Crash of a Hawker 900XP near Bitter Creek: 2 killed

Date & Time: Feb 7, 2024 at 1047 LT
Type of aircraft:
Operator:
Registration:
N900VA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Grand Junction - Tacoma
MSN:
HA-0020
YOM:
2007
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The airplane departed Grand Junction Airport at 1037LT on a positioning flight to Tacoma, carrying a crew of two. About 10 minutes later, it entered an uncontrolled descent and crashed in a uninhabited area located near the Bitter Creek River, eastern Utah, near the border with Colorado. The airplane was destroyed by impact forces and a post crash fire and the wreckage was found about 17 km west northwest from the Mack-Mesa Airport located in Colorado. Both occupants were killed.

Crash of a Learjet 35A in McMinville

Date & Time: May 13, 2013 at 1245 LT
Type of aircraft:
Operator:
Registration:
N22MS
Flight Type:
Survivors:
Yes
Schedule:
Grand Junction - McMinville
MSN:
209
YOM:
1978
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
17563
Captain / Total hours on type:
996.00
Copilot / Total flying hours:
2553
Copilot / Total hours on type:
94
Aircraft flight hours:
15047
Circumstances:
The crew of the twinjet reported that the positioning flight after maintenance was uneventful. However, during the landing roll at their home base, the thrust reversers, steering, and braking systems did not respond. As the airplane approached the end of the runway, the pilot activated the emergency braking system; however, the airplane overran the end of the runway, coming to rest in a ditch. None of the three occupants were injured, but the airplane sustained substantial damage to both wings and the fuselage. Two squat switches provided redundancy within the airplane’s electrical system and were configured to prevent inadvertent activation of the thrust reversers and nosewheel steering during flight and to prevent the airplane from landing with the brakes already applied. Because postaccident examination revealed that the squat switch assemblies on the left and right landing gear struts were partially detached from their mounting pads such that both switches were deactivated, all of these systems were inoperative as the airplane landed. The switch assemblies were undamaged, and did not show evidence of being detached for a long period of time. The brakes and steering were working during taxi before departure, but this was most likely because either one or both of the switches were making partial contact at that time. Therefore, it was most likely that the squat switch assemblies were manipulated on purpose during maintenance in an effort to set the airplane’s systems to “air mode.” Examination of the maintenance records did not reveal any recent procedures that required setting the airplane to air mode, and all mechanics involved in the maintenance denied disabling the switches. Mechanics did, however, miss two opportunities to identify the anomaly, both during the return-to-service check and the predelivery aircraft and equipment status check. The anomaly was also missed by the airplane operator’s mechanic and flight crew who performed the preflight inspection. The airplane’s emergency braking system was independent of the squat switches and appeared to operate normally during a postaccident test. Prior to testing, it was noted that the emergency brake gauge indicated a full charge; therefore, although evidence suggests that the emergency brake handle was used, it was not activated with enough force by the pilot. The pilot later conceded this fact and further stated that he should have used the emergency braking system earlier during the landing roll. The airplane was equipped with a cockpit voice recorder (CVR), which captured the entire accident sequence. Analysis revealed that the airplane took just over 60 seconds to reach the runway end following touchdown, and, during that time, two attempts were made by the pilot to activate the thrust reversers. The pilot stated that as the airplane approached the runway end, the copilot made a third attempt to activate the thrust reversers, which increased the engine thrust, and thereby caused the airplane to accelerate. Audio captured on the CVR corroborated this statement.
Probable cause:
Failure of maintenance personnel to reattach the landing gear squat switches following maintenance, which rendered the airplane's steering, braking, and thrust reverser systems inoperative during landing. Contributing to the accident were the failure of both the maintenance facility mechanics and the airplane operator's mechanic and flight crew to identify the error during postmaintenance checks, a failure of the airplane's pilot to apply the emergency brakes in a timely manner, and the copilot's decision to attempt to engage the thrust reversers as the airplane approached the runway end despite multiple indications that they were inoperative and producing partial forward, rather than reverse, thrust.
Final Report:

Crash of a Cessna 425 Conquest I in Canadian

Date & Time: Mar 28, 2011 at 0825 LT
Type of aircraft:
Operator:
Registration:
N410VE
Flight Type:
Survivors:
Yes
Schedule:
Grand Junction - Canadian
MSN:
425-0097
YOM:
1981
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
22500
Captain / Total hours on type:
1000.00
Aircraft flight hours:
7412
Circumstances:
While on a straight-in global-positioning-system approach, the airplane broke out of the clouds directly over the end of the runway. The pilot then remained clear of the clouds and executed a no-flap circling approach to the opposite direction runway. The pilot said that his airspeed was high when he touched down. The landing was hard, and the right main landing gear tire blew out, the airplane departed the runway to the left, and the left main landing gear collapsed. No preaccident mechanical malfunctions or failures were found that would have precluded normal operation.
Probable cause:
The pilot’s continuation of the approach with excessive airspeed, which resulted in a hard landing and a loss of directional control.
Final Report:

Crash of a Cessna 560 Citation Encore at Miramar NAS: 4 killed

Date & Time: Mar 10, 2004 at 2042 LT
Type of aircraft:
Operator:
Registration:
165938
Flight Type:
Survivors:
No
Schedule:
Grand Junction - Miramar
MSN:
560-0567
YOM:
2000
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The crew was returning to Miramar NAS following a routine training mission in Grand Junction. On final approach to Miramar NAS by night, the aircraft crashed near the interstate 15, about 2,400 metres short of runway 24R. The aircraft was destroyed and all four occupants were killed. A weather observation taken from the base at 2045LT reported five-mile visibility with light fog or haze, and a cloud ceiling at 800 feet.
Crew:
Lt Col T. Nicholson,
Lt Col Robert Zeisler.
Passengers:
Sgt Francisco Cortez,
Cpl Jeremy Lindroth.

Crash of a Swearingen SA226TC Metro II in Grand Junction

Date & Time: Nov 18, 2003 at 0721 LT
Type of aircraft:
Operator:
Registration:
N332BA
Flight Type:
Survivors:
Yes
Schedule:
Rifle – Grand Junction
MSN:
TC-222E
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2419
Captain / Total hours on type:
140.00
Aircraft flight hours:
23972
Circumstances:
According to the pilot, he was told to enter left base and was cleared to land. The pilot stated that, when he reduced the airspeed to lower the landing gear, he "heard the gear come down," and he verified "three green in the [landing] gear indicator." He landed the airplane on its "main [landing gear] wheels first" and slowly let the nose of the airplane drop. Although both main landing gear assemblies remained down and locked, the nose landing gear collapsed, allowing the nose of the airplane and both propellers to strike the runway. The airplane slid approximately 3,000 feet, coming to a stop on the right edge of the runway. Several fractured propeller pieces impacted the left and right sides of the fuselage substantially damaging two fuselage station bulkheads. The fuselage bulkhead, forward of the nose landing gear well, was also substantially damaged due to contact with the runway. The pilot said that, during the approach, from base to final, he did not hear a landing gear warning horn. An air traffic control specialist, stated that he told the pilot to enter a left base and that he was cleared to land. The specialist stated that he observed the airplane roll out on a 2-mile final "with the gear down." As the airplane was rolling down the runway the "nose wheel collapsed." An FAA inspector examined the airplane and noted that, according to the Fairchild SA226 Maintenance Manual, the nose landing gear's up-lock mechanism was not properly lubricated, a "critical clearance" measurement between the nose landing gear's bell crank roller and positioning cam was found to be out of tolerance, and when the throttles were retarded, the landing gear warning horn activated, but it was "barely audible." According to the Fairchild SA226 Maintenance Manual, the landing gear should be lubed every 200 hours. The FAA inspector stated that the approved maintenance inspection sheet for the operator, did not show the requirement for the main landing gear or nose landing gear to be lubed every 200 hours.
Probable cause:
The operator's improper maintenance and servicing of the airplane's nose landing gear assembly, resulting in the collapse of the nose landing gear during the landing roll. Contributing factors include the nose section of the airplane's subsequent contact with the runway, the impact of several fractured propeller pieces into the fuselage, and the operator's inadequate maintenance and servicing procedures.
Final Report:

Crash of a Beechcraft E90 King Air in Kremmling

Date & Time: Mar 19, 2003 at 1930 LT
Type of aircraft:
Operator:
Registration:
N711TZ
Flight Type:
Survivors:
Yes
Schedule:
Grand Junction – Kremmling
MSN:
LW-226
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10564
Captain / Total hours on type:
212.00
Aircraft flight hours:
8040
Circumstances:
The pilot reported that he maneuvered for a left hand downwind leg for landing from the east to west. The pilot set up his downwind leg at 8,400 feet mean sea level putting him at what would have been 1,000 feet above the airport elevation of 7,411 feet. The pilot reported it was very dark and he could see the airport, but could not see the terrain. The pilot reported that suddenly he saw the ground. The airplane impacted the terrain and came to rest. The pilot reported that the airplane was experiencing no malfunctions prior to the accident. The airplane accident site was on the snow-covered edge of a mountain ridge at an elevation of 8,489 feet. An examination of the airplane's systems revealed no anomalies. Published terminal procedures for the runway indicated high terrain of 8,739 feet south-southeast of the airport. The published airport diagram for the airport directs right traffic for the pattern to runway 27.
Probable cause:
The pilot's improper in-flight planning and his failure to maintain safe clearance from the high terrain. Factors contributing to the accident were the high terrain and the dark night.
Final Report:

Crash of a Piper PA-42 Cheyenne III in Grand Junction: 3 killed

Date & Time: Oct 31, 1992 at 0815 LT
Type of aircraft:
Operator:
Registration:
N250TJ
Survivors:
No
Schedule:
Moab - Grand Junction
MSN:
42-8001024
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
4700
Aircraft flight hours:
4784
Circumstances:
The commuter air carrier departed Moab, Utah, and flew to Grand Junction, CO, via rnav direct Macks intersection. After crossing macks intersection, the airplane turned right but instead of intercepting the localizer course, the airplane continued on a slightly divergent track to the east of the localizer. The pilot told control tower personnel, 'I'm showing twelve miles out on the ILS...getting real...erroneous signal, here. Any complaints?' the pilot was advised no difficulty reports had been received. The airplane impacted a mesa one minute later about five miles to the left of the localizer course. The cockpit was destroyed and no meaningful information was obtained from the navigational radios. All of the airport's navigational aids were later flight checked and no discrepancies were found. Although Vmc prevailed at the airport, the accident site was above the reported ceiling height. All three occupants were killed.
Probable cause:
Improper ifr procedure and resultant disorientation which resulted in a collision with terrain.
Final Report:

Crash of a Swearingen SA26T Merlin II in Glenwood Springs

Date & Time: Feb 13, 1992 at 2055 LT
Type of aircraft:
Registration:
N26JB
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Grand Junction - Denver
MSN:
T26-163
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8600
Captain / Total hours on type:
750.00
Aircraft flight hours:
3988
Circumstances:
The pilot of the air ambulance feathered the right propeller after reporting 'a bit of a problem' with the right engine. He attempted to divert to the nearest suitable airport, but after receiving its latest weather report, elected to return to base. The airplane made a left turn, reentered IMC, and impacted a mountainside on a magnetic heading of 092°. The heading to the airport of intended landing was 272°. The accident occurred during a snowstorm at night. All five occupants survived and were rescued the following afternoon. Thick grease on the right engine fuel control camshaft prevented a spring from returning the 3d cam to a lower altitude position. The cam was found struck on the shaft at a position equating to an altitude of approximately 15,000 feet. The fuel flow schedule for flight idle was below specifications. In addition, shroud material was found delaminated from the left engine second stage compressor housing.
Probable cause:
Malfunction of the right engine fuel control that caused the engine to flame out, and delamination of the left engine compressor shroud. Factors were: the pilot became disoriented, the mountainous terrain, the dark night, and the weather conditions.
Final Report:

Crash of a Cessna 340A near Crawford: 5 killed

Date & Time: Sep 25, 1986 at 1740 LT
Type of aircraft:
Registration:
N6663G
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Gunnison – Grand Junction
MSN:
340A-0693
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
2241
Captain / Total hours on type:
1420.00
Aircraft flight hours:
1560
Circumstances:
The pilot took off on a VFR flight with no flight plan filed or weather briefing. He encountered a weather squall line en route with low ceilings, fog, mixed rain and snow. While he was attempting to maneuver VFR through the weather at a low altitude above the ground, the aircraft entered clouds and impacted terrain at 7,500 feet msl in mountainous terrain. All five occupants were killed.
Probable cause:
Occurrence #1: in flight encounter with weather
Phase of operation: maneuvering
Findings
1. (f) weather condition - low ceiling
2. (f) weather condition - fog
3. (f) weather condition - rain
4. (f) weather condition - snow
5. (f) terrain condition - mountainous/hilly
6. (c) preflight planning/preparation - inadequate - pilot in command
7. (c) hazardous weather advisory - not obtained - pilot in command
8. (c) vfr flight into imc - inadvertent - pilot in command
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: maneuvering
Findings
9. (c) in-flight planning/decision - improper - pilot in command
10. (c) proper altitude - not maintained - pilot in command
Final Report:

Crash of a Piper PA-31-310 Navajo in Paonia: 1 killed

Date & Time: Sep 28, 1984 at 0830 LT
Type of aircraft:
Registration:
N7205L
Flight Type:
Survivors:
No
Site:
Schedule:
Grand Junction - Paonia
MSN:
31-716
YOM:
1971
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
25587
Captain / Total hours on type:
1960.00
Aircraft flight hours:
9321
Circumstances:
The aircraft was flying at a very low altitude over mountainous terrain. As the aircraft approached a crest of a ridge the aircraft started to buffet and then encountered a downslope wind condition. The combination of approaching a stall and encountering a downdraft forced the aircraft into trees. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: in flight collision with object
Phase of operation: maneuvering
Findings
1. (f) object - tree(s)
2. (f) weather condition - downdraft
3. (c) proper altitude - not maintained - pilot in command
4. (c) proper climb rate - not attained - pilot in command
----------
Occurrence #2: loss of control - in flight
Phase of operation: maneuvering
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Findings
5. (f) terrain condition - mountainous/hilly
Final Report: