loud, then softer, and then loud again. He heard it for 3 to 5 seconds. Another witness saw an airplane below the cloud bases that was turning to the right with a nose low pitch attitude of about 75 to 80 degrees. It made six to seven turns before it disappeared from sight behind terrain, and the radius of the turn got tighter as the airplane descended. Examination of the airframe, systems, and engines revealed no anomalies that would have precluded normal operation. Anti-ice fluid was on the leading edges of the wing and tail anti-ice panels. An Airmen’s Meteorological Information (AIRMET) in effect for an area that included the accident site noted that the freezing level was from 4,000 to 10,000 feet with the potential for icing from the freezing level to 20,000 feet.
Probable cause:
An in-flight loss of control for undetermined reasons.
Final Report:

Crash of a Dassault Falcon 20C in Detroit

Date & Time: Aug 28, 2001 at 1805 LT
Type of aircraft:
Operator:
Registration:
N617GA
Flight Type:
Survivors:
Yes
Schedule:
Detroit – Rockford
MSN:
88
YOM:
1967
Flight number:
GAE617
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
24000
Captain / Total hours on type:
900.00
Copilot / Total flying hours:
5700
Copilot / Total hours on type:
200
Aircraft flight hours:
13282
Circumstances:
The airplane sustained substantial damage on impact with terrain and objects after traveling off the end of the runway during a main wheels up landing. The captain reported that prior to takeoff, he closed the cargo door and the copilot confirmed the door light was out. After takeoff at an altitude of about 600 feet, the cockpit door popped open and the crew noticed the cargo door was open. The captain elected to return to land. The captain reported he requested repeatedly for gear and flaps extension, but the copilot was late in doing so and it "caused us to overshoot the runway centerline." The copilot then began calling for a go around/missed approach at which time he raised the gear and the retracted some of the flaps. The copilot reported the captain continued to descend toward the runway and overshot the runway centerline to the right. The copilot reported that at this time he lowered the gear. The nose gear extended prior to touchdown, however the main gear did not. The airplane touched down approximately 1/2 way down the runway and traveled off the end. A witness reported noticing that the exterior door latch was not down as the airplane taxied to the runway.
Probable cause:
The wheels up landing performed by the flightcrew during the emergency landing and improper aircraft preflight by the pilot in command. Factors were the unsecured cargo door, the cemetery fence, and the lack of crew coordination during the flight.
Final Report:

Crash of a Beechcraft H18 in Rockford: 1 killed

Date & Time: Sep 22, 1987 at 0802 LT
Type of aircraft:
Operator:
Registration:
N5850S
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Kenosha - Atlanta
MSN:
BA-720
YOM:
1965
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3200
Captain / Total hours on type:
800.00
Aircraft flight hours:
6716
Circumstances:
The commercial pilot was on a repositioning flight from Kenosha, Wisconsin to Atlanta, Georgia, after having been without sleep for about 20 hours. Witnesses observed the aircraft circling a subdivision near Rockford, Illinois at a low altitude, just above the treetops. The aircraft was in a steep left bank, described as 70-90°, when it reversed direction into a steep right bank and descended into the trees. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: abrupt maneuver
Phase of operation: maneuvering - turn to reverse direction
Findings
1. (c) clearance - misjudged - pilot in command
2. (f) fatigue (lack of sleep) - pilot in command
3. (c) judgment - poor - pilot in command
----------
Occurrence #2: in flight collision with object
Phase of operation: maneuvering - turn to reverse direction
Findings
4. (f) object - tree(s)
Final Report:

Crash of a Beechcraft E18S in Cleveland: 1 killed

Date & Time: Jun 22, 1972 at 0740 LT
Type of aircraft:
Registration:
N42A
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Philadelphia - Cleveland - Rockford
MSN:
BA-133
YOM:
1956
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
15176
Captain / Total hours on type:
1361.00
Circumstances:
Just after liftoff, while in initial climb, the left wing detached. Out of control, the airplane crashed in a huge explosion and was destroyed by impact forces and a post crash fire. The pilot, sole on board, was killed.
Probable cause:
Structural failure and detachment of the left wing during initial climb and uncontrolled descent due to the presence of fatigue cracks. The following factors were reported:
- Inadequate inspection of the aircraft on part of the maintenance personnel,
- Wings spars,
- Fatigue fracture,
- Left wing failed, folded up,
- Fatigue crack was present during prior inspection but was not detected.
Final Report:

Crash of a Beechcraft D18S off Manitou Beach: 2 killed

Date & Time: Jul 27, 1970 at 0045 LT
Type of aircraft:
Registration:
N332R
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Rockford - Detroit
MSN:
A-8
YOM:
1945
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3050
Captain / Total hours on type:
1200.00
Circumstances:
The pilot and his passenger departed Rockford in the early morning and completed several flights in the region all along the day. While cruising by night over Lake Michigan, the pilot lost control of the airplane that crashed into the lake off Manitou Beach. Both occupants were killed.
Probable cause:
Loss of control in flight after the pilot became lost/disoriented. The following factors were considered as contributing:
- Physical impairment,
- Pilot fatigue,
- Departed Rockford approximately 18 hours prior to the accident,
- Flew 10 hours during the day,
- Attended copilot picnic observed with can beer,
- Toxicologic not decisive.
Final Report:

Crash of a Stinson SM-2A Junior in Rockford: 1 killed

Date & Time: Jan 21, 1932 at 1800 LT
Type of aircraft:
Operator:
Registration:
NC443H
Flight Phase:
Survivors:
No
Site:
Schedule:
Rockford – Chicago
MSN:
1088
YOM:
1929
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
Shortly after takeoff from Rockford Airport, the pilot lost his orientation due to poor visibility caused by foggy conditions. He decided to bail out and abandoned the aircraft. Doing so, he struck the stabilizer and was later found dead. Out of control, the aircraft dove into the ground and crashed in Calvin Park, a district of Rockford. There were no casualties on the ground.