Crash of a Beechcraft 200 Super King Air in Wernadinga Station: 8 killed

Date & Time: Sep 4, 2000 at 1510 LT
Operator:
Registration:
VH-SKC
Flight Phase:
Survivors:
No
Schedule:
Perth - Leonora
MSN:
BB-47
YOM:
1975
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
2053
Captain / Total hours on type:
138.00
Aircraft flight hours:
18771
Circumstances:
On 4 September 2000, a Beech Super King Air 200 aircraft, VH-SKC, departed Perth, Western Australia at 1009 UTC on a charter flight to Leonora with one pilot and seven passengers on board. Until 1032 the operation of the aircraft and the communications with the pilot appeared normal. However, shortly after the aircraft had climbed through its assigned altitude, the pilot’s speech became significantly impaired and he appeared unable to respond to ATS instructions. Open microphone transmissions over the next 8-minutes revealed the progressive deterioration of the pilot towards unconsciousness and the absence of any sounds of passenger activity in the aircraft. No human response of any kind was detected for the remainder of the flight. Five hours after taking off from Perth, the aircraft impacted the ground near Burketown, Queensland, and was destroyed. There were no survivors.
Probable cause:
Due to the limited evidence available, it was not possible to draw definitive conclusions as to the factors leading to the incapacitation of the pilot and occupants of VH-SKC.
The following findings were identified:
1. The pilot was correctly licensed, had received the required training, and there was no evidence to suggest that he was other than medically fit for the flight.
2. The weather conditions on the day presented no hazard to the operation of the aircraft on its planned route.
3. The flightpath flown was consistent with the aircraft being controlled by the autopilot in heading and pitch-hold modes with no human intervention after the aircraft passed position DEBRA.
4. After the aircraft climbed above the assigned altitude of FL250, the speech and breathing patterns of the pilot, evidenced during the radio transmissions, displayed changes consistent with hypoxia.
5. Testing revealed that Carbon Monoxide and Hydrogen Cyanide were highly unlikely to have been factors in the occurrence.
6. The low Carbon Monoxide and Cyanide levels, and the absence of irritation in the airways of the occupants indicated that a fire in the cabin was unlikely.
7. The incapacitation of the pilot and passengers was probably due to hypobaric hypoxia because of the high cabin altitude and their not receiving supplemental oxygen.
8. A rapid or explosive depressurisation was unlikely to have occurred.
9. The reasons for the pilot and passengers not receiving supplemental oxygen could not be determined.
10. Setting the visual alert to operate when the cabin pressure altitude exceeds 10,000 ft and incorporating an aural warning in conjunction with the visual alert, may have prevented the accident.
11. The training and actions of the air traffic controller were not factors in the accident.
Significant factors:
1. The aircraft was probably unpressurised for a significant part of its climb and cruise for undetermined reasons.
2. The pilot and passengers were incapacitated, probably due to hypobaric hypoxia, because of the high cabin altitude and their not receiving supplemental oxygen.
Final Report:

Crash of a Beechcraft 70 Queen Air in Leonora

Date & Time: Jun 24, 2000 at 1740 LT
Type of aircraft:
Registration:
VH-MWJ
Flight Phase:
Survivors:
Yes
Schedule:
Leonora – Laverton
MSN:
LB-29
YOM:
1970
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The Beechcraft Queen Air and Rockwell Aero Commander were being used by a company to conduct private category passenger-carrying flights to transport its workers from Leonora to Laverton in Western Australia. The Aero Commander had departed and was established in the Leonora circuit area when the Queen Air took off. The pilot and one of the passengers of the Queen Air reported the take-off roll appeared normal until the aircraft crossed the runway intersection, when they felt a bump in the aircraft. The pilot reported hearing a loud bang and noticed that the inboard cowl of the right engine had opened. He also reported that he believed he had insufficient runway remaining to stop safely, so he continued the takeoff. The cowl separated from the aircraft at the time, or just after the pilot rotated the aircraft to the take-off attitude. He reported that although the aircraft had left the ground after the rotation, it then would not climb. The aircraft remained at almost treetop level until the pilot and front-seat passenger noticed the side of a tailings dump immediately in front of the aircraft. The pilot said that he pulled the control column fully back. The aircraft hit the hillside parallel to the slope of the embankment, with little forward speed. The impact destroyed the aircraft. Although the occupants sustained serious injuries, they evacuated the aircraft without external assistance. There was no post-impact fire. The aircraft-mounted emergency locator transmitter (ELT) did not activate.
Probable cause:
The examination of the Queen Air wreckage found no mechanical fault that may have contributed to the accident sequence other than the inboard cowl of the right engine detaching during the takeoff. The cowl latching mechanisms appeared to have been capable of operating normally. The two top hinges failing in overload associated with the lack of cowl latch damage suggested that the cowl was probably improperly secured before takeoff. The cowl appeared to have subsequently opened when it experienced the jolt when the aircraft crossed the runway intersection. The lack of any further cowl damage indicated that it detached cleanly and consequently its dislodgment should not have adversely affected the flying qualities of the aircraft.
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601P) in Teutonic Bore: 1 killed

Date & Time: May 28, 1980 at 1137 LT
Operator:
Registration:
VH-KXY
Flight Phase:
Survivors:
Yes
Schedule:
Teutonic Bore – Leonora – Perth
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2810
Captain / Total hours on type:
149.00
Circumstances:
The aircraft was engaged on the return segment of a flight from Perth to Teutonic Bore, with an intended refuelling stop at Leonora. After embarking the two passengers and their baggage, the pilot started the engines and taxied for a take-off into the north, on the 1350 metre long main strip. The weather conditions were fine with a northerly surface wind of about 7 knots. The initial part of the take-off run was apparently normal but, after travelling some 400 metres and at about the point of rotation, one of the passengers noted an engine power surge. The take-off was continued, the aircraft became airborne and shortly afterwards the landing gear was retracted. After the aircraft had slowly climbed straight ahead to an altitude of about 200-300 feet above ground level, the passenger heard a marked change in the engine noise and felt the aircraft decelerating. The extent of the power loss and the absence of any yawing force indicated both engines had lost power simultaneously. Level flight straight ahead was reportedly maintained for an estimated 10 seconds and then the aircraft entered a descending left turn. At about this time the pilot, in response to a query from the passenger, advised that he intended to return to the airstrip but then stated "we're going down", or words to that effect. The terrain in the area was generally firm and flat. It was lightly covered with scrub and there was occasional small trees but a safe landing with only minimal damage was possible. When VH-KXY struck the ground the gear and flaps were retracted and the rate of descent was high. The aircraft was in a level attitude but yawed approximately 45 degrees to the right. After the initial impact, the aircraft slid across the ground on a track of 220 degrees magnetic for 67 metres before coming to rest. There was no post-impact fire. One passenger was able to exit via the cabin door by his own efforts. The other occupants were trapped in the wreckage and were rescued some 30 minutes later by persons who attended the accident. The pilot died shortly after being removed from the aircraft.
Probable cause:
The probable cause of the accident was that, following a substantial loss of power by both engines, the pilot did not carry out the procedures necessary for a safe forced landing. The cause of the loss of power by both engines has not been determined.
Final Report: