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Crash of a Cessna 421C Golden Eagle III in Las Cruces: 4 killed

Date & Time: Aug 27, 2014 at 1903 LT
Registration:
N51RX
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Las Cruces – Phoenix
MSN:
421C-0871
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
2432
Captain / Total hours on type:
52.00
Aircraft flight hours:
8181
Circumstances:
According to the line service technician who worked for the fixed-base operator (FBO), before taking off for the air ambulance flight with two medical crewmembers and one patient onboard, the pilot verbally asked him to add 40 gallons of fuel to the airplane, but the pilot did not specify the type of fuel. The line service technician drove a fuel truck to the front of the airplane and added 20 gallons of fuel to each of the multiengine airplane's wing tanks. The pilot was present during the refueling and helped the line service technician replace both fuel caps. Shortly after takeoff, a medical crewmember called the company medical dispatcher and reported that they were returning to the airport because smoke was coming from the right engine. Two witnesses reported seeing smoke from the airplane Several other witnesses reported seeing or hearing the impact and then immediately seeing smoke or flames. On-scene evidence showed the airplane was generally eastbound and upright when it impacted terrain. A postimpact fire immediately ensued and consumed most of the airplane. Investigators who arrived at the scene the day following the accident reported clearly detecting the smell of jet fuel. The airplane, which was equipped with two reciprocating engines, should have been serviced with aviation gasoline, and this was noted on labels near the fuel filler ports, which stated "AVGAS ONLY." However, a postaccident review of refueling records, statements from the line service technician, and the on-scene smell of jet fuel are consistent with the airplane having been misfueled with Jet A fuel instead of the required 100LL aviation gasoline, which can result in detonation in the engine and the subsequent loss of engine power. Postaccident examination of the engines revealed internal damage and evidence of detonation. It was the joint responsibility of the line technician and pilot to ensure that the airplane was filled with aviation fuel instead of jet fuel and their failure to do so led to the detonation in the engine and the subsequent loss of power during initial climb.In accordance with voluntary industry standards, the FBO's jet fuel truck should have been equipped with an oversized fuel nozzle; instead, it was equipped with a smaller diameter nozzle, which allowed the nozzle to be inserted into the smaller fuel filler ports on airplanes that used aviation gasoline. The FBO's use of a small nozzle allowed it to be inserted in the accident airplane's filler port and for jet fuel to be inadvertently added to the airplane.
Probable cause:
The misfueling of the airplane with jet fuel instead of the required aviation fuel, and the resultant detonation and a total loss of engine power during initial climb. Contributing to the accident were the line service technician's inadvertent misfueling of the airplane, the pilot's inadequate supervision of the fuel servicing, and the fixed-base operator's use of a small fuel nozzle on its jet fuel truck.
Final Report:

Crash of a Mitsubishi MU-2B-36 Marquise in Scottsdale

Date & Time: Jul 20, 1996 at 0857 LT
Type of aircraft:
Operator:
Registration:
N999FA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Scottsdale - Phoenix
MSN:
676
YOM:
1975
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4559
Captain / Total hours on type:
81.00
Aircraft flight hours:
8878
Circumstances:
The right engine lost power after an uncontained engine failure during the initial takeoff climb. The airplane would not climb and the pilot was forced to land. The pilot selected a street for a forced landing area. The pilot landed gear up while maneuvering to avoid hitting street light poles and automobiles. After touchdown, the airplane slid into a block wall. A fire erupted as a result of a post impact fuel leak in the left wing. The airplane's engines were examined at the manufacturer's facilities. The right engine exhibited evidence of an uncontained separation of the second stage turbine rotor disk. Examination of the disk fragments revealed a low cycle fatigue fracture mode. The fatigue initiated from multiple areas at and adjacent to the inside diameter bore surface near the aft side of the disk. According to the engine manufacturer, the multiple indication areas were associated with uninspectable size porosity and the primary carbides in the cast material. There were no material or casting defects detected on any of the fractures through the wheel.
Probable cause:
Aan uncontained failure of the second stage turbine wheel due to fatigue. Factors were: obstructions in the forced landing area and the inability of the airplane to climb after the turbine wheel failure.
Final Report:

Crash of a Douglas B-26C Invader near Cimarron: 2 killed

Date & Time: Jun 26, 1988 at 1715 LT
Type of aircraft:
Registration:
N4813E
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Goodland - Phoenix
MSN:
29243
YOM:
1944
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1086
Circumstances:
The pilot received a weather briefing before takeoff, but did not file a flight plan. During the flight, the aircraft (Douglas A-26C, N4813E) crashed in mountainous terrain at an elevation of about 11,200 feet near Baldy Mountain. Scouting personnel, who were camped in the vicinity, reported the weather was poor with a low ceiling, restricted visibility, rain and hail. An examination of the crash site revealed the aircraft impacted in a steep, right wing low, nose low attitude. Much of the wreckage collapsed into the impact crater. The degree of destruction was consistent with a high speed impact. Chordwise scratch marks were found on the prop blades. Several tree branches and limbs at the crash site had smooth cuts. The pilot was type rated in the A-26, but his certificate had a limitation that restricted him to flying it in 'VFR only.' Neither the pilot nor the rated passenger held an instrument rating. The rated passenger did not have a type rating in the A-26, but the pilot possessed a waiver to fly N4813E as a single pilot airplane. Both occupants were killed.
Probable cause:
Occurrence #1: in flight encounter with weather
Phase of operation: cruise - normal
Findings
1. (f) light condition - dusk
2. (f) visual/aural perception - pilot in command
3. (f) terrain condition - high terrain
4. (f) weather condition - low ceiling
5. (f) weather condition - fog
6. (f) weather condition - rain
7. (f) weather condition - hail
8. (f) weather condition - obscuration
9. (c) vfr flight into imc - continued - pilot in command
----------
Occurrence #2: loss of control - in flight
Phase of operation: cruise
Findings
10. (c) aircraft control - not maintained - pilot in command
11. (c) spatial disorientation - pilot in command
12. (f) lack of total instrument time - pilot in command
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Findings
13. (f) terrain condition - mountainous/hilly
Final Report:

Crash of a Cessna T207A Skywagon in Sedona

Date & Time: Oct 18, 1984 at 0915 LT
Operator:
Registration:
N6262H
Survivors:
Yes
Schedule:
Phoenix - Sedona
MSN:
207-0456
YOM:
1978
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1217
Captain / Total hours on type:
26.00
Aircraft flight hours:
2029
Circumstances:
On final approach about 1.5 miles from the airport the power loss occurred as the pilot attempted to add power. After flying over a ridge and several trees the aircraft touched down in the rough terrain and caught fire. The fire appeared to have started in the vicinity of the fuel strainer and progressed rearward. There were no indications of fire until the aircraft came to rest. The only discrepancy noted during inspection of the aircraft and engine was that 3 left bank fuel injectors were blocked with a substance later identified as primarily being dirt. Both occupants escaped unhurt.
Probable cause:
Occurrence #1: loss of engine power
Phase of operation: approach - vfr pattern - final approach
Findings
1. (c) reason for occurrence undetermined
----------
Occurrence #2: forced landing
Phase of operation: descent - emergency
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: landing - flare/touchdown
Findings
2. Terrain condition - ground
----------
Occurrence #4: fire
Phase of operation: other
Final Report:

Crash of a Cessna 401 in Sunflower: 5 killed

Date & Time: Mar 18, 1982 at 1210 LT
Type of aircraft:
Registration:
N499W
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Phoenix - Amarillo
MSN:
401-0273
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
2950
Captain / Total hours on type:
364.00
Aircraft flight hours:
5484
Circumstances:
At 1027 the pilot received a weather briefing for Holbrook, AZ. The pilot was told of forecasts for "at least moderate icing in clouds or in precipitation above the freezing level" and the briefer stated "I guarantee you moderate to severe turbulence..." for a route into Holbrook. The pilot later got weather info for Amarillo, TX and filed an IFR flt plan to Amarillo. The aircraft departed at 1150. At 1204 the pilot reported he had an engine problem. Radar plots indicate the aircraft was maintaining a climb of about 500 fpm up to 11,200 ft. Thirty seconds later the aircraft had descended to 8,500 ft. Radio and contact was lost about 1207. Based on a weather study the probable meteorological conditions that existed about the time & in the area of the accident were moderate to severe turbulence below 12,000 ft msl & while in the clouds above freezing level the aircraft likely encountered moderate to severe rime icing. The aircraft was not certificated for flt into known icing conditions. The flight was transporting prisoners for various government agencies.
Probable cause:
Occurrence #1: in flight encounter with weather
Phase of operation: climb - to cruise
Findings
1. (f) weather condition - rain
2. (f) weather condition - turbulence in clouds
3. (f) weather condition - icing conditions
4. (c) flight into known adverse weather - initiated - pilot in command
5. (c) operation with known deficiencies in equipment - attempted - pilot in command
----------
Occurrence #2: loss of control - in flight
Phase of operation: climb - to cruise
Findings
6. (c) wing - ice
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Cessna 404 Titan II in Grand Canyon: 8 killed

Date & Time: Jul 21, 1980 at 1702 LT
Type of aircraft:
Operator:
Registration:
N2683S
Flight Phase:
Survivors:
No
Schedule:
Grand Canyon - Phoenix
MSN:
404-0606
YOM:
1979
Flight number:
YR306
Crew on board:
1
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
2474
Captain / Total hours on type:
323.00
Aircraft flight hours:
718
Circumstances:
At 1702, Scenic Airlines flight 306, a Cessna 404, VFR commuter flight to Phoenix, crashed approximately three miles south of runway 21 after takeoff from the Grand Canyon National Park Airport. The aircraft cut a swath through a densely wooded area on a magnetic heading of 165° and came to rest upright about 230 feet from the initial point of impact with trees. Impact forces and an intense fire destroyed the aircraft. The pilot and six of the seven passengers were killed in the accident. One passenger survived the accident but died five days later as a result of thermal injuries.
Probable cause:
The probable cause of the accident was a substantial loss of power from the left engine at a critical point in the takeoff an the failure of the pilot to establish a minimum drag configuration which degraded the marginal single-engine climb performance of the aircraft. The loss of power resulted from the seizure of the turbocharger following a progressive failure of the turbine wheel blades initiated by foreign object ingestion which had occurred previous to this flight and was not detected during maintenance on the engine 4 days before the accident.
Final Report:

Crash of a Cessna 401B in Phoenix

Date & Time: Jun 5, 1979 at 1708 LT
Type of aircraft:
Operator:
Registration:
N77MG
Survivors:
Yes
Schedule:
Long Beach - Phoenix
MSN:
401B-0006
YOM:
1969
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
519
Captain / Total hours on type:
140.00
Circumstances:
While descending to Phoenix Airport, both engines failed simultaneously. The pilot reduced his altitude and attempted an emergency landing few miles from the airfield. The aircraft came to rest on its belly and was damaged beyond repair. The pilot escaped unhurt.
Probable cause:
Controlled collision with ground following a mismanagement of fuel. The following contributing factors were reported:
- Fuel starvation,
- Failed to follow approved procedures,
- Improper emergency procedures,
- Wet, soft ground,
- Complete failure of both engines,
- Forced landing off airport on land,
- Pilot did not recall changing fuel selector after power loss,
- Tip tanks separated and burned,
- Left auxiliary tank empty,
- Right auxiliary tank demolished.
Final Report:

Crash of a Cessna 402B near Hyder

Date & Time: Sep 7, 1978 at 1323 LT
Type of aircraft:
Operator:
Registration:
N7866Q
Flight Phase:
Survivors:
Yes
Site:
Schedule:
Yuma - Phoenix
MSN:
402B-0116
YOM:
1971
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8289
Captain / Total hours on type:
2622.00
Circumstances:
While in cruising altitude on a flight from Yuma to Phoenix, the left engine caught fire after the exhaust pipe separated in flight. The pilot reduced his altitude and attempted an emergency landing in a desert area located near Hyder, AZ. The airplane crash landed and came to rest in flames. It was destroyed while both occupants escaped with minor injuries.
Probable cause:
Engine fire in flight due to improper maintenance. The following contributing factors were reported:
- Powerplant failure: exhaust system,
- Excessive vibration and then separation of exhaust pipe due to fatigue fracture,
- Fire in engine,
- Forced landing off airport on land,
- Bolt connecting ball joint on left engine right side found missing.
Final Report:

Crash of a Learjet 23 in Hollywood

Date & Time: Mar 30, 1978 at 2250 LT
Type of aircraft:
Operator:
Registration:
N133W
Survivors:
Yes
Schedule:
Phoenix - Hollywood
MSN:
23-021
YOM:
1965
Crew on board:
3
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2600
Captain / Total hours on type:
1680.00
Circumstances:
After touchdown at Hollywood-Burbank Airport, the crew started the braking procedure but the airplane was unable to halt within the remaining distance. It overran and eventually collided with a fence. All five occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
Overran and collided with fence upon landing due to the failure of the normal braking system. The following contributing factors were reported:
- Material failure,
- Hydroplaning on wet runway,
- Airport conditions: wet runway,
- Rain,
- Left outboard anti-skid valve inoperative.
Final Report:

Crash of a Cessna 414 Chancellor near Farson: 1 killed

Date & Time: Mar 2, 1977 at 1208 LT
Type of aircraft:
Operator:
Registration:
N8066Q
Flight Phase:
Survivors:
No
Schedule:
Billings - Phoenix
MSN:
414-0501
YOM:
1974
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
11500
Circumstances:
While in cruising altitude, the twin engine airplane entered an uncontrolled descent and crashed in flames near Farson. The pilot, sole on board, was killed.
Probable cause:
Airframe failure in flight and uncontrolled descent caused by the pilot exceeded designed stress limits of aircraft. The following contributing factors were reported:
- Overload failure,
- Separation in flight,
- Wings, empennage separated.
Final Report: