Crash of a BAe 3102 Jetstream 31 in Wick

Date & Time: Sep 17, 2003 at 1447 LT
Type of aircraft:
Operator:
Registration:
G-EEST
Survivors:
Yes
Schedule:
Aberdeen – Wick
MSN:
781
YOM:
1987
Location:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7885
Captain / Total hours on type:
1195.00
Copilot / Total flying hours:
6800
Copilot / Total hours on type:
1000
Aircraft flight hours:
17845
Aircraft flight cycles:
20730
Circumstances:
The aircraft was landing on Runway 31 at Wick Airport. It crossed the threshold at 130 kt which was 21 kt faster than the correct threshold speed. After the co-pilot closed the power levers the aircraft floated about six feet above the runway surface. The aircraft touched down and bounced before touching down a second time more heavily, cracking a wing spar and flexing the aircraft structure sufficient to allow the right propeller to contact the runway. The aircraft bounced again before touching down for the third and final time. The investigation determined that just before the first touchdown, one or both power levers were moved aft of the flight idle position. It was concluded that both the commander and co-pilot were making inputs on the flying controls from that moment onwards until after the second, heavy touchdown. There was no evidence of any technical fault on the aircraft and the weather conditions were well within the limitations set for the aircraft. No safety recommendations were made.
Probable cause:
It is reasonable to conclude that the manoeuvres conducted by G-EEST during the landing were the result of combined control inputs made by the commander and co-pilot. The evidence indicates that this period of combined control started at least 0.28 seconds before the first touchdown and finished at some stage after the second and damaging touchdown. After the first touchdown the aircraft became airborne in a high-drag, low-lift configuration which was intended for ground operation only and a 5.6g impact ensued on the second touchdown. There was no evidence of any technical fault on the aircraft that could have been a factor and the meteorological conditions were within the limitations set for the aircraft. A more complete understanding of the accident might have been possible with additional flight data parameters such as engine performance, aircraft pitch, and power lever position.
Final Report:

Crash of a Swearingen SA227AC Metro III in Aberdeen

Date & Time: Dec 24, 2002 at 0745 LT
Type of aircraft:
Operator:
Registration:
OY-BPH
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Aberdeen - Aalborg
MSN:
AC-580B
YOM:
1984
Flight number:
NFA924
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4600
Captain / Total hours on type:
2800.00
Circumstances:
At approximately 0630 hrs on 24 December 2002, the pilots arrived by car at Aberdeen Airport. With no requirement for their aircraft to transport mail on this occasion, it was decided to fly directly to their home airport in Denmark. The aircraft had been refuelled the previous day and the total fuel on board of 2,200 lb was sufficient for the flight; with no cargo on board, take-off weight was calculated as 12,000 lb (maximum take-off weight: 16,000 lb). The commander carried out an external inspection on OY-BPH while the co-pilot, who was the designated handling pilot for the flight to Denmark, submitted a flight plan. The weather at 0720 hrs was reported as follows: Surface wind 150°M/ 12 kt; visibility 2,500 metres in mist; cloud scattered 100 feet agl, overcast at 200 feet agl; air temperature +9°C; QNH 994 hPa. The runway was reported as wet and Low Visibility Procedures (LVP) had been in force at Aberdeen since 0633 hrs. OY-BPH, callsign 'Birdie Nine Two Four', was parked on Taxiway Bravo and the crew called for, and were given, start clearance at 0736 hrs by 'Ground Movement Control' on frequency 121.7 MHz. Then, following their after-start checks, the crew were cleared to taxi to 'Whiskey Five' for Runway 16 at 0740 hrs. During taxi, the crew were passed and correctly acknowledged the following clearance: "LEAVE CONTROLLED AIRSPACE CLIMBING FLIGHT LEVEL ONE FIVE FIVE SQUAWK SIX TWO FOUR ZERO". Then, at 0742 hrs as the aircraft approached 'Whiskey Five', the crew were transferred to 'Aberdeen Tower' on frequency 118.1 MHz. On the 'Tower' frequency, they were given line-up clearance for Runway 16. At 0743 hrs, the controller transmitted: "BIRDIE NINE TWO FOUR WITH A LEFT TURN DIRECT KARLI CLEAR TAKE OFF ONE SIX SURFACE WIND ONE SIX ZERO ONE TWO KNOTS". The crew correctly acknowledged this clearance. The controller watched the initial movement of the aircraft along the runway before transferring her attention to another aircraft, which was lining up. Shortly after, at 0746 hrs, she transmitted: "OY-BPH REPORT TURNING LEFT" but received no reply. About this time, a telephone message was received in the 'Tower' from a witness in front of the Terminal Building to the effect that an aircraft appeared to have crashed just south of the airfield. This witness had heard a "change in pitch" from the aircraft but had seen no flames prior to it disappearing from his sight: ATC personnel immediately activated their emergency procedures. For the reduced power take-off roll, with the flaps at ¼, the power was set by the commander. The crew considered that the performance of the aircraft was normal, with no unusual instrument indications. The calculated V1 and VR speeds (co-incident at 100 kt) were achieved and called by the commander and, at VR, the co-pilot rotated the aircraft to a pitch attitude of about 12° to 15° nose-up. As the aircraft left the ground, the co-pilot detected the aircraft 'yawing' to the right; almost immediately, he was also aware of a distinct smell of smoke. He called to the commander that he had an engine failure, called for maximum power and tried to maintain control by corrective aileron and rudder inputs. The commander felt the aircraft roll about 15° to the right and realised that there was a problem with the right (No 2) engine. He reached for both power levers and moved them forward. There were no audio or visual warnings associated with the apparent problem. The commander looked at the EGT gauges with the power levers fully forward and noted that the No 2 engine indicated about 600°C EGT, whereas the left (No 1) engine indicated greater than 650°C EGT (the normal maximum) and that its fuel 'Bypass' light was on. He retarded the No 1 power lever until the 'Bypass' light extinguished and noted the resultant EGT at about 630°C. He did not recall any other abnormal indications on the engine instruments but, later in the investigation, the commander recalled hearing a sound "like a compressor stall from the right engine". About this time, the co-pilot heard the automatic "Bank Angle" voice activate. As the aircraft continued to turn to the right, the co-pilot called that he "couldn't control the aircraft". The commander reached for and pulled No 2 engine 'Stop and Feather Control' but, almost immediately, OY-BPH struck the ground initially with the right wing. The aircraft slid along the surface of a field, through a fence and onto a road, before coming to rest. As it did so, the co-pilot was aware that the aircraft had struck a car, which was now at rest outside the right forward side of the cockpit. The co-pilot saw that the whole of the right wing was on fire and called this to the commander before evacuating out of the left door of the aircraft. As the copilot left, the commander pulled No 1 engine 'Stop and Feather Control' and activated both engine fire extinguishers before leaving the aircraft. Outside OY-BPH, the co-pilot went to the car to check if anyone was still inside; as he did so, he saw someone running away. With the intense fire and the car apparently empty, both pilots moved well away from the aircraft. At 0748 hrs, the co-pilot used his mobile phone to advise ATC of the accident and to request assistance. The local emergency services had been alerted at 0745 hrs by a member of the public, who reported a road accident; by 0753 hrs, the local fire service was on the scene. By 0754 hrs, the first AFS vehicle was on the scene and three further AFS vehicles arrived one minute later. A fifth vehicle arrived at 0800 hrs. The fire was quickly extinguished and the Fire Officer confirmed that all the aircraft and vehicle occupants had been located and that there had been no serious injuries. Following runway and taxiway inspections, the airport was re-opened at 0954 hrs.
Probable cause:
Although the investigation was hampered by the lack of FDR data, which might have provided information on engine handling and behaviour, the available evidence from the crew and the initial examination of the aircraft at the accident site, pointed to a major loss of power in the right engine. As a result of the discovery of dead birds close to the point of lift-off on the runway, and a section of braided wire found near the start of the take-off roll, consideration was given as to whether the these had been factors in the accident. The braided wire was not identified as having originated from OY-BPH. There was conclusive evidence that the left engine, which had continued to run, had ingested parts of birds, but no such evidence was found with the right engine. Nevertheless, the crew were adamant that there was a power loss from the right engine and were not conscious of any power reduction from the left engine. The technical examination of the left engine and its propeller assembly revealed evidence of damage consistent with this unit delivering a high level of power at impact. The examination of the right engine and propeller revealed all damage to be consistent with a low, or no, power condition at impact, consistent with either a genuine loss of power or as a consequence of the commander pulling the 'Stop and Feather' control immediately before impact. However, an exhaustive examination of the right engine revealed no evidence of anything that could have caused a failure. Therefore, the items found on the runway were not considered to have been causal or contributory factors in the accident. The crew's recollection of the event included a low EGT indication, at 600°C. This suggested that either the engine might have flamed out, should they have only momentarily looked at the indication as the engine was cooling down, or that the engine was operating at reduced power for an undetermined reason. Flame out could have occurred due to a number of reasons, including, for example, water contamination of the fuel. However, analysis of the bulk supply samples proved negative and, moreover, there were no reports of contaminated fuel from other operators at Aberdeen Airport. Ingestion of ice or water could also have resulted in a flame-out, although this is considered unlikely due to the conditions not being conducive to the formation of engine icing, the lack of significant standing water on the runway, and the absence of heavy precipitation. However, it could not be completely discounted and, if flame-out had occurred, the non-incorporation of the FAA mandated auto-relight system would have reduced the possibility of an immediate relight. Approximately six months before the accident, the left engine had failed during a landing roll-out whilst the aircraft was being operated in Spain. This failure was never satisfactorily explained although, at one stage, the fuel cut-off valve came under suspicion. The valves were interchanged, according to the records, so that the unit that had been fitted to the left engine was installed on the right engine, at the time of the accident. Whilst a stray electrical signal causing the valve to close would certainly result in the engine flaming out, rumours that such events had occurred were not substantiated by the engine manufacturer. In summary, the left engine experienced a bird strike, but with no apparent power loss, and the extensive technical examination could not identify any reason for a loss of power on the right engine. Although an engine failure during takeoff after V1 is a serious emergency, the aircraft was at a relatively light weight and, even with an such a failure, the crew should have been able to fly OYBPH safely away. However, if other factors had been involved, the margins for safe flight would have become more critical. These other factors could have included incorrect operation of the NTS system and/or a failure of the feathering system on the right engine, a concurrent power loss from the left engine, or the crew not handling the emergency effectively. There is no doubt that the left engine had been producing power at impact, but a definite conclusion could not be made as to the blade pitch angles of the right propeller. From the evidence of the commander and the propeller examination by the manufacturer, it is probable that the right propeller was close to the feather position at ground impact. The functionality of the NTS and feathering system could not be determined but, as noted earlier, the pre-flight NTS check actually only ensured that oil pressure was available for this system, and did not check the operation of the whole system. With the evidence that only the left engine had ingested birds, there was a possibility that the left engine was not producing maximum power, although the crew considered it was operating normally. The commander could remember that he compared the engine EGT indications, once he had pushed both power levers forward, and recalled that the left EGT was indicating greater than 650°C with the 'Bypass' light on. He then retarded the left power lever until the 'Bypass' light went out, following which the EGT indicated about 630°C. This retardation of the power lever was not required, as the function of the 'Bypass' system is to reduce the fuel flow in order to keep the engine parameters within limits. This reported retardation could, however, have resulted in a lower engine power than was possible within the available limits, possibly with an associated reduction in EGT. While it remains a possibility that the left engine may have experienced a transient power reduction as a result of the bird ingestion, it is likely that the commander's action in retarding the left power lever resulted in a more significant reduction of power. To maintain straight flight, following an engine failure, it is vital to apply sufficient corrective rudder input to maintain the wings essentially level and minimise the drag due to sideslip. In the case of OYBPH, there was a constant turn to the right before ground impact. The commander's recollection was that left rudder had been applied by the co-pilot, but not to full deflection. The amount of rudder deflection required depends mainly on the airspeed and the difference in engine power but, with the wings not level, more deflection was obviously required, and was available. Greater use of rudder would have reduced the overall drag of the aircraft, with consequent improvement in the aircraft's performance. Furthermore, following an engine failure, the second segment climb requirement is to climb from 35 feet to 400 feet at V2 with the landing gear selected to up. The commander did not raise the gear because he did not observe a positive rate of climb. However, evidence from the FDR was that a maximum airspeed of 128 kt was achieved and, as this was some 19 kt higher than the V2 speed, it indicated that the aircraft had a capability to climb which was not being used. These last three factors may have combined to reduce the climb capability of the aircraft to zero and, in that situation, the decision to not raise the gear was correct. However, all these factors were influenced by inappropriate crew actions. Although both pilots had flown together before, the lack of adherence to JAR-OPS conversion requirements may have been partly responsible for their actions during the emergency.
Final Report:

Crash of a Cessna 404 Titan II in Glasgow: 8 killed

Date & Time: Sep 3, 1999 at 1236 LT
Type of aircraft:
Registration:
G-ILGW
Flight Phase:
Survivors:
Yes
Schedule:
Glasgow – Aberdeen
MSN:
404-0690
YOM:
1980
Flight number:
Saltire 3W
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
4190
Captain / Total hours on type:
173.00
Copilot / Total flying hours:
2033
Copilot / Total hours on type:
93
Aircraft flight hours:
6532
Circumstances:
The aircraft had been chartered to transport an airline crew of nine persons from Glasgow to Aberdeen. The aircraft was crewed by two pilots and, so far as could be determined, its take-off weight was between 8,320 and 8,600 lb. The maximum permitted take-off weight was 8,400 lb. ATC clearance for an IFR departure was obtained before the aircraft taxied from the business aviation apron for take-off from runway 23, with a take-off run available of 2,658 metres. According to survivors, the take-off proceeded normally until shortly after the aircraft became airborne when they heard a thud or bang. The aircraft was then seen by external witnesses at low height, to the left of the extended runway centerline, in a wings level attitude that later developed into a right bank and a gentle descent. Witnesses reported hearing an engine spluttering and saw at least one propeller rotating slowly. There was a brief 'emergency' radio transmission from the commander and the aircraft was seen entering a steep right turn. It then entered a dive. A witness saw the wings levelled just before the aircraft struck the ground on a northerly track. Three survivors were helped from the wreckage by a nearby farm worker before flames from a severe post-impact fire engulfed the cabin.
Probable cause:
The following causal factors were identified:
- The left engine suffered a catastrophic failure of its accessory gear train leading to a progressive but complete loss of power from that engine,
- The propeller of the failed engine was not feathered and therefore the aircraft was incapable of climbing on the power of one engine alone,
- The commander feathered the propeller of the right-hand engine, which was mechanically capable of producing power resulting in a total loss of thrust,
- The commander attempted to return to the departure airfield but lost control of the aircraft during a turn to the right.
Final Report:

Crash of a Fairchild-Hiller FH-227B in Keflavik

Date & Time: Jul 26, 1998 at 2355 LT
Type of aircraft:
Operator:
Registration:
N564LE
Flight Type:
Survivors:
Yes
Schedule:
Billund - Aberdeen - Keflavik
MSN:
564
YOM:
1967
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On final approach, when the landing gears were extended, the crew heard loud cracking noise. The landing was aborted and the aircraft passed the tower for visual inspection and one of the crew went to the cabin for visual check of the landing gears where he observed that the right landing gear lock strut rear member had broken loose from the side member assembly and was hanging down. Upon touchdown the gear folded up and the aircraft right propeller, wing tip and bottom of the fuselage touched ground and the aircraft went off the runway in a gentle right turn. The fuselage bottom skin and frame structure sustained extensive damage and the right wing tip, propeller blades, lock strut assembly and drag strut were destroyed. The aircraft operated on a ferry flight from Billund, Denmark to Miami-Opa Locka, Florida, with en route stops at among others Aberdeen and Keflavík.
Probable cause:
Preliminary investigation revealed that no lubricant was found in the lock strut hinge pin that should normally be packed with grease.

Crash of an Embraer EMB-110P1 Bandeirante near Leeds: 12 killed

Date & Time: May 24, 1995 at 1751 LT
Operator:
Registration:
G-OEAA
Survivors:
No
Schedule:
Leeds - Aberdeen
MSN:
110-256
YOM:
1980
Flight number:
NE816
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
12
Captain / Total flying hours:
3257
Captain / Total hours on type:
1026.00
Copilot / Total flying hours:
302
Copilot / Total hours on type:
46
Aircraft flight hours:
15348
Circumstances:
On the morning of 24 May 1995 the aircraft had returned to its base at Leeds/Bradford from Aberdeen, U.K. on a scheduled passenger flight landing at 09:44 local time. The crew, which was not the one later involved in the accident, stated that all of the aircraft's systems and equipment had been serviceable during the flight. Some routine maintenance was performed on the aircraft which was later prepared for a scheduled passenger flight, NE816, to Aberdeen. It was positioned at the passenger terminal where it was taken over by the crew which was to operate the service, comprising the commander, who occupied the left hand seat, the first officer and a flight attendant. Nine passengers were boarded. The weather at Leeds/Bradford Airport was poor with Runway Visual Range (RVR) reported as 1,100 metres; scattered cloud at 400 feet above the aerodrome elevation of 682 feet and a light south-easterly wind. It was raining and the airfield had recently been affected by a thunderstorm. The freezing level was at 8,000 feet and warnings of strong winds and thunderstorms were in force for the Leeds/Bradford area. The crew called ATC for permission to start the engines at 17:41 hrs. Having backtracked the runway to line up, the aircraft took-off from runway 14 at 17:47 hrs and the crew was instructed by ATC to maintain the runway heading (143°M). The aircraft began to turn to the left shortly after becoming airborne. One minute and fifty seconds after the start of the take-off roll and as the aircraft was turning through a heading of 050° and climbing through 1,740 feet amsl, the first officer transmitted to Leeds/Bradford aerodrome control: "Knightway 816 we've got a problem with the artificial horizon sir and we'd like to come back." The aerodrome controller passed instructions for a radar heading of 360° and cleared the aircraft to 3,000 feet QNH. These instructions were read back correctly but the aircraft continued its left turn onto 300° before rolling into a right hand turn with about 30° of bank. About 20 seconds before this turn reversal, the aircraft had been instructed to call the Leeds/Bradford approach controller. The aircraft was now climbing through an altitude of 2,800 feet in a steep turn to the right and the approach controller transmitted: "I see you carrying out an orbit just tell me what i can do to help". The first officer replied: "Are we going straight at the moment sir" The controller informed him that the aircraft was at that time in a right hand turn but after observing further radar returns he said that it was then going straight on a south-easterly heading. The first officer's response to this transmission was: "Radar vectors slowly back to one four then sir please". The controller then ordered a right turn onto a heading of 340°. This instruction was correctly acknowledged by the first officer but the aircraft began a left hand turn with an initial angle of bank between 30° and 40°. This turn continued onto a heading of 360° when the first officer again asked "Are we going straight at the moment sir" to which the controller replied that the aircraft looked to be going straight. Seconds later the first officer asked: "Any report of the tops sir". This was the last recorded transmission from the aircraft, although at 17:52 hrs a brief carrier wave signal was recorded but it was obliterated by the controller's request to another departing aircraft to see if its pilot could help with information on the cloud tops. At this point, the aircraft had reached an altitude of 3,600 feet, having maintained a fairly constant rate of climb and airspeed. The ATC clearance to 3000 feet had not been amended. After the controller had confirmed that the aircraft appeared to be on a steady northerly heading, the aircraft immediately resumed its turn to the left and began to descend. The angle of bank increased to about 45° while the altitude reduced to 2,900 feet in about 25 seconds. As the aircraft passed a heading of 230° it ceased to appear on the secondary radar. There were four further primary radar returns before the aircraft finally disappeared from radar. There had been a recent thunderstorm in the area and it was raining intermittently with a cloud base of about 400 feet and a visibility of about 1,100 metres. Residents in the vicinity of the accident site reported dark and stormy conditions. Several witnesses described the engine noise as pulsating or surging and then fading just prior to impact. Other witnesses saw a fireball descending rapidly out of the low cloud base and one witness saw the aircraft in flames before it stuck the ground. All of the occupants died at impact. From subsequent examination it was apparent that, at a late stage in the descent, the aircraft had broken up, losing a large part of the right wing outboard of the engine, and the right horizontal stabiliser. There was some disruption of the fuselage before it struck the ground. The airborne structural failure that had occurred was the result of flight characteristics which were beyond the design limits of the aircraft following the loss of control shortly before impact.
Probable cause:
The following causal factors were identified:
- One or, possibly, both of the aircraft's artificial horizons malfunctioned and, in the absence of a standby horizon, for which there was no airworthiness requirement, there was no single instrument available for assured attitude reference or simple means of determining which flight instruments had failed.
- The commander, who was probably the handling pilot, was initially unable to control the aircraft's heading without his artificial horizon, and was eventually unable to retain control of the aircraft whilst flying in IMC by reference to other flight instruments.
- The aircraft went out of control whilst flying in turbulent instrument meteorological conditions and entered a spiral dive from which the pilot, who was likely to have become spatially disoriented, was unable to recover.
Final Report:

Crash of a Partenavia P.68B Observer near Tórshavn: 3 killed

Date & Time: Jul 6, 1987
Type of aircraft:
Operator:
Registration:
G-SPOT
Flight Type:
Survivors:
No
Schedule:
Aberdeen – Vágar
MSN:
15
YOM:
1981
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
On approach to Vágar Airport, the crew encountered poor weather conditions and limited visibility when the aircraft struck a rocky face (150 metres high) located 15 km southeast from the airport, near Tórshavn. All three occupants were killed.

Crash of a De Havilland DHC-6 Twin Otter 310 in Flotta

Date & Time: Apr 20, 1983 at 1300 LT
Operator:
Registration:
G-STUD
Survivors:
Yes
Schedule:
Aberdeen - Flotta
MSN:
545
YOM:
1977
Location:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
10
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9010
Captain / Total hours on type:
1503.00
Copilot / Total flying hours:
184
Copilot / Total hours on type:
100
Aircraft flight hours:
7000
Circumstances:
Strong winds were reported at Flotta as the Twin Otter approached Orkney Island. The aircraft first contacted the airport at 11:56, and was informed that the surface wind was indicating 260°/26 knots. The pilot accordingly elected to make a straight in approach to runway 35. The pilot preferred the cross-wind to come from his left-hand side, so that he could 'see' the left main wheel onto the runway. The aircraft touched down left main wheel first, then on the right main wheel and, as the nosewheel touched, the commander selected reverse thrust from the propellers. As the aircraft touched down, the audible stall warning sounded momentarily. Shortly after reverse thrust from the propellers had been selected and achieved, the aircraft’s left wing started to rise. The captain applied full left wing down aileron and full left rudder, then cancelling reverse thrust from the right-hand propeller and increasing forward power on that engine. However, he was still unable to prevent the left wing from rising further. The right-hand wing-tip contacted the ground, the aircraft yawed to the right and then fell back momentarily onto the main wheels before ‘cartwheeling’ through an aerodrome boundary fence and coming to rest on its left side, with both wings detached. All 12 occupants escaped uninjured while the airplane was damaged beyond repair.
Probable cause:
The accident was caused by a loss of control, shortly after touchdown, following a strong lateral gust which was in excess of the maximum cross-wind capability of the aircraft. The lack of accurate surface wind information at the runway threshold was a contributory factor.
Final Report:

Crash of an Avro 748-1-105 in Lerwick: 17 killed

Date & Time: Jul 31, 1979 at 1601 LT
Type of aircraft:
Operator:
Registration:
G-BEKF
Flight Phase:
Survivors:
Yes
Schedule:
Lerwick - Aberdeen
MSN:
1542
YOM:
1962
Flight number:
DA0034
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
44
Pax fatalities:
Other fatalities:
Total fatalities:
17
Captain / Total flying hours:
6487
Captain / Total hours on type:
4403.00
Copilot / Total flying hours:
4563
Copilot / Total hours on type:
57
Aircraft flight hours:
29007
Circumstances:
The aircraft was engaged on a series of charter flights, carrying oil company personnel between Aberdeen, Scotland and Sumburgh, Shetland Islands. The inbound flight to Sumburgh had been made without incident and no significant malfunction of the aircraft had been reported. The crew, consisting of two pilots and a stewardess, then had a stopover of nearly seven hours before departing on the return flight, Dan-Air 0034, with 44 passengers on board. It has not been established who was the handling pilot on this sector. At 15:48 hrs, in conditions of moderate visibility, but with low cloud, rain and a fresh easterly wind, the aircraft was taxied out to the holding point 'India', the intersection of the disused runway and runway 15/33. Meanwhile the stewardess gave the company's standard safety briefing, using a megaphone because the passenger address (PA) system was 'screeching'. The briefing included mention of the location of the lifejackets, how they should be put on, and the method of inflation; also mentioned was the location of the emergency exits. A diagram displaying the method of donning the jackets was fixed to the forward bulkhead of the cabin. Because of other aircraft movements, 'KF' was held at point 'India' for six minutes before being cleared, at 15:57 hrs, to 'enter and backtrack' for a take-off on runway 09, which was virtually into wind. Whilst the aircraft was backtracking, ATC passed the crew the en route clearance, which was read back correctly by the co-pilot. The aircraft was seen to turn close to the western end of the runway and line up on the runway heading. At 15:59 hrs the flight received take-off clearance from ATC and this was acknowledged by the co-pilot. There is evidence to show that the engines were accelerated whilst the aircraft was held stationary on the brakes and that full take-off power, using watermethanol, was achieved on the take-off run, which commenced at almost exactly 16:00 hrs. Evidence from the aircraft's Flight Data Recorder (FDR) shows that the aircraft accelerated normally through the decision speed, V1 (92 kts), to the rotation and safety speed VR/2 (99 kts). No rotation was carried out and even though the aircraft reached a speed significantly higher than VR of the order of 113 kts, it failed to become airborne. About 5 seconds after reaching the scheduled rotation speed, and after passing the intersection with the disused runway, the aircraft began to decelerate. Veering gradually to the left as it crossed the grass overrun area, it then made contact with a discontinuity or 'step', approximately 40 centimetres high, at the edge of the airfield perimeter road and partial collapse of the undercarriage followed. After crossing the road in a left wing low and nose down attitude the aircraft passed over the inclined sea defences and came to rest in the sea some 50 metres from the shore line. The emergency services arrived at the point on the road adjacent to the crash site within two minutes of the accident. However, about a minute later the aircraft sank, nose first, in some ten metres of water, leaving only the rear section of the fuselage visible. Twenty-nine passengers and the stewardess were rescued, or managed to swim to the shore, under adverse weather conditions. Despite rescue attempts mounted from the shore, by small craft and by helicopters summoned to the scene, fifteen passengers and the two pilots died by drowning.
Probable cause:
It was concluded that the accident was caused by the locked condition of the elevators which prevented the rotation of the aircraft into a flying attitude. It is likely that the elevator gust-lock became re-engaged during the pilot's pre-take-off check, and that this condition was not apparent to either pilot until the take-off was so far advanced that a successful abandonment within the overrun area could not be reasonably have been made. The re-engagement of the gust-lock was made possible by the condition of the gust-lock lever gate plate and gate-stop strip.
Final Report:

Crash of a Britten-Norman BN-2A Trislander III-1 in Aberdeen

Date & Time: May 15, 1979
Type of aircraft:
Operator:
Registration:
G-BCYC
Survivors:
Yes
MSN:
1011
YOM:
1975
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Upon touchdown, the tree engine aircraft went out of control and came to halt. There were no casualties but the aircraft was written off.

Crash of an Airspeed AS.10 Oxford I in Lethnot: 2 killed

Date & Time: Aug 24, 1950
Type of aircraft:
Operator:
Registration:
PH311
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Turnhouse - Aberdeen
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The crew was performing a flight from RAF Turnhouse (Edinburgh) to Aberdeen-Dyce Airport. En route, while cruising in clouds, the twin engine aircraft hit the slope of Mt Crain Trench located near Lethnot. Both occupants were killed.
Crew (66 Grp CF):
F/Lt L. J. Waugh, Pilot.
Passenger:
S/Ldr A. L. Carrie.