Crash of a Beechcraft 200 Super King Air in Nairobi

Date & Time: Mar 26, 2021 at 1630 LT
Operator:
Registration:
5Y-NJS
Flight Type:
Survivors:
Yes
Schedule:
Nairobi – Kisumu – Eldoret – Nairobi
MSN:
BB-837
YOM:
1981
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6589
Captain / Total hours on type:
4600.00
Aircraft flight hours:
12177
Circumstances:
The aircraft, registered 5Y-NJS operated by Westwind Aviation Ltd crashed at Ngong Racecourse. The flight with two onboard was on a private mission to Kisumu, Eldoret and back to Nairobi. The aircraft departed Wilson Airport (HKNW) at 0420Z and landed at Kisumu Airport (HKKI) at 0502Z. It then departed HKKI to HKEL at 1142Z and landed at 1200Z where it picked one passenger. The flight then departed HKEL to HKNW with three onboard at 1247Z with an estimated flight time of 40 minutes. According to the preliminary information obtained from the Captain, the aircraft attained flight level 250 42NM from Eldoret VOR. The flight was then cleared to fly direct to GV VOR by Nairobi Area Control Centre. During descend to flight level 100 they encountered bad weather whereby the wings developed heavy icing. The Captain deployed deicing systems on the wings but the problem persisted. The situation prompted the Captain to request Wilson Control to descend to “Monstry fix” for landing at HKNW which was approved. As the flight continued descending the left engine went off. The Captain requested Wilson Tower for assistance. After 30 seconds, the right engine also went off. The Captain elected to make an emergency landing at Ngong Racecourse. On landing along, the left wing collided with trees and broke-off and separated together with the left engine and the left main landing gear. The turned clockwise through 180° and faced the opposite direction. All three onboard escaped unhurt but the aircraft was destroyed.

Crash of a Beechcraft 200 Super King Air in Rockford: 1 killed

Date & Time: Aug 20, 2020 at 1542 LT
Operator:
Registration:
N198DM
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Rockford - DuPage
MSN:
BB-1198
YOM:
1984
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3650
Aircraft flight hours:
8018
Circumstances:
On August 20, 2020, about 1542 central daylight time, a Beech B200 airplane (marketed as a King Air 200), N198DM, was destroyed when it was involved in an accident near Rockford, Illinois. The private pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations (CFR) Part 91 positioning flight. The purpose of the flight was to relocate the airplane to the pilot's home base at the DuPage Airport (DPA), West Chicago, Illinois. The airplane had been at Chronos Aviation, LLC (a 14 CFR Part 145 repair station), at the Rockford International Airport (RFD), Rockford, Illinois, for maintenance work. Multiple airport-based cameras recorded the accident sequence. The videos showed the airplane taking off from runway 19. Shortly after liftoff, the airplane started turning left, and the airplane developed a large left bank angle as it was turning. The airplane departed the runway to the left and impacted the ground. During the impact sequence, an explosion occurred, and there was a postimpact fire. A video study estimated the airplane’s maximum groundspeed during the takeoff as 105.5 knots (kts). Data recovered from an Appareo Stratus device onboard the airplane showed that about 1538, the airplane began taxing to runway 19. At 1540:34, the airplane crossed the hold short line for runway 19. At 1541:19, the airplane began a takeoff roll on runway 19. At 1541:42, the airplane began to depart the runway centerline to the left of the runway. Subsequent tracklog points showed the airplane gaining some altitude, and the tracklog terminated adjacent to a taxiway in a grassy area. The Appareo Stratus data showed the airplane began to increase groundspeed on a true heading of roughly 185° about 1541. Airplane pitch began to increase at 1541:41 as the groundspeed reached about 104 kts. The groundspeed increased to 107 kts within the next 2 seconds, and the pitch angle reached around 4° nose-up at this time. In the next few seconds, pitch lowered to around 0° as the groundspeed decayed to around 98 kts. The pitch then became 15° nose-up as the groundspeed continued to decay to about 95 kts. A right roll occurred of about 13° and changed to a rapidly increasing left roll over the next 5 seconds. The left roll reached a maximum of about 86° left as the pitch angle increasingly became negative (the airplane nosed down). The pitch angle reached a maximum nose down condition of -73°. The data became invalid after 1541:53.4. An airplane performance study based on the Appareo Stratus data showed that during the takeoff from runway 19, the airplane accelerated to a groundspeed of 98 kts and an airspeed of 105 kts before rotating and lifting off. The airplane pitched up, climbed, and gained height above the ground. Then, 4 seconds after rotation, the airplane began descending and slowing, consistent with a loss of power. A nose-left sideslip, a left side force, and a left roll were recorded, consistent with the loss or reduction in thrust of the left engine. The sideslip was reduced, likely due to opposite rudder input, and the airplane briefly rolled right. The airplane pitched up and was able to begin climbing again; however, it continued to lose speed. The sideslip then reversed, and the airplane rolled left again and impacted the ground. One witness reported that he observed the accident sequence. He did not hear any abnormal engine noises, nor did he see any smoke or flames emit from the airplane before impact. The airplane came to rest on a flat grass field to the east of runway 19 on airport property. The airplane sustained fire damage and was fragmented from impacting terrain.
Probable cause:
The pilot’s failure to maintain airplane control following a reduction of thrust in the left engine during takeoff. The reason for the reduction in thrust could not be determined based on the available evidence.
Final Report:

Crash of a Beechcraft B200 Super King Air near Brus Laguna

Date & Time: Jul 20, 2020
Operator:
Registration:
N740P
Flight Type:
Survivors:
Yes
MSN:
BB-1218
YOM:
1985
Country:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Engaged in an illegal flight, the twin engine airplane landed on a dirt road located about 35 km southwest of Brus Laguna. The nose gear collapsed and the aircraft came to rest, damaged beyond repair. No one was found on site and a load of 806 kilos of cocaine was seized.

Crash of a Beechcraft 200 Super King Air near Iriona: 2 killed

Date & Time: Mar 12, 2020
Operator:
Registration:
HK-5075
Flight Phase:
Flight Type:
Survivors:
No
Site:
MSN:
BB-801
YOM:
1981
Location:
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The twin engine aircraft was engaged in an illegal flight carrying two pilots and a probable load of cocaine bags. En route, the aircraft crashed in unknown circumstances in a prairie located in a mountainous area near Iriona. The aircraft disintegrated on impact and both occupants were killed.

Crash of a Beechcraft B200 Super King near Coleman: 3 killed

Date & Time: Feb 20, 2020 at 0600 LT
Operator:
Registration:
N860J
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Abilene – Harlingen
MSN:
BB-1067
YOM:
1982
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
5300
Circumstances:
The pilot and two passengers departed on an instrument flight rules cross-country flight in night instrument meteorological conditions (IMC). The pilot was instructed by air traffic control to climb to 12,000 ft, and then cleared to climb to FL230. The pilot reported to the controller that the airplane encountered freezing drizzle and light rime icing during the climb from 6,500 ft to 8,000 ft mean sea level (msl). As the airplane climbed through 11,600 ft msl, the pilot reported that they had an issue with faulty deicing equipment and needed to return to the airport. The controller instructed the pilot to descend and cleared the airplane back to the airport. When asked by the controller if there was an emergency, the pilot stated that they “blew a breaker,” and were unable to reset it. As the controller descended the airplane toward the airport, the pilot reported that they were having issues with faulty instruments. At this time, the airplane was at an altitude of about 4,700 ft. The controller instructed the pilot to maintain 5,000 ft, and the pilot responded that he was “pulling up.” There was no further communication with the pilot. Review of the airplane’s radar track showed the airplane’s departure from the airport and the subsequent turn and southeast track toward its destination. The track appeared as a straight line before a descending, right turn was observed. The turn radius decreased before the flight track ended. The airplane impacted terrain in a right-wing-low attitude. The wreckage was scattered and highly fragmented along a path that continued for about 570 ft. Examination of the wreckage noted various pieces of the flight control surfaces and cables in the wreckage path. Control continuity could not be established due the fragmentation of the wreckage; however, no preimpact anomalies were found. Examination of the left and right engines found rotational signatures and did not identify any pre-impact anomalies. A review of maintenance records noted two discrepancies with the propeller deice and surface deice circuit breakers, which were addressed by maintenance personnel. Impact damage and fragmentation prevented determination of which circuit breaker(s) the pilot was having issues with or an examination of any deicing systems on the airplane. The radio transmissions and transponder returns reflected in the radar data indicate that the airplane’s electrical system was operational before the accident. It is likely that the pilot’s communications with the controller and attempted troubleshooting of the circuit breakers introduced distractions from his primary task of monitoring the flight instruments while in IMC. Such interruptions would make him vulnerable to misleading vestibular cues that could adversely affect his ability to effectively interpret the instruments and maintain control of the airplane. The pilot’s report of “faulty instruments” during a decreasing radius turn and his initial distraction with the circuit breakers and radio communications is consistent with the effects of spatial disorientation.
Probable cause:
The pilot’s loss of airplane control due to spatial disorientation. Contributing to the accident was the pilot’s distraction with a “popped” circuit breaker and communications with air traffic control.
Final Report:

Crash of a Beechcraft B200 King Air off Dutch Harbor

Date & Time: Jan 16, 2020 at 0806 LT
Operator:
Registration:
N547LM
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Dutch Harbor - Adak
MSN:
BB-1642
YOM:
1998
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6470
Captain / Total hours on type:
756.00
Aircraft flight hours:
7058
Circumstances:
According to the pilot, when the airplane’s airspeed reached about 90 knots during the takeoff roll, he applied back pressure to the control yoke to initiate the takeoff and noted a brief positive rate of climb followed by a sinking sensation. The airspeed rapidly decayed, and the stall warning horn sounded. To correct for the decaying airspeed, he lowered the nose then pulled back on the airplane’s control yoke and leveled the wings just before impacting the ocean. The pilot stated there were no pre accident mechanical malfunctions or anomalies that would have precluded normal operation. Wind about the time of the accident was recorded as 110º downwind of the airplane at 15 knots gusting to 28 knots. The passengers recalled that the pilot’s preflight briefing mentioned the downwind takeoff but included no discussion of the potential effect of the wind conditions on the takeoff. The airplane’s estimated gross weight at the time of the accident was about 769.6 pounds over its approved maximum gross weight, and the airplane’s estimated center of gravity was about 8.24 inches beyond the approved aft limit at its maximum gross weight. It is likely that the pilot’s decision to takeoff downwind and operate the airplane over the maximum gross weight with an aft center of gravity led to the aerodynamic stall during takeoff and loss of control. Downwind takeoffs result in higher groundspeeds and increase takeoff distance. While excessive aircraft weight increases the takeoff distance and stability, and an aft center of gravity decreases controllability. Several instances of the operator’s noncompliance with its operational procedures and risk mitigations were discovered during the investigation, including two overweight flights, inaccurate and missing information on aircraft flight logs, and the accident pilot’s failure to complete a flight risk assessment for the accident flight. The operator had a safety management system (SMS) in place at the time of the accident that required active monitoring of its systems and processes to ensure compliance with internal and external requirements. However, the discrepancies noted with several flights, including the accident flight, indicate that the operator’s SMS program was inadequate to actively monitor, identify, and mitigate hazards and deficiencies.
Probable cause:
The pilot’s improper decision to takeoff downwind and to load the airplane beyond its allowable gross weight and center of gravity limits, which resulted in an aerodynamic stall and loss of control. Contributing to the accident was the inadequacy of the operator’s safety management system to actively monitor, identify, and mitigate hazards and deficiencies.
Final Report:

Ground accident of a Beechcraft 200 Super King Air in Fresno

Date & Time: Dec 18, 2019 at 0730 LT
Operator:
Registration:
N72MM
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
BB-497
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
9838
Circumstances:
Parked at Fresno-Yosemite Airport, the twin engine airplane was stolen by a teenager aged 17. She lost control of the airplane that collided with a fence and a building. The only occupant was uninjured and arrested. The aircraft was damaged beyond repair.
Probable cause:
No investigations were conducted by the NTSB on this event.